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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20134C3421997-01-27027 January 1997 Special Rept:On 970110,improper Stack Monitor Calibr Occurred.Caused by Use of Flawed Procedure.Revised Q-2 Surveillance Data Sheet ML20116D9851996-07-24024 July 1996 14 Day Rept:On 960710,non-conservative Setting for Safety Channel 2 High Voltage Sensing Circuit Occurred.Caused by Failures in Safety Channel 2 High Sensing Circuit.Performed Successful Check of Sensing Circuit Loss of Voltage Setting ML20116D9921996-07-12012 July 1996 Ro:On 960711,Safety Channel 2 High Voltage Sensing Circuit Failed.Allowed Reactor to Sit Over Weekend & Planned to Restart ML20107L7481996-04-25025 April 1996 Ro:On 960404,failures in Safety Channel 2 High Voltage Sensing Circuits Resulted in Safety 2 Trip.Stated Resistors Replaced & Safety Channel 2 High Voltage Power Supply Temporarily Replaced W/Exact Duplicate on 960412 ML20107L7601996-04-0505 April 1996 Ro:On 960404,spurious Safety Channel 2 Loss of High Voltage Trip Occurred.Caused by Previously Undetected Matl Failure. Repairs Should Be Completed by 960410 & Restart Approved Subject to Successful post-repair Checks ML20086D1041995-06-30030 June 1995 Ro:On 950609,failure of Primary Coolant Return Line Flow Sensor to Initiate Trip Occurred.Flow Sensors Checked After Debris Removal & as of 950626 Problem Considered Resolved ML20091L2891995-06-12012 June 1995 Ro:On 950609,primary Coolant Flow Line Return Sensor Failed. Caused by Debris in Line.Line Repaired ML20082D0221995-04-0303 April 1995 Ro:On 950309-13,leakage of Coolant HX Occurred After Primary Coolant Resistivity Increase Noted.Primary & Secondary Flow Secured & Shell Side of HX Drained.No Leakage Collected.Hx Returned to Primary Sys & Placed in Operation ML20099H7641992-08-10010 August 1992 Ro:On 920727,temp Recorder Point 2 Noted to Be Reading Downscale,Indicating Failure in Circuit Monitoring Water Temp at Exit of South Ctr Fuel Box 2.Caused by Blockage in Fuel Box.Planned Maint Underway.Event Not Reportable ML20086H8081991-12-0303 December 1991 Final Ro:On 911119,safety Channel 2 Meter Flickered & Dropped Out Hard Downscale (Pegged).Caused by Intermitten Fault in Fine Adjust Potentiometer of Circuit. Poteniometer Replaced & Amplifier Card Reseated ML20086G2631991-11-27027 November 1991 Ro:Unscheduled Reactor Trip Occurred While Measuring Temp Coefficient of Reactivity.Caused by Secondary Cooling Water Dropping Below 8 Gpm Min Required by Limiting Safety Sys Setting.Cooling Water Logic Placed in City Water Mode ML20086H8151991-11-20020 November 1991 Ro:On 911120,unscheduled Shutdown Conducted Due to Failure of Safety Channel 2 Circuit on 911119.Possibly Caused by Problem in Safety Channel 2 Meter Circuit.Permission to Restart Not Yet Sought ML20086G2681991-11-19019 November 1991 Ro:Reactor Tripped on Loss of Secondary Cooling Flow on City Water & Gate Valve on City Water Flow Partially Closed to Allow Operation at Higher Temp.All Safety & Control Sys Functioned Properly.Detailed Rept Will Be Submitted ML20085H4911991-10-16016 October 1991 Ro:On 911003,failure to Perform Required Surveillance of Limiting Safety Sys Setting of Loss of Secondary Coolant Pump Power Discovered.Trip Check on Loss of Pump Power Incorporated Into Q-1 Quarterly Scram Checks ML20085H5071991-10-0303 October 1991 Ro:Possibility That Tests for Operability on Loss of Secondary Coolant Well Pump Power May Not Meet Tech Spec Surveillance Requirement 3.2.2(2) Discovered.Minutes of 911007 Executive Committee Meeting Encl ML20058F4281990-10-29029 October 1990 Ro:On 901002,three Reactor Startups Occurred W/O Performing Daily Checkout or Control Blade Interlock Checks Following Previous Shutdown