|
---|
Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20134C3421997-01-27027 January 1997 Special Rept:On 970110,improper Stack Monitor Calibr Occurred.Caused by Use of Flawed Procedure.Revised Q-2 Surveillance Data Sheet ML20116D9851996-07-24024 July 1996 14 Day Rept:On 960710,non-conservative Setting for Safety Channel 2 High Voltage Sensing Circuit Occurred.Caused by Failures in Safety Channel 2 High Sensing Circuit.Performed Successful Check of Sensing Circuit Loss of Voltage Setting ML20116D9921996-07-12012 July 1996 Ro:On 960711,Safety Channel 2 High Voltage Sensing Circuit Failed.Allowed Reactor to Sit Over Weekend & Planned to Restart ML20107L7481996-04-25025 April 1996 Ro:On 960404,failures in Safety Channel 2 High Voltage Sensing Circuits Resulted in Safety 2 Trip.Stated Resistors Replaced & Safety Channel 2 High Voltage Power Supply Temporarily Replaced W/Exact Duplicate on 960412 ML20107L7601996-04-0505 April 1996 Ro:On 960404,spurious Safety Channel 2 Loss of High Voltage Trip Occurred.Caused by Previously Undetected Matl Failure. Repairs Should Be Completed by 960410 & Restart Approved Subject to Successful post-repair Checks ML20086D1041995-06-30030 June 1995 Ro:On 950609,failure of Primary Coolant Return Line Flow Sensor to Initiate Trip Occurred.Flow Sensors Checked After Debris Removal & as of 950626 Problem Considered Resolved ML20091L2891995-06-12012 June 1995 Ro:On 950609,primary Coolant Flow Line Return Sensor Failed. Caused by Debris in Line.Line Repaired ML20082D0221995-04-0303 April 1995 Ro:On 950309-13,leakage of Coolant HX Occurred After Primary Coolant Resistivity Increase Noted.Primary & Secondary Flow Secured & Shell Side of HX Drained.No Leakage Collected.Hx Returned to Primary Sys & Placed in Operation ML20099H7641992-08-10010 August 1992 Ro:On 920727,temp Recorder Point 2 Noted to Be Reading Downscale,Indicating Failure in Circuit Monitoring Water Temp at Exit of South Ctr Fuel Box 2.Caused by Blockage in Fuel Box.Planned Maint Underway.Event Not Reportable ML20086H8081991-12-0303 December 1991 Final Ro:On 911119,safety Channel 2 Meter Flickered & Dropped Out Hard Downscale (Pegged).Caused by Intermitten Fault in Fine Adjust Potentiometer of Circuit. Poteniometer Replaced & Amplifier Card Reseated ML20086G2631991-11-27027 November 1991 Ro:Unscheduled Reactor Trip Occurred While Measuring Temp Coefficient of Reactivity.Caused by Secondary Cooling Water Dropping Below 8 Gpm Min Required by Limiting Safety Sys Setting.Cooling Water Logic Placed in City Water Mode ML20086H8151991-11-20020 November 1991 Ro:On 911120,unscheduled Shutdown Conducted Due to Failure of Safety Channel 2 Circuit on 911119.Possibly Caused by Problem in Safety Channel 2 Meter Circuit.Permission to Restart Not Yet Sought ML20086G2681991-11-19019 November 1991 Ro:Reactor Tripped on Loss of Secondary Cooling Flow on City Water & Gate Valve on City Water Flow Partially Closed to Allow Operation at Higher Temp.All Safety & Control Sys Functioned Properly.Detailed Rept Will Be Submitted ML20085H4911991-10-16016 October 1991 Ro:On 911003,failure to Perform Required Surveillance of Limiting Safety Sys Setting of Loss of Secondary Coolant Pump Power Discovered.Trip Check on Loss of Pump Power Incorporated Into Q-1 Quarterly Scram Checks ML20085H5071991-10-0303 October 1991 Ro:Possibility That Tests for Operability on Loss of Secondary Coolant Well Pump Power May Not Meet Tech Spec Surveillance Requirement 3.2.2(2) Discovered.Minutes of 911007 Executive Committee Meeting Encl ML20058F4281990-10-29029 