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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20134C3421997-01-27027 January 1997 Special Rept:On 970110,improper Stack Monitor Calibr Occurred.Caused by Use of Flawed Procedure.Revised Q-2 Surveillance Data Sheet ML20116D9851996-07-24024 July 1996 14 Day Rept:On 960710,non-conservative Setting for Safety Channel 2 High Voltage Sensing Circuit Occurred.Caused by Failures in Safety Channel 2 High Sensing Circuit.Performed Successful Check of Sensing Circuit Loss of Voltage Setting ML20116D9921996-07-12012 July 1996 Ro:On 960711,Safety Channel 2 High Voltage Sensing Circuit Failed.Allowed Reactor to Sit Over Weekend & Planned to Restart ML20107L7481996-04-25025 April 1996 Ro:On 960404,failures in Safety Channel 2 High Voltage Sensing Circuits Resulted in Safety 2 Trip.Stated Resistors Replaced & Safety Channel 2 High Voltage Power Supply Temporarily Replaced W/Exact Duplicate on 960412 ML20107L7601996-04-0505 April 1996 Ro:On 960404,spurious Safety Channel 2 Loss of High Voltage Trip Occurred.Caused by Previously Undetected Matl Failure. Repairs Should Be Completed by 960410 & Restart Approved Subject to Successful post-repair Checks ML20086D1041995-06-30030 June 1995 Ro:On 950609,failure of Primary Coolant Return Line Flow Sensor to Initiate Trip Occurred.Flow Sensors Checked After Debris Removal & as of 950626 Problem Considered Resolved ML20091L2891995-06-12012 June 1995 Ro:On 950609,primary Coolant Flow Line Return Sensor Failed. Caused by Debris in Line.Line Repaired ML20082D0221995-04-0303 April 1995 Ro:On 950309-13,leakage of Coolant HX Occurred After Primary Coolant Resistivity Increase Noted.Primary & Secondary Flow Secured & Shell Side of HX Drained.No Leakage Collected.Hx Returned to Primary Sys & Placed in Operation ML20099H7641992-08-10010 August 1992 Ro:On 920727,temp Recorder Point 2 Noted to Be Reading Downscale,Indicating Failure in Circuit Monitoring Water Temp at Exit of South Ctr Fuel Box 2.Caused by Blockage in Fuel Box.Planned Maint Underway.Event Not Reportable ML20086H8081991-12-0303 December 1991 Final Ro:On 911119,safety Channel 2 Meter Flickered & Dropped Out Hard Downscale (Pegged).Caused by Intermitten Fault in Fine Adjust Potentiometer of Circuit. Poteniometer Replaced & Amplifier Card Reseated ML20086G2631991-11-27027 November 1991 Ro:Unscheduled Reactor Trip Occurred While Measuring Temp Coefficient of Reactivity.Caused by Secondary Cooling Water Dropping Below 8 Gpm Min Required by Limiting Safety Sys Setting.Cooling Water Logic Placed in City Water Mode ML20086H8151991-11-20020 November 1991 Ro:On 911120,unscheduled Shutdown Conducted Due to Failure of Safety Channel 2 Circuit on 911119.Possibly Caused by Problem in Safety Channel 2 Meter Circuit.Permission to Restart Not Yet Sought ML20086G2681991-11-19019 November 1991 Ro:Reactor Tripped on Loss of Secondary Cooling Flow on City Water & Gate Valve on City Water Flow Partially Closed to Allow Operation at Higher Temp.All Safety & Control Sys Functioned Properly.Detailed Rept Will Be Submitted ML20085H4911991-10-16016 October 1991 Ro:On 911003,failure to Perform Required Surveillance of Limiting Safety Sys Setting of Loss of Secondary Coolant Pump Power Discovered.Trip Check on Loss of Pump Power Incorporated Into Q-1 Quarterly Scram Checks ML20085H5071991-10-0303 October 1991 Ro:Possibility That Tests for Operability on Loss of Secondary Coolant Well Pump Power May Not Meet Tech Spec Surveillance Requirement 3.2.2(2) Discovered.Minutes of 911007 Executive Committee Meeting Encl ML20058F4281990-10-29029 October 1990 Ro:On 901002,three