ML20058F3481990-10-25025 October 1990 Ro:On 901025,three Reactor Startups Performed W/O Daily Checkout Being Performed within Required Time Interval,Per SOP SOP-A.2, Reactor Startup ML20248F1081989-09-29029 September 1989 Ro:On 890915 & 18,reactor Trips Occurred When Safety Channel 1 High Voltage Power Supply Dropped to 90% or Less of Rated Voltage.Caused by Instabilities in 15-volt Dc Power Supply. Trip Relays Replaced & Bistable Adjusted ML20244D5981989-03-31031 March 1989 Final Rept Re Higher than Expected High Streaming Radiation Levels Present at Vertical Ports During Full Power Operation.Caused by Inadequate Survey of Rabbit Shield on 870120.Extra Shielding Installed on Rabbit Sys Shield ML20244A7401989-03-31031 March 1989 Ro:On 890317,reactor Trip W/High Primary Coolant Temp Indication Occurred.Caused by Failure of Specific Temp Recorder Sys Due to Dust/Corrosion Buildup on Slide Wire Causing Excessive Resistance.Buildup Cleaned Off ML20235W6951989-02-21021 February 1989 Ro:On 890221,potential Failure to Rept Significant Change in Level 1 Administration Existed,Per Tech Spec 6.6.3. Evaluation Determined No Significant Administration Oversi Oversights Involved ML20206J7841988-11-14014 November 1988 Ro:On 881104,unscheduled Reactor Shutdown Occurred Due to Failure of Temp Recorder to Indicate Properly.Caused by Failure of Microswitch.Microswitch & Vacuum Tube Replaced & Calibr Check Performed ML20150B6821988-06-23023 June 1988 Ro:On 880610,clutch Current Indication Lamp for Control Blade safety-2 Burned Out at Full Power,Dropping Control Blade from 56% Withdrawn to Fully Inserted Position.Clutch Replaced & Lamp Replacement Frequency Increased ML20196A3661988-06-23023 June 1988 Ro:On 880610,control Blade Safety 2 Clutch Indicating Lamp Burned Out.Burned Out Clutch Current Indicating Bulb Replaced to Include Necessary Control Blade Drive & Drop Time Checks ML20195H8791988-06-0909 June 1988 Final Ro:On 880409,recurrence of Safety Channel 1 Circuit to Provide Proper Power Indication Occurred After Return to Normal Operations on 880401 Following Previous Failures on 880315 & 16.Caution Memo Issued to Operators ML20151W3711988-04-25025 April 1988 Ro:On 880321,0401 & 09,safety Channel 1 Failed to Bottom Meter Stop.Cause Not Yet Identified.New Program Developed to Isolate & Correct Cause of Failure ML20151B3681988-03-28028 March 1988 Reportable Occurrence:On 880314,safety Channel 1 Circuit Failed to Provide Proper Power Indication for Several Seconds on Two Occasions.Caused by Capacitor Failure. Capacitor Replaced W/Substitute of Different Mfg ML20148E8161988-03-15015 March 1988 Ro:On 880315,failure of Safety Channel 1 Circuit Occurred. Failed Component Replacement Has Restored Safety Channel 1 to Normal ML20209G7221987-04-13013 April 1987 Ro:On 870401,reactor Experienced Safety Channel 1 Trip. Caused by Operator Error.Rapid Recovery Restart Performed by Operator.Memorandum Issued Placing Restrictions on Automatic Operation & Limiting Removal of Regulating Blade ML20207J0321986-12-19019 December 1986 Ro:On 861211,actuation of Evacuation Alarm & Evacuation Alarm/Core Vent Sys Interlocks Occurred While Stack Count Rate Approx 300 Cps,In Potential Violation of Tech Specs. Cause Not Given.Vent Will Be Secured at 10 Cps During Drill ML20132B4241985-09-17017 September 1985 Ro:On 850904,one Control Blade Failed to Drop Fully Into Core on Demand from 64% Withdrawn Position.Probably Caused by Bearings Supporting Blade/Shaft Coupling or Magnesium Shroud housing-to-blade Clearance ML20132B4521985-09-0404 September 1985 Ro:On 850904,one Reactor Control Blade Failed to Drop on Demand from 64% Removed Position.Probably Caused by Binding in Clutch S-3 Possibly Due to Moisture or Other Effect Reducing