October 1990 Ro:On 901002,three Reactor Startups Occurred W/O Performing Daily Checkout or Control Blade Interlock Checks Following Previous Shutdown ML20058F3481990-10-25025 October 1990 Ro:On 901025,three Reactor Startups Performed W/O Daily Checkout Being Performed within Required Time Interval,Per SOP SOP-A.2, Reactor Startup ML20248F1081989-09-29029 September 1989 Ro:On 890915 & 18,reactor Trips Occurred When Safety Channel 1 High Voltage Power Supply Dropped to 90% or Less of Rated Voltage.Caused by Instabilities in 15-volt Dc Power Supply. Trip Relays Replaced & Bistable Adjusted ML20244D5981989-03-31031 March 1989 Final Rept Re Higher than Expected High Streaming Radiation Levels Present at Vertical Ports During Full Power Operation.Caused by Inadequate Survey of Rabbit Shield on 870120.Extra Shielding Installed on Rabbit Sys Shield ML20244A7401989-03-31031 March 1989 Ro:On 890317,reactor Trip W/High Primary Coolant Temp Indication Occurred.Caused by Failure of Specific Temp Recorder Sys Due to Dust/Corrosion Buildup on Slide Wire Causing Excessive Resistance.Buildup Cleaned Off ML20235W6951989-02-21021 February 1989 Ro:On 890221,potential Failure to Rept Significant Change in Level 1 Administration Existed,Per Tech Spec 6.6.3. Evaluation Determined No Significant Administration Oversi Oversights Involved ML20206J7841988-11-14014 November 1988 Ro:On 881104,unscheduled Reactor Shutdown Occurred Due to Failure of Temp Recorder to Indicate Properly.Caused by Failure of Microswitch.Microswitch & Vacuum Tube Replaced & Calibr Check Performed ML20150B6821988-06-23023 June 1988 Ro:On 880610,clutch Current Indication Lamp for Control Blade safety-2 Burned Out at Full Power,Dropping Control Blade from 56% Withdrawn to Fully Inserted Position.Clutch Replaced & Lamp Replacement Frequency Increased ML20196A3661988-06-23023 June 1988 Ro:On 880610,control Blade Safety 2 Clutch Indicating Lamp Burned Out.Burned Out Clutch Current Indicating Bulb Replaced to Include Necessary Control Blade Drive & Drop Time Checks ML20195H8791988-06-0909 June 1988 Final Ro:On 880409,recurrence of Safety Channel 1 Circuit to Provide Proper Power Indication Occurred After Return to Normal Operations on 880401 Following Previous Failures on 880315 & 16.Caution Memo Issued to Operators ML20151W3711988-04-25025 April 1988 Ro:On 880321,0401 & 09,safety Channel 1 Failed to Bottom Meter Stop.Cause Not Yet Identified.New Program Developed to Isolate & Correct Cause of Failure ML20151B3681988-03-28028 March 1988 Reportable Occurrence:On 880314,safety Channel 1 Circuit Failed to Provide Proper Power Indication for Several Seconds on Two Occasions.Caused by Capacitor Failure. Capacitor Replaced W/Substitute of Different Mfg ML20148E8161988-03-15015 March 1988 Ro:On 880315,failure of Safety Channel 1 Circuit Occurred. Failed Component Replacement Has Restored Safety Channel 1 to Normal ML20209G7221987-04-13013 April 1987 Ro:On 870401,reactor Experienced Safety Channel 1 Trip. Caused by Operator Error.Rapid Recovery Restart Performed by Operator.Memorandum Issued Placing Restrictions on Automatic Operation & Limiting Removal of Regulating Blade ML20207J0321986-12-19019 December 1986 Ro:On 861211,actuation of Evacuation Alarm & Evacuation Alarm/Core Vent Sys Interlocks Occurred While Stack Count Rate Approx 300 Cps,In Potential Violation of Tech Specs. Cause Not Given.Vent Will Be Secured at 10 Cps During Drill ML20132B4241985-09-17017 September 1985 Ro:On 850904,one Control Blade Failed to Drop Fully Into Core on Demand from 64% Withdrawn Position.Probably Caused by Bearings Supporting Blade/Shaft Coupling or Magnesium Shroud housing-to-blade Clearance ML20132B4521985-09-0404 September 1985 Ro:On 850904,one Reactor Control Blade Failed to Drop on Demand from 64% Removed Position.Probably Caused by Binding in Clutch S-3 Possibly Due to Moisture or Other Effect Reducing Clearance 1997-01-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20207C0881998-12-31031 December 1998 Rev 11 to Uftr SAR, Consisting of Change Page 12-20 ML20217M6581998-03-27027 March 1998 Updated Proposal Submitted to NRC to Meet 10CFR50.64 Requirements for Updating Scheduling of Uftr Conversion from Heu to LEU Fuel ML20203C4551997-12-0303 December 1997 Safety Evaluation Supporting Amend 22 to License R-56 ML20216A8791997-08-31031 August 1997 Univ of Fl Training Reactor Annual Progress Rept for 960901-970813 ML20148G3561997-05-29029 May 1997 Univ of Fl Training Reactor Operator Requalification & Recertification Training Program Plan,Jul 1997-June 1999 ML20134C3421997-01-27027 January 1997 Special Rept:On 970110,improper Stack Monitor Calibr Occurred.Caused by Use of Flawed Procedure.Revised Q-2 Surveillance Data Sheet ML20137C1481996-12-31031 December 1996 195-96 Annual Progress Rept, Replacing Pages IV-6,IV-11 & IV-12 ML20128N4671996-10-10010 October 1996 Safety Evaluation Supporting Amend 21 to License R-56 ML20135D0081996-08-31031 August 1996 Univ of Fl Training Reactor Annual Progress Rept for 950901-960831 ML20116J5791996-08-0909 August 1996 Annual Progress Rept of Univ of Florida Training Reactor 940901-950831 ML20116D9851996-07-24024 July 1996 14 Day Rept:On 960710,non-conservative Setting for Safety Channel 2 High Voltage Sensing Circuit Occurred.Caused by Failures in Safety Channel 2 High Sensing Circuit.Performed Successful Check of Sensing Circuit Loss of Voltage Setting ML20116D9921996-07-12012 July 1996 Ro:On 960711,Safety Channel 2 High Voltage Sensing Circuit Failed.Allowed Reactor to Sit Over Weekend & Planned to Restart ML20107L7481996-04-25025 April 1996 Ro:On 960404,failures in Safety Channel 2 High Voltage Sensing Circuits Resulted in Safety 2 Trip.Stated Resistors Replaced & Safety Channel 2 High Voltage Power Supply Temporarily Replaced W/Exact Duplicate on 960412 ML20107L7601996-04-0505 April 1996 Ro:On 960404,spurious Safety Channel 2 Loss of High Voltage Trip Occurred.Caused by Previously Undetected Matl Failure. Repairs Should Be Completed by 960410 & Restart Approved Subject to Successful post-repair Checks ML20101L3491996-03-27027 March 1996 Updated Proposal Submitted to NRC to Meet 10CFR50.64 Requirements for Updating Scheduling of Uftr Conversion from HEU to LEU Fuel ML20086D1041995-06-30030 June 1995 Ro:On 950609,failure of Primary Coolant Return Line Flow Sensor to Initiate Trip Occurred.Flow Sensors Checked After Debris Removal & as of 950626 Problem Considered Resolved ML20091L2891995-06-12012 June 1995 Ro:On 950609,primary Coolant Flow Line Return Sensor Failed. Caused by Debris in Line.Line Repaired ML20082D0221995-04-0303 April 1995 Ro:On 950309-13,leakage of Coolant HX Occurred After Primary Coolant Resistivity Increase Noted.Primary & Secondary Flow Secured & Shell Side of HX Drained.No Leakage Collected.Hx Returned to Primary Sys & Placed in Operation ML20115B5881994-08-31031 August 1994 Annual Progress Rept of Univ of Fl Training Reactor for Sept 1993 - Aug 1994 ML20072P7141993-08-31031 August 1993 Annual Progress Rept of Univ of Fl Training Reactor for Sept 1992 - Aug 1993 ML20044G8351993-05-28028 May 1993 