Reactor Startups Occurred W/O Performing Daily Checkout or Control Blade Interlock Checks Following Previous Shutdown ML20058F3481990-10-25025 October 1990 Ro:On 901025,three Reactor Startups Performed W/O Daily Checkout Being Performed within Required Time Interval,Per SOP SOP-A.2, Reactor Startup ML20248F1081989-09-29029 September 1989 Ro:On 890915 & 18,reactor Trips Occurred When Safety Channel 1 High Voltage Power Supply Dropped to 90% or Less of Rated Voltage.Caused by Instabilities in 15-volt Dc Power Supply. Trip Relays Replaced & Bistable Adjusted ML20244D5981989-03-31031 March 1989 Final Rept Re Higher than Expected High Streaming Radiation Levels Present at Vertical Ports During Full Power Operation.Caused by Inadequate Survey of Rabbit Shield on 870120.Extra Shielding Installed on Rabbit Sys Shield ML20244A7401989-03-31031 March 1989 Ro:On 890317,reactor Trip W/High Primary Coolant Temp Indication Occurred.Caused by Failure of Specific Temp Recorder Sys Due to Dust/Corrosion Buildup on Slide Wire Causing Excessive Resistance.Buildup Cleaned Off ML20235W6951989-02-21021 February 1989 Ro:On 890221,potential Failure to Rept Significant Change in Level 1 Administration Existed,Per Tech Spec 6.6.3. Evaluation Determined No Significant Administration Oversi Oversights Involved ML20206J7841988-11-14014 November 1988 Ro:On 881104,unscheduled Reactor Shutdown Occurred Due to Failure of Temp Recorder to Indicate Properly.Caused by Failure of Microswitch.Microswitch & Vacuum Tube Replaced & Calibr Check Performed ML20150B6821988-06-23023 June 1988 Ro:On 880610,clutch Current Indication Lamp for Control Blade safety-2 Burned Out at Full Power,Dropping Control Blade from 56% Withdrawn to Fully Inserted Position.Clutch Replaced & Lamp Replacement Frequency Increased ML20196A3661988-06-23023 June 1988 Ro:On 880610,control Blade Safety 2 Clutch Indicating Lamp Burned Out.Burned Out Clutch Current Indicating Bulb Replaced to Include Necessary Control Blade Drive & Drop Time Checks ML20195H8791988-06-0909 June 1988 Final Ro:On 880409,recurrence of Safety Channel 1 Circuit to Provide Proper Power Indication Occurred After Return to Normal Operations on 880401 Following Previous Failures on 880315 & 16.Caution Memo Issued to Operators ML20151W3711988-04-25025 April 1988 Ro:On 880321,0401 & 09,safety Channel 1 Failed to Bottom Meter Stop.Cause Not Yet Identified.New Program Developed to Isolate & Correct Cause of Failure ML20151B3681988-03-28028 March 1988 Reportable Occurrence:On 880314,safety Channel 1 Circuit Failed to Provide Proper Power Indication for Several Seconds on Two Occasions.Caused by Capacitor Failure. Capacitor Replaced W/Substitute of Different Mfg ML20148E8161988-03-15015 March 1988 Ro:On 880315,failure of Safety Channel 1 Circuit Occurred. Failed Component Replacement Has Restored Safety Channel 1 to Normal ML20209G7221987-04-13013 April 1987 Ro:On 870401,reactor Experienced Safety Channel 1 Trip. Caused by Operator Error.Rapid Recovery Restart Performed by Operator.Memorandum Issued Placing Restrictions on Automatic Operation & Limiting Removal of Regulating Blade ML20207J0321986-12-19019 December 1986 Ro:On 861211,actuation of Evacuation Alarm & Evacuation Alarm/Core Vent Sys Interlocks Occurred While Stack Count Rate Approx 300 Cps,In Potential Violation of Tech Specs. Cause Not Given.Vent Will Be Secured at 10 Cps During Drill ML20132B4241985-09-17017 September 1985 Ro:On 850904,one Control Blade Failed to Drop Fully Into Core on Demand from 64% Withdrawn Position.Probably Caused by Bearings Supporting Blade/Shaft Coupling or Magnesium Shroud housing-to-blade Clearance