|
---|
Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20134C3421997-01-27027 January 1997 Special Rept:On 970110,improper Stack Monitor Calibr Occurred.Caused by Use of Flawed Procedure.Revised Q-2 Surveillance Data Sheet ML20116D9851996-07-24024 July 1996 14 Day Rept:On 960710,non-conservative Setting for Safety Channel 2 High Voltage Sensing Circuit Occurred.Caused by Failures in Safety Channel 2 High Sensing Circuit.Performed Successful Check of Sensing Circuit Loss of Voltage Setting ML20116D9921996-07-12012 July 1996 Ro:On 960711,Safety Channel 2 High Voltage Sensing Circuit Failed.Allowed Reactor to Sit Over Weekend & Planned to Restart ML20107L7481996-04-25025 April 1996 Ro:On 960404,failures in Safety Channel 2 High Voltage Sensing Circuits Resulted in Safety 2 Trip.Stated Resistors Replaced & Safety Channel 2 High Voltage Power Supply Temporarily Replaced W/Exact Duplicate on 960412 ML20107L7601996-04-0505 April 1996 Ro:On 960404,spurious Safety Channel 2 Loss of High Voltage Trip Occurred.Caused by Previously Undetected Matl Failure. Repairs Should Be Completed by 960410 & Restart Approved Subject to Successful post-repair Checks ML20086D1041995-06-30030 June 1995 Ro:On 950609,failure of Primary Coolant Return Line Flow Sensor to Initiate Trip Occurred.Flow Sensors Checked After Debris Removal & as of 950626 Problem Considered Resolved ML20091L2891995-06-12012 June 1995 Ro:On 950609,primary Coolant Flow Line Return Sensor Failed. Caused by Debris in Line.Line Repaired ML20082D0221995-04-0303 April 1995 Ro:On 950309-13,leakage of Coolant HX Occurred After Primary Coolant Resistivity Increase Noted.Primary & Secondary Flow Secured & Shell Side of HX Drained.No Leakage Collected.Hx Returned to Primary Sys & Placed in Operation ML20099H7641992-08-10010 August 1992 Ro:On 920727,temp Recorder Point 2 Noted to Be Reading Downscale,Indicating Failure in Circuit Monitoring Water Temp at Exit of South Ctr Fuel Box 2.Caused by Blockage in Fuel Box.Planned Maint Underway.Event Not Reportable ML20086H8081991-12-0303 December 1991 Final Ro:On 911119,safety Channel 2 Meter Flickered & Dropped Out Hard Downscale (Pegged).Caused by Intermitten Fault in Fine Adjust Potentiometer of Circuit. Poteniometer Replaced & Amplifier Card Reseated ML20086G2631991-11-27027 November 1991 Ro:Unscheduled Reactor Trip Occurred While Measuring Temp Coefficient of Reactivity.Caused by Secondary Cooling Water Dropping Below 8 Gpm Min Required by Limiting Safety Sys Setting.Cooling Water Logic Placed in City Water Mode ML20086H8151991-11-20020 November 1991 Ro:On 911120,unscheduled Shutdown Conducted Due to Failure of Safety Channel 2 Circuit on 911119.Possibly Caused by Problem in Safety Channel 2 Meter Circuit.Permission to Restart Not Yet Sought ML20086G2681991-11-19019 November 1991 Ro:Reactor Tripped on Loss of Secondary Cooling Flow on City Water & Gate Valve on City Water Flow Partially Closed to Allow Operation at Higher Temp.All Safety & Control Sys Functioned Properly.Detailed Rept Will Be Submitted ML20085H4911991-10-16016 October 1991 Ro:On 911003,failure to Perform Required Surveillance of Limiting Safety Sys Setting of Loss of Secondary Coolant Pump Power Discovered.Trip Check on Loss of Pump Power Incorporated Into Q-1 Quarterly Scram Checks ML20085H5071991-10-0303 October 1991 Ro:Possibility That Tests for Operability on Loss of Secondary Coolant Well Pump Power May Not Meet Tech Spec Surveillance Requirement 3.2.2(2) Discovered.Minutes of 911007 Executive Committee Meeting Encl ML20058F4281990-10-29029 October 1990 Ro:On 901002,three Reactor Startups Occurred W/O Performing Daily Checkout or Control Blade Interlock Checks Following Previous Shutdown ML20058F3481990-10-25025 