ML19332D019

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Application for Amend to License DPR-29,requesting Temporary Waiver of Compliance to Tech Spec 3.7.D.1 Which Requires That Isolation Valves Listed in Table 3.7-1 Be Operable During Power Operation.Head Spray Valves Cannot Be Removed
ML19332D019
Person / Time
Site: Quad Cities Constellation icon.png
Issue date: 11/15/1989
From: Stols R
COMMONWEALTH EDISON CO.
To: Murley T
Office of Nuclear Reactor Regulation
Shared Package
ML19332D020 List:
References
0371T, 371T, NUDOCS 8911290305
Download: ML19332D019 (3)


Text

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o 4 , 7 j Commonwealth Edloon

+  : 72 West Adams Street, Crucap, ihmois ,

[Ls A33fEIs7Fehry i676sfDffi6e BoTIBI Ctucago,Ilknois 60690 0767 j

j L November 15, 1989 l

N Dr. Thomas E. Hurley, Director  !

Office of Nuclear Reactor Regulation U.S. Nuclear Regulatory Commission Washington, DC 20555  ;

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Subject:

Quad Cities Station Unit 1 Application for Amendment to facility 'i Operating License DPR-29, Appendix A  !

Tochrical Specification; RRC_hodaLMou50454 __.

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Reference:

R. Stols to T. E. Hurley letter dated  !

June 9, 1989 j Dr. Hurley -l Commonwealth Edison requests that a Temporary Halver of Compliance be granted to allow the restart of Qua0 Cities Unit 1. The basis for this request  ;

is delineated in Attachment 1. Commonwealth Edison requests that the Halver of Compilance be in effect during the review and approval period for the proposed Technical Specification. The proposed changes are delineated in- ,

Attachment 2 and further discussed in Attachments 3 and 4. 1 Members of the Commonwealth Edison and NRC Staffs have discussed the circumstances of the event on November 14, 1989 and it was agreed that a .t o 3 Temporary Halver of Compliance should be pursued to document the acceptability of unit startup until the amendment-can be reviewed and approved. .

-l The proposed changes have been reviewed and approved by both On-site and Off-site review in accordance with Commonwealth Edison Company's proce- ,

dures. The; proposed amendment has been reviewed in accordance with 10 CFR 50.92.(c) and it has been determined that the proposed amendment does not '

involve.a significant hazards consideration. The evaluation is documented in Attachment 5.

Commonwealth Edison is notifying the State of Illinois by providing a  :

1-copy of this letter and the Attachments to the designated State'0fficial.

1 0371T:1 8911290305 891115 DR ADOCK0500g4  ;

\ l a

' 'O o Dr. T.E. Murley >2- November 15, 1989 i

L Commonwealth Edison requests a review and approval of this proposed Temporary Walver of Compliance and amendment on an expedited basis.

Commonwealth Edison appreciates the Staff's prompt attention to this matter.

I Please direct any questions you may have regarding this matter to this office.

Very truly yours, l

f' R. Stols '

Nuclear Licensing Administrator i 1m Attachments cc: T.M. Ross - Project Manager, Quad Cities R.L. Higgins - Senior Resident Inspector, Quad Cities A.B. Davis - Regional Administrator, RIII Office of Nuclear facility Safety - IDNS l

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0371T:2 l

S .

F A11ACHMlltI_1 BASIll0fLIEMEQRARLMIVER OF _ COMPLIANCE _REMESI V

Commonwealth Edison has identified that literal compliance to Technical Specification 3.7.0.1 cannot be achieved due to a plant modification which was performed during the Unit 1 Refueling Outage. Durir,g the Unit 1 outage, the Head Spray line and valves were removed as part of the IGSCC mitiga-tion program. . Commonwealth Edison notified the NRC of the intent to perform the modification in the Unit 1 IGSCC Inspection Plan submitted on Junc 9, 1989, 1 however, failed to submit the associated Technical SpecificcMon to allow for NRC issuance of the amendment prior to startep., This was identified during a review of Technical Specification amendments to be incorporated in the Quad Cities' Technical Specification Improvement Program. Commowealth Edison is performing an investigation on the root cause of the event. Appropriate corrective actions will be implemented based on the investigation results.

Current Technical Specification 3.7,0.1 requires that all isoletion valves listed on Table 3.7-1 be operable during power operation. Head Spray Valves H0-1001-60 and 1001-63 w1re included in the listing of isolation valves.

Due to the removal of these valves, literal compliance cannot be achieved.

Technical Specification 3.7.0.2 states that in the event an isolation valve becomes inoperable, reactor power operation may continue, provided at least one valve in each line is in the mode corresponding to the isolated condition. The remaining piping on the head spray system (reactor side) is fitted with a blind flange,.thereby the intent (not the letter) of Specification 3.7.D.2 is met.

The current configuration is thereby consistent with the philosophy of providing the isolation of the reactor pressure boundary to prevent a unisolable release pathway 1n the event of an accident. The modification was tested to ensure integrity of the installation. Commonwealth Edison therefore request that a temporary waiver of compilance be granted to allow the restart of Unit 1. Unit

.startup 1s currently scheduled for Saturday, November 18.

0371T:3