Clearance 1997-01-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20207C0881998-12-31031 December 1998 Rev 11 to Uftr SAR, Consisting of Change Page 12-20 ML20217M6581998-03-27027 March 1998 Updated Proposal Submitted to NRC to Meet 10CFR50.64 Requirements for Updating Scheduling of Uftr Conversion from Heu to LEU Fuel ML20203C4551997-12-0303 December 1997 Safety Evaluation Supporting Amend 22 to License R-56 ML20216A8791997-08-31031 August 1997 Univ of Fl Training Reactor Annual Progress Rept for 960901-970813 ML20148G3561997-05-29029 May 1997 Univ of Fl Training Reactor Operator Requalification & Recertification Training Program Plan,Jul 1997-June 1999 ML20134C3421997-01-27027 January 1997 Special Rept:On 970110,improper Stack Monitor Calibr Occurred.Caused by Use of Flawed Procedure.Revised Q-2 Surveillance Data Sheet ML20137C1481996-12-31031 December 1996 195-96 Annual Progress Rept, Replacing Pages IV-6,IV-11 & IV-12 ML20128N4671996-10-10010 October 1996 Safety Evaluation Supporting Amend 21 to License R-56 ML20135D0081996-08-31031 August 1996 Univ of Fl Training Reactor Annual Progress Rept for 950901-960831 ML20116J5791996-08-0909 August 1996 Annual Progress Rept of Univ of Florida Training Reactor 940901-950831 ML20116D9851996-07-24024 July 1996 14 Day Rept:On 960710,non-conservative Setting for Safety Channel 2 High Voltage Sensing Circuit Occurred.Caused by Failures in Safety Channel 2 High Sensing Circuit.Performed Successful Check of Sensing Circuit Loss of Voltage Setting ML20116D9921996-07-12012 July 1996 Ro:On 960711,Safety Channel 2 High Voltage Sensing Circuit Failed.Allowed Reactor to Sit Over Weekend & Planned to Restart ML20107L7481996-04-25025 April 1996 Ro:On 960404,failures in Safety Channel 2 High Voltage Sensing Circuits Resulted in Safety 2 Trip.Stated Resistors Replaced & Safety Channel 2 High Voltage Power Supply Temporarily Replaced W/Exact Duplicate on 960412 ML20107L7601996-04-0505 April 1996 Ro:On 960404,spurious Safety Channel 2 Loss of High Voltage Trip Occurred.Caused by Previously Undetected Matl Failure. Repairs Should Be Completed by 960410 & Restart Approved Subject to Successful post-repair Checks ML20101L3491996-03-27027 March 1996 Updated Proposal Submitted to NRC to Meet 10CFR50.64 Requirements for Updating Scheduling of Uftr Conversion from HEU to LEU Fuel ML20086D1041995-06-30030 June 1995 Ro:On 950609,failure of Primary Coolant Return Line Flow Sensor to Initiate Trip Occurred.Flow Sensors Checked After Debris Removal & as of 950626 Problem Considered Resolved ML20091L2891995-06-12012 June 1995 Ro:On 950609,primary Coolant Flow Line Return Sensor Failed. Caused by Debris in Line.Line Repaired ML20082D0221995-04-0303 April 1995 Ro:On 950309-13,leakage of Coolant HX Occurred After Primary Coolant Resistivity Increase Noted.Primary & Secondary Flow Secured & Shell Side of HX Drained.No Leakage Collected.Hx Returned to Primary Sys & Placed in Operation ML20115B5881994-08-31031 August 1994 Annual Progress Rept of Univ of Fl Training Reactor for Sept 1993 - Aug 1994 ML20072P7141993-08-31031 August 1993 Annual Progress Rept of Univ of Fl Training Reactor for Sept 1992 - Aug 1993 ML20044G8351993-05-28028 May 1993 Revised, Operator Requalification & Recertification Training Program Plan of Univ of Florida Training Reactor, Jul 1993 Through June 1995. ML20069D0971992-08-31031 August 1992 Annual Progress Rept of Univ of Fl Training Reactor for Period 900901-910831 ML20099H7641992-08-10010 August 1992 Ro:On 920727,temp Recorder Point 2 Noted to Be Reading Downscale,Indicating Failure in Circuit Monitoring Water Temp at Exit of South Ctr Fuel Box 2.Caused by Blockage in Fuel Box.Planned Maint Underway.Event Not Reportable ML20094S4071992-04-30030 April 1992 