ML20132B4521985-09-0404 September 1985 Ro:On 850904,one Reactor Control Blade Failed to Drop on Demand from 64% Removed Position.Probably Caused by Binding in Clutch S-3 Possibly Due to Moisture or Other Effect Reducing Clearance 1997-01-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20207C0881998-12-31031 December 1998 Rev 11 to Uftr SAR, Consisting of Change Page 12-20 ML20217M6581998-03-27027 March 1998 Updated Proposal Submitted to NRC to Meet 10CFR50.64 Requirements for Updating Scheduling of Uftr Conversion from Heu to LEU Fuel ML20203C4551997-12-0303 December 1997 Safety Evaluation Supporting Amend 22 to License R-56 ML20216A8791997-08-31031 August 1997 Univ of Fl Training Reactor Annual Progress Rept for 960901-970813 ML20148G3561997-05-29029 May 1997 Univ of Fl Training Reactor Operator Requalification & Recertification Training Program Plan,Jul 1997-June 1999 ML20134C3421997-01-27027 January 1997 Special Rept:On 970110,improper Stack Monitor Calibr Occurred.Caused by Use of Flawed Procedure.Revised Q-2 Surveillance Data Sheet ML20137C1481996-12-31031 December 1996 195-96 Annual Progress Rept, Replacing Pages IV-6,IV-11 & IV-12 ML20128N4671996-10-10010 October 1996 Safety Evaluation Supporting Amend 21 to License R-56 ML20135D0081996-08-31031 August 1996 Univ of Fl Training Reactor Annual Progress Rept for 950901-960831 ML20116J5791996-08-0909 August 1996 Annual Progress Rept of Univ of Florida Training Reactor 940901-950831 ML20116D9851996-07-24024 July 1996 14 Day Rept:On 960710,non-conservative Setting for Safety Channel 2 High Voltage Sensing Circuit Occurred.Caused by Failures in Safety Channel 2 High Sensing Circuit.Performed Successful Check of Sensing Circuit Loss of Voltage Setting ML20116D9921996-07-12012 July 1996 Ro:On 960711,Safety Channel 2 High Voltage Sensing Circuit Failed.Allowed Reactor to Sit Over Weekend & Planned to Restart ML20107L7481996-04-25025 April 1996 Ro:On 960404,failures in Safety Channel 2 High Voltage Sensing Circuits Resulted in Safety 2 Trip.Stated Resistors Replaced & Safety Channel 2 High Voltage Power Supply Temporarily Replaced W/Exact Duplicate on 960412 ML20107L7601996-04-0505 April 1996 Ro:On 960404,spurious Safety Channel 2 Loss of High Voltage Trip Occurred.Caused by Previously Undetected Matl Failure. Repairs Should Be Completed by 960410 & Restart Approved Subject to Successful post-repair Checks ML20101L3491996-03-27027 March 1996 Updated Proposal Submitted to NRC to Meet 10CFR50.64 Requirements for Updating Scheduling of Uftr Conversion from HEU to LEU Fuel ML20086D1041995-06-30030 June 1995 Ro:On 950609,failure of Primary Coolant Return Line Flow Sensor to Initiate Trip Occurred.Flow Sensors Checked After Debris Removal & as of 950626 Problem Considered Resolved ML20091L2891995-06-12012 June 1995 Ro:On 950609,primary Coolant Flow Line Return Sensor Failed. Caused by Debris in Line.Line Repaired ML20082D0221995-04-0303 April 1995 Ro:On 950309-13,leakage of Coolant HX Occurred After Primary Coolant Resistivity Increase Noted.Primary & Secondary Flow Secured & Shell Side of HX Drained.No Leakage Collected.Hx Returned to Primary Sys & Placed in Operation ML20115B5881994-08-31031 August 1994 Annual Progress Rept of Univ of Fl Training Reactor for Sept 1993 - Aug 1994 ML20072P7141993-08-31031 August 1993 Annual Progress Rept of Univ of Fl Training Reactor for Sept 1992 - Aug 1993 ML20044G8351993-05-28028 May 1993 Revised, Operator Requalification & Recertification Training Program Plan of Univ of Florida Training Reactor, Jul 1993 Through June 1995. ML20069D0971992-08-31031 August 1992 Annual Progress Rept of Univ of Fl Training Reactor for Period 900901-910831 ML20099H7641992-08-10010 August 1992 Ro:On 920727,temp Recorder Point 2 Noted to Be Reading Downscale,Indicating Failure in Circuit Monitoring Water Temp at Exit of South Ctr Fuel Box 2.Caused by Blockage in Fuel Box.Planned Maint Underway.Event Not Reportable ML20094S4071992-04-30030 April 1992 Rev 7 to SAR Section 5.2 Re Secondary Cooling sys,9.2.3 Re Demineralized Water Makeup sys,9.2.4 Re Purification Sys & 9.2.5 Re Potable & Sanitary Water Sys ML20091C0451992-03-26026 March 1992 Updated Proposal Submitted to NRC to Meet 10CFR50.64 Requirements for Updating Scheduling of Univ of Florida Training Reactor Conversion from HEU to LEU Fuel ML20087A0521991-12-29029 December 1991 Rev 1 to Operator Requalification & Recertification Training Program Plan of Univ of Florida Training Reactor, Jul 1991 Through June 1993 ML20086H8081991-12-0303 December 1991 Final Ro:On 911119,safety Channel 2 Meter Flickered & Dropped Out Hard Downscale (Pegged).Caused by Intermitten Fault in Fine Adjust Potentiometer of Circuit. Poteniometer Replaced & Amplifier Card Reseated ML20086G2631991-11-27027 November 1991 Ro:Unscheduled Reactor Trip Occurred While Measuring Temp Coefficient of Reactivity.Caused by Secondary Cooling Water Dropping Below 8 Gpm Min Required by Limiting Safety Sys Setting.Cooling Water Logic Placed in City Water Mode ML20086H8151991-11-20020 November 1991 Ro:On 911120,unscheduled Shutdown Conducted Due to Failure of Safety Channel 2 Circuit on 911119.Possibly Caused by Problem in Safety Channel 2 Meter Circuit.Permission to Restart Not Yet Sought ML20086G2681991-11-19019 November 1991 Ro:Reactor Tripped on Loss of Secondary Cooling Flow on City Water & Gate Valve on City Water Flow Partially Closed to Allow Operation at Higher Temp.All Safety & Control Sys Functioned Properly.Detailed Rept Will Be Submitted ML20085H4911991-10-16016 October 1991 Ro:On 911003,failure to Perform Required Surveillance of Limiting Safety Sys Setting of Loss of Secondary Coolant Pump Power Discovered.Trip Check on Loss of Pump Power Incorporated Into Q-1 Quarterly Scram Checks ML20085H5071991-10-0303 October 1991 Ro:Possibility That Tests for Operability on Loss of Secondary Coolant Well Pump Power May Not Meet Tech Spec Surveillance Requirement 3.2.2(2) Discovered.Minutes of 911007 Executive Committee Meeting Encl ML20105B3751991-08-31031 August 1991 Annual Progress Rept of Univ of Florida Training Reactor, Sept 1990 - Aug 1991 ML20070T4061991-03-27027 March 1991 Updated Proposal Submitted to NRC to Meet 10CFR50.64 Requirements for Updating Scheduling of Univ of Florida Test Reactor Conversion from High Enriched U to Low Enriched U ML20058F4281990-10-29029 October 1990 Ro:On 901002,three Reactor Startups Occurred W/O Performing Daily Checkout or Control Blade Interlock Checks Following Previous Shutdown ML20058F3481990-10-25025 October 1990 Ro:On 901025,three Reactor Startups Performed W/O Daily Checkout Being Performed within Required Time Interval,Per SOP SOP-A.2, Reactor Startup ML20072S3761990-08-31031 August 1990 Annual Progress Rept of Univ of Florida Training Reactor, for Sept 1989 - Aug 1990 ML20248F1081989-09-29029 September 1989 Ro:On 890915 & 18,reactor Trips Occurred When Safety Channel 1 High Voltage Power Supply Dropped to 90% or Less of Rated Voltage.Caused by Instabilities in 15-volt Dc Power Supply. Trip Relays Replaced & Bistable Adjusted ML20006D5491989-08-31031 August 1989 Annual Progress Rept of Univ of Florida Training Reactor, Sept 1988 - Aug 1989. W/900207 Ltr ML20244A7401989-03-31031 March 1989 Ro:On 890317,reactor Trip W/High