Revised, Operator Requalification & Recertification Training Program Plan of Univ of Florida Training Reactor, Jul 1993 Through June 1995. ML20069D0971992-08-31031 August 1992 Annual Progress Rept of Univ of Fl Training Reactor for Period 900901-910831 ML20099H7641992-08-10010 August 1992 Ro:On 920727,temp Recorder Point 2 Noted to Be Reading Downscale,Indicating Failure in Circuit Monitoring Water Temp at Exit of South Ctr Fuel Box 2.Caused by Blockage in Fuel Box.Planned Maint Underway.Event Not Reportable ML20094S4071992-04-30030 April 1992 Rev 7 to SAR Section 5.2 Re Secondary Cooling sys,9.2.3 Re Demineralized Water Makeup sys,9.2.4 Re Purification Sys & 9.2.5 Re Potable & Sanitary Water Sys ML20091C0451992-03-26026 March 1992 Updated Proposal Submitted to NRC to Meet 10CFR50.64 Requirements for Updating Scheduling of Univ of Florida Training Reactor Conversion from HEU to LEU Fuel ML20087A0521991-12-29029 December 1991 Rev 1 to Operator Requalification & Recertification Training Program Plan of Univ of Florida Training Reactor, Jul 1991 Through June 1993 ML20086H8081991-12-0303 December 1991 Final Ro:On 911119,safety Channel 2 Meter Flickered & Dropped Out Hard Downscale (Pegged).Caused by Intermitten Fault in Fine Adjust Potentiometer of Circuit. Poteniometer Replaced & Amplifier Card Reseated ML20086G2631991-11-27027 November 1991 Ro:Unscheduled Reactor Trip Occurred While Measuring Temp Coefficient of Reactivity.Caused by Secondary Cooling Water Dropping Below 8 Gpm Min Required by Limiting Safety Sys Setting.Cooling Water Logic Placed in City Water Mode ML20086H8151991-11-20020 November 1991 Ro:On 911120,unscheduled Shutdown Conducted Due to Failure of Safety Channel 2 Circuit on 911119.Possibly Caused by Problem in Safety Channel 2 Meter Circuit.Permission to Restart Not Yet Sought ML20086G2681991-11-19019 November 1991 Ro:Reactor Tripped on Loss of Secondary Cooling Flow on City Water & Gate Valve on City Water Flow Partially Closed to Allow Operation at Higher Temp.All Safety & Control Sys Functioned Properly.Detailed Rept Will Be Submitted ML20085H4911991-10-16016 October 1991 Ro:On 911003,failure to Perform Required Surveillance of Limiting Safety Sys Setting of Loss of Secondary Coolant Pump Power Discovered.Trip Check on Loss of Pump Power Incorporated Into Q-1 Quarterly Scram Checks ML20085H5071991-10-0303 October 1991 Ro:Possibility That Tests for Operability on Loss of Secondary Coolant Well Pump Power May Not Meet Tech Spec Surveillance Requirement 3.2.2(2) Discovered.Minutes of 911007 Executive Committee Meeting Encl ML20105B3751991-08-31031 August 1991 Annual Progress Rept of Univ of Florida Training Reactor, Sept 1990 - Aug 1991 ML20070T4061991-03-27027 March 1991 Updated Proposal Submitted to NRC to Meet 10CFR50.64 Requirements for Updating Scheduling of Univ of Florida Test Reactor Conversion from High Enriched U to Low Enriched U ML20058F4281990-10-29029 October 1990 Ro:On 901002,three Reactor Startups Occurred W/O Performing Daily Checkout or Control Blade Interlock Checks Following Previous Shutdown ML20058F3481990-10-25025 October 1990 Ro:On 901025,three Reactor Startups Performed W/O Daily Checkout Being Performed within Required Time Interval,Per SOP SOP-A.2, Reactor Startup ML20072S3761990-08-31031 August 1990 Annual Progress Rept of Univ of Florida Training Reactor, for Sept 1989 - Aug 1990 ML20248F1081989-09-29029 September 1989 Ro:On 890915 & 18,reactor Trips Occurred When Safety Channel 1 High Voltage Power Supply Dropped to 90% or Less of Rated Voltage.Caused