October 1990 Ro:On 901025,three Reactor Startups Performed W/O Daily Checkout Being Performed within Required Time Interval,Per SOP SOP-A.2, Reactor Startup ML20248F1081989-09-29029 September 1989 Ro:On 890915 & 18,reactor Trips Occurred When Safety Channel 1 High Voltage Power Supply Dropped to 90% or Less of Rated Voltage.Caused by Instabilities in 15-volt Dc Power Supply. Trip Relays Replaced & Bistable Adjusted ML20244D5981989-03-31031 March 1989 Final Rept Re Higher than Expected High Streaming Radiation Levels Present at Vertical Ports During Full Power Operation.Caused by Inadequate Survey of Rabbit Shield on 870120.Extra Shielding Installed on Rabbit Sys Shield ML20244A7401989-03-31031 March 1989 Ro:On 890317,reactor Trip W/High Primary Coolant Temp Indication Occurred.Caused by Failure of Specific Temp Recorder Sys Due to Dust/Corrosion Buildup on Slide Wire Causing Excessive Resistance.Buildup Cleaned Off ML20235W6951989-02-21021 February 1989 Ro:On 890221,potential Failure to Rept Significant Change in Level 1 Administration Existed,Per Tech Spec 6.6.3. Evaluation Determined No Significant Administration Oversi Oversights Involved ML20206J7841988-11-14014 November 1988 Ro:On 881104,unscheduled Reactor Shutdown Occurred Due to Failure of Temp Recorder to Indicate Properly.Caused by Failure of Microswitch.Microswitch & Vacuum Tube Replaced & Calibr Check Performed ML20150B6821988-06-23023 June 1988 Ro:On 880610,clutch Current Indication Lamp for Control Blade safety-2 Burned Out at Full Power,Dropping Control Blade from 56% Withdrawn to Fully Inserted Position.Clutch Replaced & Lamp Replacement Frequency Increased ML20196A3661988-06-23023 June 1988 Ro:On 880610,control Blade Safety 2 Clutch Indicating Lamp Burned Out.Burned Out Clutch Current Indicating Bulb Replaced to Include Necessary Control Blade Drive & Drop Time Checks ML20195H8791988-06-0909 June 1988 Final Ro:On 880409,recurrence of Safety Channel 1 Circuit to Provide Proper Power Indication Occurred After Return to Normal Operations on 880401 Following Previous Failures on 880315 & 16.Caution Memo Issued to Operators ML20151W3711988-04-25025 April 1988 Ro:On 880321,0401 & 09,safety Channel 1 Failed to Bottom Meter Stop.Cause Not Yet Identified.New Program Developed to Isolate & Correct Cause of Failure ML20151B3681988-03-28028 March 1988 Reportable Occurrence:On 880314,safety Channel 1 Circuit Failed to Provide Proper Power Indication for Several Seconds on Two Occasions.Caused by Capacitor Failure. Capacitor Replaced W/Substitute of Different Mfg ML20148E8161988-03-15015 March 1988 Ro:On 880315,failure of Safety Channel 1 Circuit Occurred. Failed Component Replacement Has Restored Safety Channel 1 to Normal ML20209G7221987-04-13013 April 1987 Ro:On 870401,reactor Experienced Safety Channel 1 Trip. Caused by Operator Error.Rapid Recovery Restart Performed by Operator.Memorandum Issued Placing Restrictions on Automatic Operation & Limiting Removal of Regulating Blade ML20207J0321986-12-19019 December 1986 Ro:On 861211,actuation of Evacuation Alarm & Evacuation Alarm/Core Vent Sys Interlocks Occurred While Stack Count Rate Approx 300 Cps,In Potential Violation of Tech Specs. Cause Not Given.Vent Will Be Secured at 10 Cps During Drill ML20132B4241985-09-17017 September 1985 Ro:On 850904,one Control Blade Failed to Drop Fully Into Core on Demand from 64% Withdrawn Position.Probably Caused by Bearings Supporting Blade/Shaft Coupling or Magnesium Shroud housing-to-blade Clearance ML20132B4521985-09-0404 September 1985 Ro:On 850904,one Reactor Control Blade Failed to Drop on Demand from 64% Removed Position.Probably Caused by Binding in Clutch S-3 Possibly Due to Moisture or Other Effect Reducing Clearance 