Rev 7 to SAR Section 5.2 Re Secondary Cooling sys,9.2.3 Re Demineralized Water Makeup sys,9.2.4 Re Purification Sys & 9.2.5 Re Potable & Sanitary Water Sys ML20091C0451992-03-26026 March 1992 Updated Proposal Submitted to NRC to Meet 10CFR50.64 Requirements for Updating Scheduling of Univ of Florida Training Reactor Conversion from HEU to LEU Fuel ML20087A0521991-12-29029 December 1991 Rev 1 to Operator Requalification & Recertification Training Program Plan of Univ of Florida Training Reactor, Jul 1991 Through June 1993 ML20086H8081991-12-0303 December 1991 Final Ro:On 911119,safety Channel 2 Meter Flickered & Dropped Out Hard Downscale (Pegged).Caused by Intermitten Fault in Fine Adjust Potentiometer of Circuit. Poteniometer Replaced & Amplifier Card Reseated ML20086G2631991-11-27027 November 1991 Ro:Unscheduled Reactor Trip Occurred While Measuring Temp Coefficient of Reactivity.Caused by Secondary Cooling Water Dropping Below 8 Gpm Min Required by Limiting Safety Sys Setting.Cooling Water Logic Placed in City Water Mode ML20086H8151991-11-20020 November 1991 Ro:On 911120,unscheduled Shutdown Conducted Due to Failure of Safety Channel 2 Circuit on 911119.Possibly Caused by Problem in Safety Channel 2 Meter Circuit.Permission to Restart Not Yet Sought ML20086G2681991-11-19019 November 1991 Ro:Reactor Tripped on Loss of Secondary Cooling Flow on City Water & Gate Valve on City Water Flow Partially Closed to Allow Operation at Higher Temp.All Safety & Control Sys Functioned Properly.Detailed Rept Will Be Submitted ML20085H4911991-10-16016 October 1991 Ro:On 911003,failure to Perform Required Surveillance of Limiting Safety Sys Setting of Loss of Secondary Coolant Pump Power Discovered.Trip Check on Loss of Pump Power Incorporated Into Q-1 Quarterly Scram Checks ML20085H5071991-10-0303 October 1991 Ro:Possibility That Tests for Operability on Loss of Secondary Coolant Well Pump Power May Not Meet Tech Spec Surveillance Requirement 3.2.2(2) Discovered.Minutes of 911007 Executive Committee Meeting Encl ML20105B3751991-08-31031 August 1991 Annual Progress Rept of Univ of Florida Training Reactor, Sept 1990 - Aug 1991 ML20070T4061991-03-27027 March 1991 Updated Proposal Submitted to NRC to Meet 10CFR50.64 Requirements for Updating Scheduling of Univ of Florida Test Reactor Conversion from High Enriched U to Low Enriched U ML20058F4281990-10-29029 October 1990 Ro:On 901002,three Reactor Startups Occurred W/O Performing Daily Checkout or Control Blade Interlock Checks Following Previous Shutdown ML20058F3481990-10-25025 October 1990 Ro:On 901025,three Reactor Startups Performed W/O Daily Checkout Being Performed within Required Time Interval,Per SOP SOP-A.2, Reactor Startup ML20072S3761990-08-31031 August 1990 Annual Progress Rept of Univ of Florida Training Reactor, for Sept 1989 - Aug 1990 ML20248F1081989-09-29029 September 1989 Ro:On 890915 & 18,reactor Trips Occurred When Safety Channel 1 High Voltage Power Supply Dropped to 90% or Less of Rated Voltage.Caused by Instabilities in 15-volt Dc Power Supply. Trip Relays Replaced & Bistable Adjusted ML20006D5491989-08-31031 August 1989 Annual Progress Rept of Univ of Florida Training Reactor, Sept 1988 - Aug 1989. W/900207 Ltr ML20244A7401989-03-31031 March 1989 Ro:On 890317,reactor Trip W/High Primary Coolant Temp Indication Occurred.Caused by Failure of Specific Temp Recorder Sys Due to Dust/Corrosion Buildup on Slide Wire Causing Excessive Resistance.Buildup Cleaned Off ML20244D5981989-03-31031 March 1989 Final Rept Re Higher than Expected High Streaming Radiation Levels Present at Vertical Ports During Full Power Operation.Caused by Inadequate Survey of Rabbit Shield on 870120.Extra Shielding Installed on Rabbit Sys Shield ML20235W6951989-02-21021 