by Instabilities in 15-volt Dc Power Supply. Trip Relays Replaced & Bistable Adjusted ML20006D5491989-08-31031 August 1989 Annual Progress Rept of Univ of Florida Training Reactor, Sept 1988 - Aug 1989. W/900207 Ltr ML20244A7401989-03-31031 March 1989 Ro:On 890317,reactor Trip W/High Primary Coolant Temp Indication Occurred.Caused by Failure of Specific Temp Recorder Sys Due to Dust/Corrosion Buildup on Slide Wire Causing Excessive Resistance.Buildup Cleaned Off ML20244D5981989-03-31031 March 1989 Final Rept Re Higher than Expected High Streaming Radiation Levels Present at Vertical Ports During Full Power Operation.Caused by Inadequate Survey of Rabbit Shield on 870120.Extra Shielding Installed on Rabbit Sys Shield ML20235W6951989-02-21021 February 1989 Ro:On 890221,potential Failure to Rept Significant Change in Level 1 Administration Existed,Per Tech Spec 6.6.3. Evaluation Determined No Significant Administration Oversi Oversights Involved ML20206J7841988-11-14014 November 1988 Ro:On 881104,unscheduled Reactor Shutdown Occurred Due to Failure of Temp Recorder to Indicate Properly.Caused by Failure of Microswitch.Microswitch & Vacuum Tube Replaced & Calibr Check Performed ML20196C0821988-08-31031 August 1988 Annual Progress Rept of Univ of Florida Training Reactor, Sept 1987 - Aug 1988 ML20196A3661988-06-23023 June 1988 Ro:On 880610,control Blade Safety 2 Clutch Indicating Lamp Burned Out.Burned Out Clutch Current Indicating Bulb Replaced to Include Necessary Control Blade Drive & Drop Time Checks ML20150B6821988-06-23023 June 1988 Ro:On 880610,clutch Current Indication Lamp for Control Blade safety-2 Burned Out at Full Power,Dropping Control Blade from 56% Withdrawn to Fully Inserted Position.Clutch Replaced & Lamp Replacement Frequency Increased ML20195H8791988-06-0909 June 1988 Final Ro:On 880409,recurrence of Safety Channel 1 Circuit to Provide Proper Power Indication Occurred After Return to Normal Operations on 880401 Following Previous Failures on 880315 & 16.Caution Memo Issued to Operators ML20151W8931988-04-27027 April 1988 Safety Evaluation Supporting Amend 17 to License R-56 ML20151W3711988-04-25025 April 1988 Ro:On 880321,0401 & 09,safety Channel 1 Failed to Bottom Meter Stop.Cause Not Yet Identified.New Program Developed to Isolate & Correct Cause of Failure ML20151B3681988-03-28028 March 1988 Reportable Occurrence:On 880314,safety Channel 1 Circuit Failed to Provide Proper Power Indication for Several Seconds on Two Occasions.Caused by Capacitor Failure. Capacitor Replaced W/Substitute of Different Mfg 1998-03-27
[Table view] |
Text
f sa r u. "- NUCLEAR FACILITIES DIVISION (m ca. %IRNET504, RE ACTOR M4N AGE R c ,n eq@g .
n NUCtEAR REACTOR BUILDING UNIVERSITY OF FLORD\ 'O .V ? .\
camwius.rtonion inii h . .
-- m mim nuu.m g N...#
Septembdr , 1985 Nuclear Regulatory Commission Suite 2900 101 Marietta Street, N.W.
Atlanta, Georgia 30323 Attention: J. Nelson Grace Regional Administrator, Region II Re: University of Florida Training Reactor Facility License: R-56, Docket No. 50-83 Gentlemen:
Pursuant to the reporting requirements of paragraph 6.6.2(3)(c) of the UFTR Technical Specifications, a description of a potential abnormal occurrence as defined in the UPTR Technical Specifications, Chapter 1 is described in this interim report to include NRC notification, occurrence scenario and proposed solutions. The potential abnormal occurrence involved the failure of one of the UFTR contral blades (Safety Blade #3) to drop fully into the core on de-mand from a 64% withdrawn position.