1997-01-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20207C0881998-12-31031 December 1998 Rev 11 to Uftr SAR, Consisting of Change Page 12-20 ML20217M6581998-03-27027 March 1998 Updated Proposal Submitted to NRC to Meet 10CFR50.64 Requirements for Updating Scheduling of Uftr Conversion from Heu to LEU Fuel ML20203C4551997-12-0303 December 1997 Safety Evaluation Supporting Amend 22 to License R-56 ML20216A8791997-08-31031 August 1997 Univ of Fl Training Reactor Annual Progress Rept for 960901-970813 ML20148G3561997-05-29029 May 1997 Univ of Fl Training Reactor Operator Requalification & Recertification Training Program Plan,Jul 1997-June 1999 ML20134C3421997-01-27027 January 1997 Special Rept:On 970110,improper Stack Monitor Calibr Occurred.Caused by Use of Flawed Procedure.Revised Q-2 Surveillance Data Sheet ML20137C1481996-12-31031 December 1996 195-96 Annual Progress Rept, Replacing Pages IV-6,IV-11 & IV-12 ML20128N4671996-10-10010 October 1996 Safety Evaluation Supporting Amend 21 to License R-56 ML20135D0081996-08-31031 August 1996 Univ of Fl Training Reactor Annual Progress Rept for 950901-960831 ML20116J5791996-08-0909 August 1996 Annual Progress Rept of Univ of Florida Training Reactor 940901-950831 ML20116D9851996-07-24024 July 1996 14 Day Rept:On 960710,non-conservative Setting for Safety Channel 2 High Voltage Sensing Circuit Occurred.Caused by Failures in Safety Channel 2 High Sensing Circuit.Performed Successful Check of Sensing Circuit Loss of Voltage Setting ML20116D9921996-07-12012 July 1996 Ro:On 960711,Safety Channel 2 High Voltage Sensing Circuit Failed.Allowed Reactor to Sit Over Weekend & Planned to Restart ML20107L7481996-04-25025 April 1996 Ro:On 960404,failures in Safety Channel 2 High Voltage Sensing Circuits Resulted in Safety 2 Trip.Stated Resistors Replaced & Safety Channel 2 High Voltage Power Supply Temporarily Replaced W/Exact Duplicate on 960412 ML20107L7601996-04-0505 April 1996 Ro:On 960404,spurious Safety Channel 2 Loss of High Voltage Trip Occurred.Caused by Previously Undetected Matl Failure. Repairs Should Be Completed by 960410 & Restart Approved Subject to Successful post-repair Checks ML20101L3491996-03-27027 March 1996 Updated Proposal Submitted to NRC to Meet 10CFR50.64 Requirements for Updating Scheduling of Uftr Conversion from HEU to LEU Fuel ML20086D1041995-06-30030 June 1995 Ro:On 950609,failure of Primary Coolant Return Line Flow Sensor to Initiate Trip Occurred.Flow Sensors Checked After Debris Removal & as of 950626 Problem Considered Resolved ML20091L2891995-06-12012 June 1995 Ro:On 950609,primary Coolant Flow Line Return Sensor Failed. Caused by Debris in Line.Line Repaired ML20082D0221995-04-0303 April 1995 Ro:On 950309-13,leakage of Coolant HX Occurred After Primary Coolant Resistivity Increase Noted.Primary & Secondary Flow Secured & Shell Side of HX Drained.No Leakage Collected.Hx Returned to Primary Sys & Placed in Operation ML20115B5881994-08-31031 August 1994 Annual Progress Rept of Univ of Fl Training Reactor for Sept 1993 - Aug 1994 ML20072P7141993-08-31031 August 1993 Annual Progress Rept of Univ of Fl Training Reactor for Sept 1992 - Aug 1993 ML20044G8351993-05-28028 May 1993 Revised, Operator Requalification & Recertification Training Program Plan of Univ of Florida Training Reactor, Jul 1993 Through June 1995. ML20069D0971992-08-31031 August 1992 Annual Progress Rept of Univ of Fl Training Reactor for Period 900901-910831 ML20099H7641992-08-10010 August 1992 Ro:On 920727,temp Recorder Point 2 Noted to Be Reading Downscale,Indicating Failure in Circuit Monitoring Water Temp at Exit of South Ctr Fuel Box 2.Caused by Blockage in Fuel Box.Planned Maint Underway.Event Not Reportable ML20094S4071992-04-30030 