February 1989 Ro:On 890221,potential Failure to Rept Significant Change in Level 1 Administration Existed,Per Tech Spec 6.6.3. Evaluation Determined No Significant Administration Oversi Oversights Involved ML20206J7841988-11-14014 November 1988 Ro:On 881104,unscheduled Reactor Shutdown Occurred Due to Failure of Temp Recorder to Indicate Properly.Caused by Failure of Microswitch.Microswitch & Vacuum Tube Replaced & Calibr Check Performed ML20196C0821988-08-31031 August 1988 Annual Progress Rept of Univ of Florida Training Reactor, Sept 1987 - Aug 1988 ML20196A3661988-06-23023 June 1988 Ro:On 880610,control Blade Safety 2 Clutch Indicating Lamp Burned Out.Burned Out Clutch Current Indicating Bulb Replaced to Include Necessary Control Blade Drive & Drop Time Checks ML20150B6821988-06-23023 June 1988 Ro:On 880610,clutch Current Indication Lamp for Control Blade safety-2 Burned Out at Full Power,Dropping Control Blade from 56% Withdrawn to Fully Inserted Position.Clutch Replaced & Lamp Replacement Frequency Increased ML20195H8791988-06-0909 June 1988 Final Ro:On 880409,recurrence of Safety Channel 1 Circuit to Provide Proper Power Indication Occurred After Return to Normal Operations on 880401 Following Previous Failures on 880315 & 16.Caution Memo Issued to Operators ML20151W8931988-04-27027 April 1988 Safety Evaluation Supporting Amend 17 to License R-56 ML20151W3711988-04-25025 April 1988 Ro:On 880321,0401 & 09,safety Channel 1 Failed to Bottom Meter Stop.Cause Not Yet Identified.New Program Developed to Isolate & Correct Cause of Failure ML20151B3681988-03-28028 March 1988 Reportable Occurrence:On 880314,safety Channel 1 Circuit Failed to Provide Proper Power Indication for Several Seconds on Two Occasions.Caused by Capacitor Failure. Capacitor Replaced W/Substitute of Different Mfg 1998-03-27
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NUCLEAR ENGINEERING SCIENCES DEPARTMENT Nuclear ReactorFacility University of Florido i j c .v., , mes., .
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Phone 504)3924429.Telea 54330 r ., ? -) n
< a u 21 P 2 : ,6 April 13, 1987 Nuclear Regulatory Commission Suite 2900 101 Marietta Street, N.W.
Atlanta, GA 30323 Attention: J. Nelson Grace Regional Administrator, Region II Re: University of Florida Training Reactor (UFTR)
Facility License R-56; Docket No. 50-83 Gentlemen:
As reported by telephone and by telecopy on April 2, 1987, the University of Florida Training Reactor experienced a Safety Channel 1 (125% overpower) full trip (blade drop plus water dump) at 1416 hours0.0164 days <br />0.393 hours <br />0.00234 weeks <br />5.38788e-4 months <br /> on April 1, 1987. The Reactor Safety Review Subcommittee (RSRS) reviewed this event and concluded it should be promptly reported since it involved a challenge of the overpower trip sys-tem on the UFTR due primarily to operator error. The event was, however, not considered to meet any specific prompt reportability requirements listed in the UFTR Technical Specifications under Section 6.6.2. Following implementa-tion of corrective / preventive actions and notification of the NRC, the RSRS authorized restart and resumption of nonnal operations. This event was re-viewed by telephone with Mr. Larry Mellen and Mr. Paul Burnett (twice) on April 2, 1987 as to the details of the occurrence. The event was further dis-cussed with Mr. Paul Frederickson on April 7, 1987. Based on the RSRS recom-mendation and NRC inspector advice, this event has been considered a promptly reportable event as specified in the reporting requirements of paragraph 6.6.2 ( 3 ) of the UFTR Technical Specifications. Therefore, this report is being transmitted to meet the requirement for a final report closing out the occur-rence.