Primary Coolant Temp Indication Occurred.Caused by Failure of Specific Temp Recorder Sys Due to Dust/Corrosion Buildup on Slide Wire Causing Excessive Resistance.Buildup Cleaned Off ML20244D5981989-03-31031 March 1989 Final Rept Re Higher than Expected High Streaming Radiation Levels Present at Vertical Ports During Full Power Operation.Caused by Inadequate Survey of Rabbit Shield on 870120.Extra Shielding Installed on Rabbit Sys Shield ML20235W6951989-02-21021 February 1989 Ro:On 890221,potential Failure to Rept Significant Change in Level 1 Administration Existed,Per Tech Spec 6.6.3. Evaluation Determined No Significant Administration Oversi Oversights Involved ML20206J7841988-11-14014 November 1988 Ro:On 881104,unscheduled Reactor Shutdown Occurred Due to Failure of Temp Recorder to Indicate Properly.Caused by Failure of Microswitch.Microswitch & Vacuum Tube Replaced & Calibr Check Performed ML20196C0821988-08-31031 August 1988 Annual Progress Rept of Univ of Florida Training Reactor, Sept 1987 - Aug 1988 ML20196A3661988-06-23023 June 1988 Ro:On 880610,control Blade Safety 2 Clutch Indicating Lamp Burned Out.Burned Out Clutch Current Indicating Bulb Replaced to Include Necessary Control Blade Drive & Drop Time Checks ML20150B6821988-06-23023 June 1988 Ro:On 880610,clutch Current Indication Lamp for Control Blade safety-2 Burned Out at Full Power,Dropping Control Blade from 56% Withdrawn to Fully Inserted Position.Clutch Replaced & Lamp Replacement Frequency Increased ML20195H8791988-06-0909 June 1988 Final Ro:On 880409,recurrence of Safety Channel 1 Circuit to Provide Proper Power Indication Occurred After Return to Normal Operations on 880401 Following Previous Failures on 880315 & 16.Caution Memo Issued to Operators ML20151W8931988-04-27027 April 1988 Safety Evaluation Supporting Amend 17 to License R-56 ML20151W3711988-04-25025 April 1988 Ro:On 880321,0401 & 09,safety Channel 1 Failed to Bottom Meter Stop.Cause Not Yet Identified.New Program Developed to Isolate & Correct Cause of Failure ML20151B3681988-03-28028 March 1988 Reportable Occurrence:On 880314,safety Channel 1 Circuit Failed to Provide Proper Power Indication for Several Seconds on Two Occasions.Caused by Capacitor Failure. Capacitor Replaced W/Substitute of Different Mfg 1998-03-27
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UNIVERSITY OF -
FLORIDA Nuclear Reactor Facility 202 Nuclear Sciences Center Department of Nuclear Engineering Sciences P.O. Box 118300 Gainesville, Florida 32611-8300 L Tel: (904) 392-1429 ;
Fax: (904) 392-3380 April 3,1995 i
14 Day Report:
Leakage ofPrimary Coolant Heat Exchanger Regional Administrator, Region II U.S. Nuclear Regulatory Commission t 101 Marietta Street, N.W., Suite 2900 Atlanta, GA 30323
Dear Sir:
Re: University of Florida Training Reactor .
Facility License: R-56, Docket No. 50-83 Pursuant to the reporting requirements of paragraph 6.6.2(g) of the UFTR Technical Specifications, a description of what was originally considered a potential violation of the Technical Specifications was reported by telephone /telecopy (Attachment I) on March 14,1995 and a 14 day written report is submitted with this letter including occurrence scenario, NRC ,
notification, evaluation of consequences, corrective action and current status. The potentially promptly reportable occurrence involved the decrease of primary coolant resistivity, originally leading management to hypothesize a leakage of the primary coolant heat exchanger. This 14 day written report is delayed one week per agreement with Mr. Ed McAlpine of Region II !
in a telephone conversation notifying of plans to restart.