April 1992 Rev 7 to SAR Section 5.2 Re Secondary Cooling sys,9.2.3 Re Demineralized Water Makeup sys,9.2.4 Re Purification Sys & 9.2.5 Re Potable & Sanitary Water Sys ML20091C0451992-03-26026 March 1992 Updated Proposal Submitted to NRC to Meet 10CFR50.64 Requirements for Updating Scheduling of Univ of Florida Training Reactor Conversion from HEU to LEU Fuel ML20087A0521991-12-29029 December 1991 Rev 1 to Operator Requalification & Recertification Training Program Plan of Univ of Florida Training Reactor, Jul 1991 Through June 1993 ML20086H8081991-12-0303 December 1991 Final Ro:On 911119,safety Channel 2 Meter Flickered & Dropped Out Hard Downscale (Pegged).Caused by Intermitten Fault in Fine Adjust Potentiometer of Circuit. Poteniometer Replaced & Amplifier Card Reseated ML20086G2631991-11-27027 November 1991 Ro:Unscheduled Reactor Trip Occurred While Measuring Temp Coefficient of Reactivity.Caused by Secondary Cooling Water Dropping Below 8 Gpm Min Required by Limiting Safety Sys Setting.Cooling Water Logic Placed in City Water Mode ML20086H8151991-11-20020 November 1991 Ro:On 911120,unscheduled Shutdown Conducted Due to Failure of Safety Channel 2 Circuit on 911119.Possibly Caused by Problem in Safety Channel 2 Meter Circuit.Permission to Restart Not Yet Sought ML20086G2681991-11-19019 November 1991 Ro:Reactor Tripped on Loss of Secondary Cooling Flow on City Water & Gate Valve on City Water Flow Partially Closed to Allow Operation at Higher Temp.All Safety & Control Sys Functioned Properly.Detailed Rept Will Be Submitted ML20085H4911991-10-16016 October 1991 Ro:On 911003,failure to Perform Required Surveillance of Limiting Safety Sys Setting of Loss of Secondary Coolant Pump Power Discovered.Trip Check on Loss of Pump Power Incorporated Into Q-1 Quarterly Scram Checks ML20085H5071991-10-0303 October 1991 Ro:Possibility That Tests for Operability on Loss of Secondary Coolant Well Pump Power May Not Meet Tech Spec Surveillance Requirement 3.2.2(2) Discovered.Minutes of 911007 Executive Committee Meeting Encl ML20105B3751991-08-31031 August 1991 Annual Progress Rept of Univ of Florida Training Reactor, Sept 1990 - Aug 1991 ML20070T4061991-03-27027 March 1991 Updated Proposal Submitted to NRC to Meet 10CFR50.64 Requirements for Updating Scheduling of Univ of Florida Test Reactor Conversion from High Enriched U to Low Enriched U ML20058F4281990-10-29029 October 1990 Ro:On 901002,three Reactor Startups Occurred W/O Performing Daily Checkout or Control Blade Interlock Checks Following Previous Shutdown ML20058F3481990-10-25025 October 1990 Ro:On 901025,three Reactor Startups Performed W/O Daily Checkout Being Performed within Required Time Interval,Per SOP SOP-A.2, Reactor Startup ML20072S3761990-08-31031 August 1990 Annual Progress Rept of Univ of Florida Training Reactor, for Sept 1989 - Aug 1990 ML20248F1081989-09-29029 September 1989 Ro:On 890915 & 18,reactor Trips Occurred When Safety Channel 1 High Voltage Power Supply Dropped to 90% or Less of Rated Voltage.Caused by Instabilities in 15-volt Dc Power Supply. Trip Relays Replaced & Bistable Adjusted ML20006D5491989-08-31031 August 1989 Annual Progress Rept of Univ of Florida Training Reactor, Sept 1988 - Aug 1989. W/900207 Ltr ML20244A7401989-03-31031 March 1989 Ro:On 890317,reactor Trip W/High Primary Coolant Temp Indication Occurred.Caused by Failure of Specific Temp Recorder Sys Due to Dust/Corrosion Buildup on Slide Wire Causing Excessive Resistance.Buildup Cleaned Off ML20244D5981989-03-31031 March 1989 Final Rept Re Higher than Expected High Streaming Radiation Levels Present at Vertical Ports During Full Power Operation.Caused by Inadequate Survey of Rabbit Shield on 870120.Extra Shielding Installed on Rabbit Sys