SCENARIO At 1416 hours0.0164 days <br />0.393 hours <br />0.00234 weeks <br />5.38788e-4 months <br /> on April 1,1987, the UFTR experienced a Safety Channel 1 (125%
overpower) Trip. There had been approximately 6.8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> full power operation until early evening on March 31 resulting in significant xenon buildup in the UFTR core on April 1, 1987. The xenon present plus a small-worth experiment resulted in a normal control blade position of 424 units versus the normal value of ~375 units at the beginning of March,1987 for a clean core and a value of ~383 units on April 1 with the experiment in place.
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1 Nuclear Regulatory Commission April 13,1987 Page Two On April 1, there was a brief operation of just over an hour including step increases in power level (10 kw, 50 kw, 80 kw) and ending with three minutes at full power for radiation surveys for Training Class for Radiation Protec-tion Technology students from Central Florida Community College. At this point a normal shutdown was performed by the operator (G.W. Fogle) so he could at-tend to other activities before continuing full power operation for a full re-stricted area survey and concurrent build up of Argon-41 inventory for ac-tivity measurement and concentration calculations for this same group of ra-diation protection technology students. Permission to restart by Dr. Vernetson (Facility Director) was interpreted as approving restart without . determination of a new critical position since restart would be performed after only a few minutes shutdown (actual shutdown time was 4 minutes) and since the critical position was already determined. The operator was aware that there was still significant xenon buildup in the core from the previous day's extended run at full power. The system was also in a hot condition from the previous hour's run.
A rapid recovery restart was performed by the operator implying no stop at 1 watt (in this case only about 100 watts or above would have been possible) to record a steady state condition. Although not a procedural violation, the op-erator normally would have delayed for a critical position determination in the vicinity of 100 watts. This fact is not considered to have directly af-fected the resulting trip except that, the longer the delay in restart, the less likely the occurrence of the trip as temperatures are reduced. The opera-tor tested the servo system at ~80 Kw and then allowed it to control the re-turn to 100 kw on the 30 second limiting period. Although aware of the xenon built up in the core, the operator failed to monitor the power increase suffi-ciently. With both temperature and xenon negative reactivity effects acting plus a small negative reactivity for a sample present in one port, the regula-ting blade was sufficiently removed (800-900 units from the bottom) that its insertion rate following a startup at a 30 second period was inadequate to avoid reaching the 125 kw transient overpower condition resulting in a Safety 1 (125% power) trip at 1416 hours0.0164 days <br />0.393 hours <br />0.00234 weeks <br />5.38788e-4 months <br />. A contributor in this trip event was that the operator began to take a set of log readings upon reaching 100 Kw and was also distracted by a question from the class for which the operation was being performed. The time period during which the operator was distracted between reading 100 kw and tripping on overpower at 125 kw is estimated to have been about 20 seconds. Basically, the operator failed to assure the automatic con-troller was bringing the reactor to a steady state power level with a near infinite period before recording log readings. As a result, the power reached the limiting safety system setting (trip point) of 125 kw at which point all safety systems responded properly for a full trip: Safety 1 trip with full drop insertion of all control blades plus dumping of primary coolant resulting in derived LSss trip indicators on the Primary Coolant Pump, Coolant Level and Coolant Flow.
r Nuclear Regulator Commission April 13,1987 Page Three EVALUATION The evaluation of this occurrence was first directed to determine whether it was promptly reportable under UFTR Tech Specs items in Section 6.6.2, "Special Reports." Although the trip represents an unanticipated change in reactivity greater than one dollar, the trip was from a known cause and hence considered to be not necessarily promptly reportable under Tech Specs Section 6.6.2(3)(d).
Therefore, item (3)(d) was eliminated from requiring prompt reporting.