NRC Notification The Executive Committee of the Reactor Safety Review Subcommittee reviewed this occurrence on September 4, 1985 and concluded that it is a potential ab-normal occurrence as defined in UFTR Technical Specifications, Chapter 1. The RSRS then instructed NRC notification as per Section 6.6.2 of the UPTR Tech Specs. This notification was carried out by both telephone to Mr. Paul Frederickson and a following telecopy on September 4, 1985 (See Attacament I).
This interim report represents the 14 day followup report as required in UPTR Tech Specs, Paragraph 6.6.2 ( 3 ) ( c ) .
occurrence Scenario 8509260 PDR AD % h hPDR 83 S
As indicated in the telephone conversation with Mr. Paul Frederickson, Section Chief , Region II, and a following telecopy on 4 September 1985 ( Attachment I),
one of the reactor control blades (Safety-3) on the University of Florida Training Reactor failed to completely insert on demand from a 64% removed po-sition. This faili.re (sticking about 31% removed) was discovered by a Reactor Operator as he commenced a power increase from the 1 watt critical position where a complete set of readings are required to be entered into the daily operations log. The operator had accidentally raised the Safety-3 about 20 units instead of the Regulating Blade for this power increase; in returning it to the normal 640 unit position he felt the response was sluggish and so he attempted to drop the blade from 640 units withdrawn to check it. Following clutch current release the blade stopped at the 310 unit position and was sub-sequently driven in with the other three blades to shut the reactor down. The Facility Director and then the Reactor Manager were notified immediately of this occurrence. 'k EQUAL OPPORTUhsTV/ AFFIRM AflVE ACTION EMPL0tta
t Nuclear Regulatory Commission
. September 17, 1985 Page Two
.It should be noted that the most recent blade drop times performed on June 21, 1985 showed a slightly increased drop time from the values determined in March following previous maintenance work. However, the blade was dropped four times with consistent and successful drop times on each check. In addition, several trips, both unscheduled and for training, showed proper S-3 drop response over the several months prior to this occurrence.on September 3, 1985.
Immediate checks (with all other control blades fully inserted) involving sub-sequent removal to various heights showed this sticking problem to be inter-mittant and to center in the 290-315 unit range but with some possible slug-gishness in the drop from other higher and lower heights. It should be noted that this is essentially a recurrence of the event reported by our facility in a letter dated January 28, 1985 with subsequent followup in an interi.n report dated February 9, 1985 and closed out in a report dated March 26, 1985.
As indicated to Mr. Frederickson on September 4, 1985 and again on September 16,1985, .the need to formulate plans, make various checks 'and, as entry 'into the core region is required, to let the core and structure cool for a period, prevents a final report on this occurrence at 'this time. However, Mr.
Frederickson did advise the submission of an interim 14-day report and recom-mended including an update on the status of the problem. This update is pro-vided in this report.
Evaluation Evaluation and determination of the methods for alleviating this problem of a sticking control blade as well as preventing recurrence were discussed by the UPTR staff on September 4, 1985.
Essentially this event represents a recurrence of the previous sticking blade event so the staff reviewed and expanded upon those items considered at the January 31 staff meeting following the original S-3 problem where it was de-cided that potential blade drag points would include:
- 1. Inside gear boxes and/or bearings (previously identified as the cause of the January 28 problem),
- 2. Inside the blade shrouds perhaps due to tailed rivets, buckling or warpage of the shroud or the control blade,
- 3. shifted blade shaft / pedestal or bearing,
,4 . shifted blade shaft / drive unit or bearing, 1
l 5. Mechanical drag of ' the . blade shaf t in its guide channel.
It was agreed that all of'these possiblities.should be investigated in a sys-tematic program until the cause of the sticking blade is isolated, corrected and prevented from recurring.