Scenario On March 9,1995, a one-hour full power run concluded at 1416 hours0.0164 days <br />0.393 hours <br />0.00234 weeks <br />5.38788e-4 months <br /> with all indications normal. At 1715 hours0.0198 days <br />0.476 hours <br />0.00284 weeks <br />6.525575e-4 months <br />, Reactor Manager D. Simpkins and SRO D. Cronin observed a red indicating light on the Primary Coolant Resistivity Solu-Bridge. Upon investigation, the primary coolant resistivity was found to be 0.25 MD-cm. This was thought to be a potential crud burst ,
I from the reactor operation at full power since a calorimetric had been performed the previous day and power adjusted. As is standard practice, the well water secondary cooling was secured and the city water cooling initiated. On March 10,1995, at 0915 hours0.0106 days <br />0.254 hours <br />0.00151 weeks <br />3.481575e-4 months <br /> SRO D. Cronin informed the Reactor Manager (at home) and the Facility Director the primary coolant l demineralizer inlet resistivity was 0.5MD-cm, while outlet resistivity was 1.2MD-cm. Normal Il 9504070247 950403 PDR ADOCK 05000083 S PDR ;
Equal opponunity/Amrnudvs Acdon inadtudon
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,Regiorial Administrator, NRC Region II Page 2 i April 3,1995 l l
levels are 1.0MO-cm or higher. Pit radiation levels were verified to be normal, and a primary pit entry was performed to obtain a primary coolant grab sample. Portable resistivity meter !
readings were 0.6MD-cm, correlating with the in-line solu-bridge. At 1115 hours0.0129 days <br />0.31 hours <br />0.00184 weeks <br />4.242575e-4 months <br />, the primary resistivity was reported as 0.7MD-cm. The concern at this point was that there could be a fuel element leak. At 1215 hours0.0141 days <br />0.338 hours <br />0.00201 weeks <br />4.623075e-4 months <br />, primary resistivity had increased to 0.8M0-cm and was continuing to rise. Gamma spectroscopy with HPGe detectors indicated the normally present Na-24, but no other radioisotopes, including fission products, were detected. Gross #Sy activity was j 7.46x104 Ci/ml, while alpha activity was less than the lower limit of detection (LLD) for the !
system used. These values are normal, indicating the resistivity problem was new and ;
apparently had not occurred during operations to provide significant activation levels. At 1500 l hours, primary resistivity had increased to 0.9MO-cm, and outlet resistivity had remained at !
1.2MD-cm. Primary and secondary cooling was secured for the weekend, but demineralizer flow was left in the normally-on condition with the problem apparently alleviated. 1 On Monda , March 13,1995, the weekly preoperational checks were performed. The primary inlet and outlet resistivities were 1.3MD-cm, verified by portable resisdvity meter checks.
Primary and secondary flow was secured at 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br /> upon satisfactorily completing weekly and daily checks prior to normal operations. At 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br />, well water secondary cooling was initiated to determine if the secondary water would cause a decrease in primary resistivity with demineralizer flow only. At 1200 hours0.0139 days <br />0.333 hours <br />0.00198 weeks <br />4.566e-4 months <br />, primary flow was established to expedite any decrease in primary resistivity. At 1235 hours0.0143 days <br />0.343 hours <br />0.00204 weeks <br />4.699175e-4 months <br />, primary resistivity decreased to 0.8MD-cm, and secondary cooling was secured. Primary flow was left in operation to facilitate coolant cleanup.
At 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />, primary resistivity was 0.7MO-cm, and MLP #95-12 (Primary Coolant Resistivity Drop) was opened and the gate valves for the city water supply, the well water supply and the heat exchanger drain were isolated. Primary and demineralizer flow was also secured until further investigations could be performed since a heat exchanger leak was now suspected.
Primary Coolant Storage Tank levels were compared to recent weekly survey results and found to be consistent indicating limited if any in or out leakage. Water samples from the Secondary Sample Tank were analyzed with negative results indicating no environmental effects ifleakage had occurred.