Shield ML20235W6951989-02-21021 February 1989 Ro:On 890221,potential Failure to Rept Significant Change in Level 1 Administration Existed,Per Tech Spec 6.6.3. Evaluation Determined No Significant Administration Oversi Oversights Involved ML20206J7841988-11-14014 November 1988 Ro:On 881104,unscheduled Reactor Shutdown Occurred Due to Failure of Temp Recorder to Indicate Properly.Caused by Failure of Microswitch.Microswitch & Vacuum Tube Replaced & Calibr Check Performed ML20196C0821988-08-31031 August 1988 Annual Progress Rept of Univ of Florida Training Reactor, Sept 1987 - Aug 1988 ML20196A3661988-06-23023 June 1988 Ro:On 880610,control Blade Safety 2 Clutch Indicating Lamp Burned Out.Burned Out Clutch Current Indicating Bulb Replaced to Include Necessary Control Blade Drive & Drop Time Checks ML20150B6821988-06-23023 June 1988 Ro:On 880610,clutch Current Indication Lamp for Control Blade safety-2 Burned Out at Full Power,Dropping Control Blade from 56% Withdrawn to Fully Inserted Position.Clutch Replaced & Lamp Replacement Frequency Increased ML20195H8791988-06-0909 June 1988 Final Ro:On 880409,recurrence of Safety Channel 1 Circuit to Provide Proper Power Indication Occurred After Return to Normal Operations on 880401 Following Previous Failures on 880315 & 16.Caution Memo Issued to Operators ML20151W8931988-04-27027 April 1988 Safety Evaluation Supporting Amend 17 to License R-56 ML20151W3711988-04-25025 April 1988 Ro:On 880321,0401 & 09,safety Channel 1 Failed to Bottom Meter Stop.Cause Not Yet Identified.New Program Developed to Isolate & Correct Cause of Failure ML20151B3681988-03-28028 March 1988 Reportable Occurrence:On 880314,safety Channel 1 Circuit Failed to Provide Proper Power Indication for Several Seconds on Two Occasions.Caused by Capacitor Failure. Capacitor Replaced W/Substitute of Different Mfg 1998-03-27
[Table view] |
Text
] a 4 e.: . NUCl. EAR ENGINEERING SCIENCES DEPARI' MENT Nuclear Reactor Facility University of Florido I
- us.vemee on,m.cnn .
cucu. mero. .uun,.. .
Ga.nevels,Ho,kao 32611 Phone (900 392-1429.Toten 64330 September 29, 1989 Final 14 Day Report:
Safety Channel 1 High Voltage Trip Nuclear Regulatory Commiss'on Region II 101 Marietta Street, N.W.
Suite 2900-Atlanta, Georgia, 30323 Attention: Stewart D. Ebneter Regional Administrator Re : University of Florida Training Reactor Facility License: R-56, Docket No. 50-83 EVENT SCE'01R10:
On Friday 15 September 1989, the University of Florida Training Reactor (UFTR) was started up at 1435 hours0.0166 days <br />0.399 hours <br />0.00237 weeks <br />5.460175e-4 months <br />; at 1703 hours0.0197 days <br />0.473 hours <br />0.00282 weeks <br />6.479915e-4 months <br />, after seven (7) minutes of full power operation, with SRO W.G. Vernetson as operator at the controls, P.M.
Whaley as- SRO on-call and the UFTR operating at 100 kW, a reactor full trip occurred (Safety Channel I high voltage power supply dropped to 90% or less of its rated voltage).
The operation in pregress was support.ing neutron activation analysis as well as gamma irradiation of several samples in the shield tank. Following a three minute delay, primary cooling was restored and the high voltage trip signal was l noted to have cleared. At the start of the following working day, on Monday, September 18, 1989, the high voltage trip was again noted to have occurred (over the weekend), indicating that the problem was not related to operating at power and was intermittent. Preliminary investigation revealed the power supply output to be normal at the time of measurement (normal voltage, ne circuit noise) indicating that the problem was intermittent and in the high voltage power supply or in the high voltage trip bistable circuit.