I
. . * -- .rm., ,, -
w_ f --y- . - + . ,
o_ -
+ , , -# e., , c , .-~~w,. ..,--g,m,#--
Nuclear Regulatory Commission
! September 17, 1985 f Page Three t
The Executive Committee of the Reactor Safety Review Subcommittee (RSRS) was apprised of this occurrence on the day it happened and met to evaluate it on September 4, 1985. The decision was also made to put the UPTR on administra-tive shutdown with. limitations noted in Attachments II and III. As indicated, they recommended reporting the event. The entire RSRS considered the event in more detail at .its regular meeting on September 6,1985. In both cases, the RSRS concluded in -agreement with the facility administration that this poten-tial abnormal occurrence did not compromise the health and safety of the public. The blade has always responded properly to drive in to allow reactor shutdown. Required shutdown margin has always been available.
The RSRS agrees that all the possibilities listed above should be investigated in a systematic program to assure the cause of the sticking blade is isolated, corrected and prevented for recurring.
Work Progress To Date Following staff and RSRS evaluations, this sticking S-3 blade problem is being
' addressed in a series of planned maintenance / inspection checks beginning with the right angle gear box, drive motor, magnetic clutch, etc. external to the biological shield (designated ex-core meaning essentially environmental back-ground radiation levels) and working in toward the core regions where rela-tively high radiation levels are expected. Each planned maintenance / inspection activity or series of activities is described in a procedure or instruction discussed by the UPTR staff and administration prior to performance. It is then being reviewed and approved by the Executive Committee of the RSRS con-sisting of the RSRS Chairman, 'the Radiation Control Officer and the Reactor Manager prior to the start of work.
As of this date, the following maintenance has been performed:
- 1. Right angle drive gear box inspection has been performed with all compo-nents found to be functioning properly.
- 2. Bearings in right angle drive unit were inspected.and replaced since a small amount of rough operation was noted in or.e bearing. This roughness was not considered sufficient to be the source of the problem.
- 3. The shaft and connecting bearing were uncoupled from the blade drive unit and removed from the control blade. Both were inspected for scar marks with no significant problems noted.
- 4. The shaft penetration was cleaned - some oxidation and carbon products were removed but not considered sufficient to have been the cause of the problem.
- 5. The bearing and shaf t were reinstalled and recoupled, tte potentiometer was repositioned and blade drop and timing checks made.
,~ . .- _ - . . . _ . _.
l o .
1 I
Nuclear Regulatory Commission September 17, 1985 Page Four
- 6. Preliminary checks indicated the sticking problem is not cleared.
Conclusions To Date The problem has been isolated to within the biological shielding ,in the vicinity of the core reflector; most likely causes are a problem with the bearings supporting the blade /shaf t coupling or with the magnesium shroud housing-to-blade clearance either warpage, misalignment or loose rivets.
1 j Consequences As concluded by the RSRS Executive Committee, the full RSRS Committee and UFTR administration, this potential abnormal occurrence did not compromise the health and safety of the public. This occurrence was discovered at a low power condition. The Safety-3 blade drive system was always functional; and even with the S-3 blade at ~30-35% withdrawn, the UPTR core has a shutdown margin of ~347% Ak/k.
Followup Since further work will involve considerable radiation dose commitment, the core and structure has been allowed to cool while the above checks and main-tenance efforts were completed. A preliminary procedure to address the remain-ing in-core maintenance checks is nearly complete and will~ be presented to the RSRS Executive Committee for approval on September 18. Work to check and in-spect for the possible in-core sources of the problem and to perform main- ,
tenance where necessary and approved is expected to begin later this week.
Casutituent The UPTR administration with concurrence of the RSRS is committed not only to clear the sticking blade problem but also to obtain a significant reduction in
- the S-3 drop time. This reduction is considered necessary to preclude recur-rence of this . event. In addition, the UFTR administration has committed .to the RSRS to clear _any restart with NRC Region II prior to removing the facility 4 from the -current administrative shutdown.
( 0 Anl % l /f William G. Vernetson D6te Acting Director of Nuclear Facilities 4
WGV/ps Attachments cc: P.M. Whaley Reac' tor Safety Review Subcommittee.
. . _ . - _ _ , . _ _ _ _ _ _ _ . _ ~ .- . . , , , . . . _ _ _ . . _ - - . . . .