ML20150E140

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/03L-0 on 781020:during Refueling Surveillance, Noted That Steam Generator 1B Level Channel 1L-548 Had Drifted Above Tech Spec Accuracy Limit.Caused by Instru Drift of Transmitter Instru Subsequently Recalibr
ML20150E140
Person / Time
Site: Zion File:ZionSolutions icon.png
Issue date: 11/17/1978
From: Hansen P
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20150E133 List:
References
LER-78-107-03L, LER-78-107-3L, NUDOCS 7812110159
Download: ML20150E140 (1)


Text

NHC F OllN! 36G U. S. NUCLL AH llLGULA10llY COfAIAlbLtOfd (7 77)

LICENSEE EVENT REPORT CONTROL ULOCX: l l l l l l (PLEASE PRINT OR TYPE ALL REQUIRED INf'ORMATION)

ID l 0i !9 ! T lucLtcLE 7

Ll 7l Loot I !S l 1 !hltb 0 l n l- l 0 LICEN:,6 14 l0 l nNuvutal O! o l -l0 l 02b h ,4 ;et l1uctroll 1l1 l1 hlbi LAl 50l@

TvPL Ju CON'T 10l1l , cf l L l@{ g j 9l0 l Ol0 l pl9 l5lhfl l O ! '! O !7 !O !@!iS 1l 1 ! 1l7 l 7 ! Rlh 7 W 00 69 DOCKET NUMuEH 8A L') kVENT OATE #4 HLf'OHT D A I L bV Et/ENT DESCRIPTION AND PROBAULE CONSEQUENCES h Io12llDurina refuelina surveillance, mechanics discovered that steam aenerator l lo l3 l lB l level channel (lL-548) had drifted hiah by 2.15?. Loop accuracy is 29.l l o 141 IThis is non-conservative for FS/FM mismatch with low S/G level and Low-Lowl 10151lS/G level Rx trips as presented in Table 3.1.1 of the Tech. Specs. As the I l o 16 I [ redundant channels were nnnrnblo nna avniinblo. *bn kon1th anA nnfety of I l o l 71, l the publ i c were nnt affected. I 10181 I l 7 8 9 .

60 SYSTE M CAUSE CAUSE COMP. VALVE CODE CODE SUSCODE COMPONENT CODE SUSCODE SUB000E icl[

7 8 l Il A l@ lE lh l E lh lI l MIS l T lR lUl@ { @ l 7l@

9 10 11 12 13 16 19 20 SE QUENTI AL OCCURRENCE REFORT REVIStON LE R 'RO EVENT YE A R REPORT NO. CODE TYPE N O.

b P8@ u 17 l Al l-l 11 l nl7 I l/l 10 I3l l T,l l-l lOl 21 ;2 23 24 26 27 26 29 3J 31 32 l

. ACTION F LIT U R E EFFECT SHUTDOWN ATTacurrNT Noon.4 Potvc COYD. COu'ONENT TAKEN ACi c. UN PLA*; T METHOD HOURS SUC'.t!TT E D F OR!.i bus. CU'"UEP " t M 'L'F AC TU * * : ft h.3._j[8)I 34 "lh lsa " l@ I Ih ,j n l n l n l 0 _l 40 lnl@ ly l@ jn l@ l P h l 2 h l(

Jo. J/ di Q 43 d4 47 CAUSE DESCRtPTION AND CORRECTIVE ACTIONS I110lIFischer Porter level trahnnit+ or model E1 tn? A 05t'nTmpnn_np dri F4 ea nut of l 11 11l ltolerance. The instrument was re-calihrated. #unctionallv checkna. nna I l3 l7i ] returned to service. Data on drift for these instruments are beina connilcid .

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,iI3l lt?o further action is recuired. 1 I l

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7 8 9 80 '

STA LS N POWER OTHER STATUS i CD F DISCOVERY DESCRIPTION t i l t,I l H l@ l Ol 0 l Ol@l tiA l l n !@l Furveillance Testina l ACTLVITY CO TENT RELE ASED OF MELE ASE AMOUNT Or ACTIVITY LOCATION OF RELE ASE j MA "A i t Ic8 l9 ["J @ I" l@[

7 10 tt 44 I l 45 80 I I PERSONNEL F APOSUnEs i NUMt1E R TYPI DESCRIPTION 39 i s 121.

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> i3 eo PERSONNE L IN1uisit s NUYtli H DCSCniPYtDN '

T T]lolo I B U Iol@l 11 1) nA 80 I

l E OSS OF Olt DAM AGE 10 F AcillTv l 1YPE DE SCHIPTION i M^

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s u u I " l@l l l to no Pull t ICIl Y 4.,-

NRC USf ONt Y l tv.uf n

  1. ' 71 fo811 *J~1N1l@OE%CitiPTION l MA l l!lIIIII11III~,

O W1 Paul Wm. Hansen 312-746-2084 ut . 2 44? '"'*

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