On September 18, 1989, under Maintenance Lag Page 89-51, the Safety Channel 1 voltage trip bistable and the Safety Channel I high voltage power supply were examined, with intermittent instabilities in the power supply documented by a chart recorder. The instabilities were traced to a 15 VDC positive power supply, as the source of the problem.
8910060218 800929 3
{DR ADOCK 0500 %- 2
. i
}
e w %u,m-%,
g .
fi}
< i
- (" c .
l.; .i NRC1
. Safety; Channel'1lHV-Trip Page 2
" September 29, 1989s Since this problem followed an extensive maintenance program involving work on Lboth Safety Channel 2 and the control blade drive circuitry, the decision was made to treat this event as a potentially promptly reportable event and make.
notification (although the reactor trip from failure of Safety Channel I high voltage power. supply - positive 15 volt power. supply - was a trip from a known cause, and therefore not necessarily a reportable occurrence per UFTR Technical Specifications Section 6.6.2). This initial notification was carried out to Mr.
Ed McAlpine of Region II with a followup letter on September 18,-1989 (See Attachment I).
Since the event was reported b, ed on a series of problems followed by the SC-1 high voltage power supply trip, a brief summary of recent maintenance history is presented.
7 September 1989 The UFTR tripped from 100 kW operation due to an electrical transient; che trip relays for the primary coolant pump
-(deenergized) and the dilutant fan (deenergized) indi-cated tripped.. Both the primary coolant pump and the dilute fan were' running norme11y through the event.
8 September 1989 The quarterly scram checks (due in September) were performed 4 as part of corrective action prior to restart. Safety Chan- !
nel 2 high voltage trip test circuit was found to be not func-tioning, although removal of high voltage was verified to properly trip the UFTR. The bistable trip point was readjust-ed and the trip circuit tested and shown to perform properly on 12 September 1989.
8 September 1989 During trouble shooting procedures on Safety Channel 2, the auto flux control reference potentiometer was found to be mechanically failed. The potentiometer was replaced with an on-hand spare and the auto flux controller calibration veri-fied on 15 September 1989 with a brief operation at power.
12 September 1989 The auto flux controller calibrat ion check was first attempted on 12 September 1989, but the control blade drive system fail-ed to withdraw the safety control blades. Trouble shooting revealed that the switch logic contacts on the Regulating Blade were operating erratically, causing the multiple blade interlock to engage and inhibit movement of all control blades except the regulating blades It was decided to replace all
. hu 3 !
7
- Nb
' j 1 .- ..
- NRC 1 3 Safety. Channel?1 HV-Trip -
Page September 29, 1989 )
control. blade drive. switches with on-hand spares to prevent .
recurrence _of the failure. On 15 September-1989, control 1 blade >3 drive circuit maintenance: was completed with a retest program on potentially affected systems. including measurement of
. control blade drop times and controlled withdrawal and insertion time checks.
- 18 September 1989 Following the, trip on 15 September, 1989 and under Maintenance
. Log Page 89-51, it was . determined that the positive 15 volt DC power supply.to'the high-voltage power supply was operating erratically. Safety Channel,2 high voltage power supply was monitored overnight to assure'prope'r operation of Safety Channel 2, and the_ Safety Channel 1 high voltage power supply' replaced on 19 September 1989. . During an operational retest of the reactor, the 7extended range light did not extinguish at the required indication, and an unscheduled shutdown was performed per UFTR operating procedures.
Under. Maintenance Log Page 89-52, the' extended range bistable was-found to be activating at about 2-1/2 times higher than
. required and was corrected. Because of the physical location of the extended range bistable with respect to the bistable _ relays for Safety Channel I high voltage power supply. trip, it was thoughtLthat work on the high voltage bistable might have caused the extended range light bistable trip point to change. . Two steps were accomplished to assure that this was a unique occurrence; first, the trip point for the other bistable that is not-routinely checked for the trip point value (source interlock at 2 cps) was checked, with satisfactory results, and second, the extended range bistable trip' point was checked and noted on the Daily Preoperational Checkouts (to be accomplished daily until September 30,-1989). No difference in set point has been noted.