At this point the Reactor Safety Review Subcommittee (RSRS) Executive Committee convened to review the occurrence. The fact of no fuelleakage and the verification of apparent heat exchanger leakage on March 13, 1995 and its possible prompt reportability per UFTR Tech Specs Section 6.6.2 Special Reports, Paragraph (1) and Paragraph (3)(c) was discussed. It was noted that preliminary radioactivity measurements and surveys did not indicate there had been a release of radioactivity to the environment based on secondary side heat exchanger and sample l tank measurements; however, there was thought to possibly be a " degradation in the coolant l boundary." Because secondary pressure is higher on both secondary systems (well or city water), any leakage should have been into the primary when the secondary was running. Since I
Regional Administrator, NRC Region II
'Page 3 April 3,1995 the decrease in resistivity occurred nearly three hours after the last operation and since the primary sample was free of unexpected radionuclides, it was noted that this is clearly a new problem and not one that was occurring during reactor operations which had been suspended until the heat exchanger would be returned to service. It was noted that all flow systems were secured along with block valves on March 13, 1995 to assure no leakage from the primary system though the primary coolant storage tank level was noted to be commensurate with expected levels and the primary coolant resistivity decreases rather slowly and the demineralizer continues to have output with resistivity in excess of 1.0 megohm-cm, all indicating any leak would apparently be small.
The committee also reviewed planned actions and approved proceeding as follows:
- 1. Check the heat exchanger and confirm maximum leakage rate; then confirm leakage by pressure test if necessary.
- 2. Assuming a leak is confirmed, determine whether we can implement repairs. If yes, then proceed. If no, then check on getting it fixed or probably replacing it with a 10 CFR 50.59 evaluation and determination needed since the company who made this heat exchanger is no longer in business and it has been in service close to 20 years and is N-stamped.
During the meeting, prompt notification of the NRC was recommended.
NRC Notification After the RSRS Executive Committee meeting on March 14,1995, NRC Region II was informed of this event per a telephone conversation on March 14,1995 with Mr. Ed McAlpine relative I to the potential leak of the heat exchanger. The situation was confirmed in a following fax transmittal (Attachment I). At this time the potential failure was described and the key Tech Spec sections were reviewed. There was also agreement to treat the event as reportable.
In a subsequent conversation on March 24,1995, Mr. Ed McAlpine of Region II was updated on the system status including removal and replacement of the heat exchanger with no leaks i detected plus replacement of the demineralizer resins as a possible ionic source to the primary coolant with all systems verified operating properly and no resistivity problem noted. Later on ;
March 24, Mr. McAlpine was informed of plans to restart per the RSRS approval to introduce l temperature on the system and clean up any ionic contamination released as well as complete a radiation survey nearing its overdue date. Mr. McAlpine was informed of the expectation that there might be a resistivity drop upon restart since the system had been opened twice but it should recover quickly.
, Regional Administrator, NRC Region II Page 4 April 3,1995 Evaluation / Corrective Action To address a possible heat exchanger leak, Maintenance Log Page MLP #95-12 and Radiation Work Permit RWP 95-1-I were opened to investigate the primary coolant resistivity drop and to control testing of the Secondary Heat Exchanger for leakage. On March 15,1995, the shell side of the heat exchanger (secondary cooling supply) was drained and the primary system placed in operation. No leakage was collected from the tube (primary coolant) side. On 2 March 17,1995, the tube side of the heat exchanger (primary coolant supply) was drained and 4 the shell (secondary cooling) side was placed in operation with city water supplying. The drain valve on the shell side of the heat exchanger was closed to place city water pressure on the heat exchanger. No leakage was collected. The city water supply was then secured and the well pump placed in operation. At shut-off head, there was no leakage collected. The heat !
exchanger was then fully drained and removed from the system. On March 20,1995, the i secondary side of the heat exchanger was pressurized with 40 lbs. of nitrogen gas overnight with no decrease in pressure. On March 21,1995, the pressure was raised to 60 lbs., but with no pressure reduction over several hours. On March 22,1995, the heat exchanger was returned ;
to the primary system and placed in operation, with well water supplying secondary cooling.
