Similar Documents at Salem |
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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0261998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 1.With 990115 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr ML18106A9831998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 2.With 981214 Ltr ML18106A9801998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 1.With 981214 Ltr ML18106A9641998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 2. with 981112 Ltr ML18106A9631998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 1. with 981112 Ltr ML18106A9151998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 2.With 981012 Ltr ML18106A9131998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 1.With 981012 Ltr ML18106A8751998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Generating Station,Unit 2.With 980915 Ltr ML18106A8741998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Unit 1.With 980915 Ltr ML18106A8161998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 1. W/980817 Ltr ML18106A8151998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 2. W/980817 Ltr ML18106A7151998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 2. W/980715 Ltr ML18106A7141998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 1. W/980715 Ltr ML18106A6541998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 1. W/980615 Ltr ML18106A6531998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 2. W/980615 Ltr ML18106A6121998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Generating Station,Unit 1.W/980515 Ltr ML18106A6111998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Unit 2. W/980515 Ltr ML18106A5561998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem,Unit 1. W/980415 Ltr ML18106A4591998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem Unit 2. W/980415 Ltr ML18106A3771998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 1.W/980316 Ltr ML18106A3761998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 2.W/980316 Ltr ML18106A3281998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 2. W/980217 Ltr ML18106A3271998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 1. W/980217 Ltr ML18106A2721997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem,Unit 2. W/980115 Ltr ML18106A2711997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem Generating Station,Unit 1.W/980115 Ltr ML18106A2081997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 1. W/971212 Ltr ML18106A2071997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 2. W/971212 Ltr ML18102B6811997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 2.W/ 971117 Ltr ML18102B6801997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 1.W/ 971117 Ltr ML18102B6271997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Salem,Unit 2. W/971015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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e PS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit October 11, 1995 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555.
Attn.: Document Control Desk MONTHLY OPERATING REPORT SALEMN0.1 DOCKET NO: 50-272 In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original copy of the monthly operating reports for the month of September are being sent to you.
General Manager -
Salem Operations RH:vls Enclosures C Mr. Thomas T. Martin Regional Administrator USNRC, Region I 631 Park Avenue King of Prussia, PA 19046 8-1-7.R4 The power is in your hands.
9510190067 950930 PDR ADOCK 05000272 95-2168 REV. 6/94 R PDR
AVERAGE DAILY UNIT POWER LEVEL
'1 e
Docket No.: 50-272 Unit Name: Salem #1 Date: 10/10/95 Completed by: Robert PhiTl.j:J)S Teleeh~!!e: 339-2735 Month September 1995 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 0 17 0 2 0 18 0
-~*-- **---*
3 0 19 0 4 0 20 0 5 0 21 0 6 0 2~ 0 7 0 23 0 8 0 24 0 9 0 25 0 10 0 26 0 11 . 0:-- 27 0 12 0 28 0 13 0 29 0 14 0 30 0 15 0 31 16 0 P *. 8 .1-7 Rl
'~
OPERATING DATA REPORT ~
Docket No: 50-272 Date: 10/10/95 Completed by: Robert Phillips Telephone: 339-2735 Operating Status
- 1. Unit Name Salem No. 1 Notes
- 2. Reporting Period September 1995
- 3. Licensed Thermal Power (MWt) 3411
- 4. Nameplate Rating (Gross MWe) 1170
- 5. Design Electrical Rating (Net MWe) 1115
- 6. Maximum Dependable Capacity(Gross MWe) 1149
- 7. Maximum Dependable Capacity (Net MWe) 1106
- 8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason~~~-N...........A~~~~~~~~~~~~~~~~~~~~~~-
- 9. Power Level to Which Restricted, if any (Net MWe) N/A
- 10. Reasons for Restrictions, if any NA This Month Year to Date Cumulative
- 12. Hours in Reporting Period 720 6551 160008 12~ No. of Hrs. Rx. was Critical 0 2660.9 104380
- 13. Reactor Reserve Shutdown Hrs. 0 0 0
- 14. Hours Generator on-Line 0 2632.1 100388.3
- 15. Unit Reserve Shutdown Hours 0 0 0
- 16. Gross Thermal Energy Generated (MWH) 0 8010326.4 318062229.2
- 17. Gross Elec. Energy Generated (MWH) 0 2689850 105301000
- 18. Net Elec .. Energy Gen. (MWH) -3133 2529502 100211666
- 19. Unit Service Facto~ 0 40.2 62.7
- 20. Unit Availability Factor 0 40.2 62.7
- 21. Unit Capacity Factor (using MDC Net) 0 34.9 56.6
- 22. Unit Capacity Factor (using DER Net) 0 34.6 56.2
- 23. Unit Forced Outage Rate 26.7 56.3 22.9
- 24. Shutdowns scheduled over next 6 months (type, dat~ and duration of each)
Scheduled refueling outage.
