ML20147E797

From kanterella
Jump to navigation Jump to search
/03L-0 on 781101:MSIV 1D from Train a Did Not Close When Signal Was Removed,Caused by Relay Plunger Sticking
ML20147E797
Person / Time
Site: Zion File:ZionSolutions icon.png
Issue date: 12/01/1978
From: Melnicoff M
COMMONWEALTH EDISON CO.
To:
Shared Package
ML20147E783 List:
References
LER-78-121-03L, LER-78-121-3L, NUDOCS 7812210213
Download: ML20147E797 (1)


Text

"HC F OM %G U. S. NUCLEAR RLGULATOHY COMMISSION (7 71)

, s LICENSEE EVENT REPORT gDNTROL DLOCK: l l' l l I l lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) lo l t l lI l Llz b lg l 1l@l 0 lo l _ l olLICEf 0 SE loNUMdEH l o lo l_l0lol@l4 l 3 LICENSE 26 26 l1 l 3TYPE l3 JVl@lbl LAIl b6l@

7 8 9 LICENSEE CODE 14 15 d CON'T lol11 a nll L l@l o i s l 010 1012 19l Sl@lillIoIll71R l@l1 l ? ln l 1 l7 lnl@

14 75 HkPOH T DATE liO 7 8 LU bl DOCKE T NUl?BE n (H 8)J EVENT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h lo121lDuring actuation testing of MSIV 10 from Safeauards Train B, it closed. I lolal Ibut then reocened when sional was removed. When tested from Tr2_4n A, I lo la i Ithe MSIV remained closed when signal was removed.Thus nroner auto l

[Opsil actuation by both trains as required by Tech. Spec. Table 3.4-1 was not l Io lo l l accomplished. However, the health and safety of the oublic was not I lo17llaffected as Train A was operable and would have actuated the MSIV I

ioisil properly in the event of an actual signal. I 80 7 8 9 .

CE CO E SLBCO E COMPONENT CODE SLOC DE SU E lol9l 7 8 l ClD l@ l I]@ l B l@ l R lE l L l Al Y lX l@ l Al@ l 20Zl @

9 10 11 12 13 10 19

_ SEOVENTI AL OCCURRENCE REPCRT REVISION ggp ng EVENT YE Aft REPORT NO. CODE TYPE NO.

'@ yg n

,,,,, l217l8l 22 l-l 2J l ll 2 l 1 l 24 26 l, 'l 27 I d 3l 23 2']

lL l JJ l-l 31 l 0l 32 i

NPL T  : T HOURS 72 SS : F r. i .:. "1 CT rEn l Digi Zi@

33 J4 g@

Ja j Zi@

30 l 0l q 01 3/ 40 l lN i@

41 j_Y_j@

42 lA 43 l@ lcl.2l7i 2l@ "

44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 11101l The safeguards sional sealing relay (clark cat. 6 4U d-120 ) fn 41 arl +n l lijij l latch when energized, allowing the MSIV to reopen when the sianal was I removed. This was due to relay plunger sticking. The relay was cleanedp i,i3i l lubricated, and exercised. Then MSIV 1D was retested successfullv from I i1 i.iil 7 g g Train B. No further action is required.

80 I

s 5  % POWE R OTHER STATUS ISCO HY DISCOVERY DESCRIPTION IiIsi IC l@ p l 0 l 0l@l NA l l Cl@l Operator Observation l ACTIVITY CONTENT Rf LE ASED OF RE LEASE AMOUNT OF ACTIVITY LOCATION OF RELE ASE I1 l c ] (_Zj (E) [,Zj@l NA l l NA l 7 8 9 10 11 44 45 80 PERSONNEL TXPOSUHES NUMOE R TYPE DESCRIPTION l t I y l 10 l 0 LoJ@l zl@l NA l PEnSOmE"mu'Jits N uen t. n oEcCniPriON@

li lx 18 010 l 0 l 0l@l12 NA l 7 11 80 1 OSS OF Olt DAMAGE TO F 4CILITY Q TYPE DE SC4tPilON  %/

li 191 IZ l@l NA l PUHl1 1' ' NRC USf. ON LY IMUE D

(} f l 2 l gnu l lN l@DESCHIP1 l NA .

TON l l l l l l l l l l l l l l ';,

I 10 68 69 80 + ;;;

NAME OF ritEPARER M. A. Melnicoff PHONE .312 /7 4 6-20 8 4 E,

. - .