Similarly, although the operator would normally have established a critical position prior to resuming power operations, SOP-A.:2, " Reactor Startup," does not preclude a restart as performed here. Finally, consideration was given to item (3)(f) for inadequacy in implementation of administrative or procedural controls. Item (3)(f) is also not considered to apply for this occurrence in that operator error was the primary cause of the occurrence and the procedure involved actually has served well, though some clarifications are recommended later in this report.
The second part of the evaluation was of the UFTR systems themselves. First, the RSRS Executive Committee agreed that this event is considered to have no impact on the health and safety of the public. Similarly, the event is con-sidered to have no impact on UFTR safety. All safety systems performed as de-signed for a full trip (blade drop to full insertion and dumping of primary coolant) with Safety Channel (125% overpower) Trip indicating and with derived limiting safety system setting (LSSS) trip indications on the primary coolant pump, primary coolant level, and primary coolant flow limiting safety system settings. The f act that Safety Channel #2 did not indicate a trip supports the evaluation that power was stopped promptly at the 125 kw level as both chan-nels are nominally set at 125 kw but one is expected to yield a trip signal slightly prior to the other due to uncertainty in the LSSS. All system indica-tions supported a trip at the 125 kw level. Since this was a transient, not a steady state, power level, no safety limit was exceeded. Finally, from the bases for the Limiting safety System Settings presented in the UFTR Tech Specs Section 2.2, the 125 kw LSSS value is specifically set at the 125% overpower value for the protection of the fuel, fuel cladding and the reactor core.
Therefore, it was considered by UFTR Management and agreed by the RSRS Execu-tive Committee on April 2, 1987 and supported by all members at the regular RSRS meeting on April 9, 1987 that the UFTR system is well designed for such an overpower trip with no safety impact expected or resulting.
Appendix 15 of the UFTR Safety Analysis Report supports this evaluation in Ap-pendix 15B where the effects of large reactivity additions are considered and in Appendix 15D where decay heat effects are considered following a long run at full power. Here the total energy generation for the hour preceding the accident was less than 35 kw-hrs with a much smaller reactivity addition of only ~0.18% Ak/k. Certainly Section 14.1, " Excess Reactivity Insertion" of the UPTR Safety Evaluation Report (NUREG-0913) also supports this evaluation.
Finally, Section 15.2, " Loss of Coolant Accident" in the UFTR Safety Analysis Report considers a scram with coolant drop from 625 kw equilibrium operation, again without excessive fuel temperatures.
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Nuclear Regulatory Commission April 13,1987 Page Four Since this event was an overpower trip with potential operator error involved in that the operator did not properly assure the steady state operation at full power and did not stabilize power and take a complete set of readings prior to raising power into the power range this event was required to be re-ported by the RSRS in agreement with UFTR management. In addition, it was recommended to and required by the RSRS that the operations in automatic con-trol should be restricted to assure such a condition does not challenge the operator in the future and that operator training be conducted to assure fol-lowing such restrictions to prevent recurrence of such a trip.
CONSEQUENCES Based on the evaluation above, this overpower trip occurrence is considered to have no impact on the health and safety of the public. In addition, the event is not considered to impact on the safe operation of the UFTR. Reporting is required by the RSRS with agreement by UFTR management because of the over-power trip challenging the trip system due to operator error.
CORRECTIVE / PREVENTIVE ACTIONS NRC Region II was notified of the trip on April 2, 1987; the trip event was discussed once with Mr. Mellen and twice with Mr. Burnett prior to restart. In addition, prior to authorizing restart, the following conditions were required by the RSRS to be implemented:
- 1. A memorandum was issued (see Attachment I) placing restrictions on auto-matic operation and limiting removal of the regulating blade to no greater than 750 units above 50 Kw power levels. The memorandum also in-dicated the following to allow for condi tions which would otherwise re-quire excessive regulating blade removal:
If the zero power critical position on the regulating blade is >30 units above the normal critical position as indicated in the opera-tions log (first day of month), then an alternate authorized bank position will be used for the safety blades.
Note that the memorandum implementing the current alternate authorized safety blade bank positions is enclosed as Attachment II.