After a successful operation with a power run to check calibration of the auto flux controller, the UFTR was returned to service. Approximately 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> later, the reactor operation supporting neutron activation analysis and a gamma irradiation was terminated by the trip on the Safety Channel I high voltage power supply, the subject of this report. Although this series of failures occurred during a short time span, no evidence of a common root cause is available.
' *- l Sf$
- UR
.l .
- l l
.NRC' i Safety Channel 1 HV-Trip Page 4 September 29,'1989 {
21 September 1989 Between 1100 and 1300, with.the reactor secured, the coolant pump and the stack dilute scram relays' tripped. 'Although this event could have been an electrical switching transient, no one
, had been present to observe the occurrence and therefore this hypothesis could not be verified.. Because of previous reactor trips, it was decided to replace the field and trip relays for both scram channels. Following retesting, the maintenance log page was left open to provide observation of the reactor protection system behavjor until it was closed out on 25 September 1989 with no recurrence of either trip indicated.
29 September 1989 During preoperational checkout, the wide range drawer was noted to be downscale. Under Maintenance Log Page 89-55, the discriminator circuit of the wide range drawer was found failed.
A f ailed transistor and a resistor were replaced with on-hand spares with the system available on this date for performing checks for return to service.
This scenario through September '18 was communicated to Mr. Ed McAlpine (Region II NRC) on September 18, 1989. prior to having finally resolved the source of the problem later in the day. As indicated above, it was promptly reported primarily because of the extensive maintenance program as indicated ~in the attached one page confirmation of the conversation (See Attachment I). As promised in Attachment I, this event was reviewed by the UFTR Reactor Safety Review Subcommittee at its regular meeting on 19 September 1989. Since September 19, 1989,'several additional events have occurred as outlined above to include the tripped scram relays on 21 September 1989 and the failed discriminate circuit on September 29, 1989. The latter simply involved two electronic components at or near failure which have now been replaced.
EVALUATION / CORRECTIVE ACTION The general evaluation of this event is that the various failures are unrelated l except possibly though the electrical transient that caused the initial trip on September 7 and could have accelerated failure of certain other components, though some failures such as the flux controller are clearly mechanical and unrelated.
Corrective action over the past ten days has involved extensive maintenance with replacement of various trip relays and adjustment of the extended range bistable when the extended range was found to be malfunction during the startup on September 18, 1989. In this case (following procedures) an unscheduled shutdown was performed and -
the bistable aligned, and the extended range and the source interlock bistables verified to be properly functioning. The check of these 2 bistables (not responsible for reactor trip) is being added to the regular quarterly surveillance to check reactor trips.
l
NRC Safety Channel 1 HV-Trip Page 5 September 29, 1989 Based upon the above analysis, this event is concluded to constitute a reactor trip from a known cause. There was no compromise to reactor safety in this event nor was there a potential for abnormal radiation exposure. All reactor safety and control systems responded properly and in a conservative manner. Therefore, the event is not considered promptly reportable; nevertheless, the prompt notification process has been utilized because this event followed performance of extensive maintenance including corrections made to the high voltage trip setting on Safety Channel 2 as part of the Q-1 quarterly scram checks. The subsequent maintenance to replace several trip relays was primarily preventive in nature while the maintenance to repair the discriminator circuit in the wide range drawer is part of normal repairs dueto aging circuitry.
CONSEQUENCES The Reactor Safety Review Subcommittee (RSRS) Executive Committee met on September 19, 1989 and agreed with the trip evaluation and that it was not promptly reportable.
The committee agreed with restart for normal operations upon successful completion of repairs.
Reactor Staff and administration including Director W.G. Vernetson present on September 15, 1989 agreed there was no compromise to reactor safety in this event, nor was there danger of personnel receiving excessive radiation doses. All reactor safety and control systems responded properly for all failures identified in this rcport.
If further information is needed, please advise.
Sincerely, b < C' -
William G. Vernetson Director of Nuclear Facilities WGV/p LD L Notary Public Notary Public. State Of Flo% At Large My Commission Expir" var. 30,1991 cc: P.M. Whaley ""*"'""**"'"'*'"='
Reactor Safety Review Subcommittee Document Control Desk Attachment l
l
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - - _ _ _ _ _ _ _ _ _ _ _ _ - _ _ - _ _ -