On March 23,1995, the primary coolant inlet and outlet resistivities were normal at 1.0 MD-cm, i respectively. l After the heat exchanger was returned to the system, MLP #95-12 was utilized along with a newly opened RWP 95-2-I to replace the primary demineralizer resins on March 23,1995, since this was the only other possible source for coolant contamination to decrease resistivity. After replacement of the resins, the system was closed up and all resistivity readings were noted to j be normal. Subsequently, a restart and operation at power was conducted with all indications )
normal and the coolant soon reaching 1.3MO-cm resistivity on the inlet to the demineralizer system. ;
1 l
Current Status /Consecuences Following successful testing of the heat exchanger and demineralizer resin replacement, this problem is considered resolved. The system is operating normally. The source of the resistivity j drop is not known but suspected to be some sort of release from the demineralizer resins which !'
had been in service for over four years.
As indicated, the RSRS Executive Committee met on March 14,1995 to review this event and then again on March 23,1995 to approve restart operations after checks were negative on the heat exchanger and the primary coolant resins were replaced. The Committee essentially agreed with actions taken and with the initial staff evaluation that the occurrence did represent a potential violation of the UFTR Technical Specifications and was promptly reportable if a heat exchanger leak were involved. After this possibility was eliminated, the event is likely not
e a.
. /' q J
t
. Regional Administrator, NRC Region II [
Page 5 ,
April 3,1995 i
promptly reportable. Reactor Management and the RSRS Executive Committee agree there has :
been no significant compromise to reactor safety in the occurrence and no impact on the health j and safety of the public. Other than considering the event in the next regular RSRS meeting, this occurrence is now considered closed.
If further information is needed, please advise. j Sincerely, M
William G. Vernetson I Director of Nuclear Facilities WGV/dms [
Attachment .
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Copies: U.S. NRC Document Control Desk Ted S. Michaels, NRC Project Manager Reactor Safety Review Subcommittee !
D. Simpkins, Reactor Manager .
i l
Sworn and subscribed this dut day of April,1995.
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DN MOREHOUSE I i
WY COWASSION 8 CC302416 EXPlRES August 27.1997 soNoto mnote em esVMNCE,NC i
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, UNIVERSITY OF FLORIDA Nuclear Reactor Facility 202 Nuclear Sciences Center Department of Nuclear Engineering Sciences P.O. Box 118300 Gainesville, Florida 32611-8300 Teh (904) 392-1429 Fax: (904) 392-3380 March 14,1995 U.S. Nuclear Regulatory Commission Potential Tech Spec Violation -
Region II Irakage of Primary Coolant 101 Marietta Street, N.W., Suite 2900 Heat Exchanger Atlanta, GA 30323 Attention: Stewart Ebneter, Regional Admmistrator Re: University of Florida Training Reactor Facility License: R-56, Docket No. 50-83 As per the telephone conversation of March 14,1995 with Mr. Ed McAlpine relative to a probable leakage of our primary coolant heat exchanger on March 9,1995 with probable verification on March 13,1995, we have concluded this occurrence is a potential abnormal occurrence and a potentially reportable occurrence per UFTR Technical Specifications, Section 6.6.2 delineating requirements for special reports. The RSRS Executive Committee has met and recommended NRC notification as per Section 6.6,2 of the UFTR Tech Specs as a potentially promptly reportable occurrence. Initial evaluation indicates the heat exchanger has a smallleak due to decreasing resistivity of the primary coolant registered when the secondary coolant is flowing. Preliminary radioactivity measurements and surveys do not indicate that there has been a release of radioactivity to the environment. It should be noted that the reactor has not been run since this problem was noted and was discove' r ed during a shutdown period on Mzrch 9, 1995.
Sincerely,
\ -
William . Vernetson Director of Nuclear Facilities WGV/dms p%, ,o Copies: D. Simpkins -
' ~ " "T r r 7, RSRS Sworn and subscribed this 17 day of March,1995.
JOAN MOREHOUSE (L%u , ,
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MY cowx5 son a CC3 416 EXPIRES M us:27.1997 Notary %blic Equal Oppor' unity /Affirmatis e Action Institution