- 2. Training was conducted for all available operators prior to restart (or participation in operations) to include:
- a. Reminder on how to take logs (verbal and written).
- b. Reminder on observing the console and noting transient versus steady-state conditions especially for a high regulating blade cri-tical position (verbal and written).
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Nuclear Regulatory Commission April 13,1987 Page Five
- c. Training on the memorandum restricting use of automatic control and limiting removal of the regulating blade.
Finally, . a commitment is made to revise SOP's A.2 (Reactor Startup) and A.3 (Operation At Power) to reflect these requirements and conduct training on them within 60 days. The special memorandum will serve as the preventive ac-tion in the interim.
FINAL NOTE These corrective / preventive actions were further reviewed at the April 9,1987 full RSRS meeting with concurrence by all members. Although this event is con-sidered to have no impact on the health and safety of the public or on reactor safety, the actions delineated above will assure such an overpower trip does not recur. With this report this incident is considered closed with corrective actions committed to be implemented as noted above.
Sincerely, uk)h Ub William G. Vernetson Director of Nuclear Facilities WGV/ps cc: Reactor Safety Review Subcommittee P.M. Whaley, Acting Reactor Manager l
NUCLEAR ENGINEERIN 3 SCIENCES DEPARTMENT NuclearReactor Facility University of Florido '
l l tnvenes a.o eee .
mamsuanees ATTACHMENT I Gainewte,Flodde 33611 Phone (804)3921429.Teesa M330 April 2, 1987 MEMORANDUM TO: UFTR Operations Staff FROM: W.G. Vernetsor50
SUBJECT:
Corrective / Preventive Actions for Safety 1 Overpower Trip Due to the Safety 1 ( overpower) trip on , April 1,1987, certain restrictions are being implemented as follows; these restrictions carry the weight of SOP requirements and will be commitments to the NRC:
- 1. If the zero power critical position on the regulating blade is more than 30 units above the normal critical position as indicated in the operations log (first day of the month),
then an alternate authorized bank position must be used for the safety blades. Specific authorization for use of this alternate bank position must be obtained each time it is used from Level 3 (Reactor Manager or designated alternate) or above.
- 2. Automatic (Servo) Control operations are restricted so there is to be no automatic operation unless:
- a. Power is within 20% of demand setting prior to going into automatic servo control and period is near in-finity yielding a near steady-state condition of reac-tor power.
- b. Regulating blade position is less than 750 units.
- 3. The regulating blade should not be withdrawn to greater than 750 units for power operation above 50 Kw.
These commitments will be incorporated into the next revision of UFTR SOP-A.2 and A.3 within 60 days.
WGV/ps cc: P.M. Whaley RSRS Emriopporks*y/Atkm2W Action fanployer I
NUCLEAR ENGINEERING SCIENCES DEPARTMENT Nuclear Reactor Facility Universityof Florida I
w.avemeeson.oi,.ceer NUCLEAR REACTOR BUILDN6G ATTACHMENT II Gainevue,Florido 32411 Phone (904) 392-1429.Teles 56330 April 2, 1987 MOMORANDUM TO: UFTR Staff FROM: W.G. Vernetson
SUBJECT:
Alternate Authorized Control Blade Positions
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Based on the 1 watt critical position determination on' April 1, 1987 (540, 540, 540, 424) following the 6.8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> full power run on March 31, 1987 which produced considerable xenon, the alter-nate authorized control blade positions as of April 2, 1987 shall be:
Safety-1: 550 units safety-2: 550 units Safety-3: 550 units with the Regulating Blade up to where required for criticality.
Note that this set is an alternate authorized control blade bank position, the use of which must be approved by Level 3 (Reactor t
Manager or designated alternate) or above each time it is used.
Documented verbal permission is acceptable.
This alternate authorized set of control Blade Positions is to be implemented per the Corrective / Preventive Actions delineated in the attached memo - item number 1 to prevent occurrences such as the overpower trip on April 1,1987 due to operations with the regulating blade removed beyond 750 units such as for xenon, ex-periment worth, etc.
Any settings other than these must also be authorized by the Reactor Manager or Facility Director.
WGV/ps cc: P.M. Whaley RSRS S-3 F.k tw opsxwtuney/Amirncswo Action tervoyer