- 25. If shutdown at end of Report Period, Estimated Date of Startup:
Under review.
8-1-7.R2
UNIT SHUTDOWN AND POWER REDUCTIONS REPORT MONTH: SEPTEMBER 1995 DOCKET NO.: 50-272 UNIT NAME: Salem #1 DATE: 10/10/95 COMPLETED BY: Robert Phillips TELEPHONE: 609-339-2735 METHOD OF SHUTTING LICENSE
' DURATION DOWN EVENT SYSTEM COMPONENT CAUSE AND CORRECTIVE ACTION 1 2 NO. DATE ! TYPE (HOURS) REASON REACTOR REPORT # CODE 4 CODE 5 TO PREVENT RECURRENCE 2671 9-1-95 F 720 D 4 --------- SH CKTBRK Tech Spec. 3.0.3 e
1 2 3 4 5 F: Forced Reason Method: Exhibit G - Instructions Exhibit 1 - same S: Scheduled A-Equipment Failure (explain) 1-Manual for Preparation of Data Source B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (LER) File D-Requlatory Restriction 4-Continuation of (NUREG-0161)
E-Operator Training & License Examination Previous Outage F-Administrative 5-Load Reduction G-Operational Error (Explain) 9-0ther H-Other (Explain)
10CFR50.59 EVALUATIONS DOCKET NO: 50-272 MONTH: SEPTEMBER 1995 UNIT NAME: SALEM 1 DATE: 10/10/95 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5162 The following items were evaluated in accordance with the proVisions of the Code of Federal Regulations 10CFR50.59. The Station Operations Review Committee has reviewed and concurs with these evaluations.
- 1. Design Change Packages (DCP)
The reporting ofDCP related 10CFR50.59 evaluations is being modified to address these items only after they have been implemented and turned over to Operations. For the next several months, during this transition phase, we anticipate few new DCPs to report.
- 2. Temporary Modifications (T-Mod)
T-Mod 95-058 "Installation of a Blind flange on 12SE72 Outlet Piping" - The purpose of this modification is to provide a secondary boundary for the leaking 12SW76 isolation valve. This temporary modification will add a blank flange in the 10" line 1-SW-P-1665 on the outlet pipe flange to the removed 12SW72 valve.
The supply and return line to Fan Coil Unit 1SWE25 (No. 12 Containment Fan Coil Unit) was isolated and tagged. The tagged valves are 12SE54, supply, and 12SW76, return. Valve 12SW72.was removed for maintenance. Valve 12SW76 will not fully isolate and leaks by. The leakage is being drained through drain valve 12SW425 with the water flow being directed to the floor drain. With the discharge header being placed back into service, the flow through the leaking valve will be too much for the floor drain to handle. Therefore it is necessary to install this blank flange. The blank flange is equivalent to a tagged closed valve. No new equipment configurations are introduced by this T-Mod. The Technical Specifications were reviewed and found to be not applicable for the current mode (undefined) and configuration. There is no reduction in the margin of safety as defined in the basis for any Technical Specification. (SORC 95-107)
IOCFR50.59 EVALUATIONS DOCKET NO: 50-272 MONTH: SEPTEMBER I995 UNIT NAME: SALEM I DATE: 10/I0/95 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5I62 (Cont'd)
- 3. Procedures SI .MD-FR.ZZ-0003(Z) "Alternate Power Source for Cafeteria" Rev. 0 - The purpose of this procedure is to provide the instructions necessary to temporarily install power cables between 2HL (280/120 Volt Bus) and breaker IHIAY (output side). With breaker 2HL4Y closed and breaker IHL4Y open, power is provided to cafeteria power panels CPP I and CPP2 during #I I Station Power Transformer (SPT) outage or when 4I60 280/I20V Transformer IXFRIH3DAY is out of service. All equipment affected by the procedure is located within the turbine buildings (UI and U2). The IHL/2HL 208/120V AC busses do not supply any equipment important to safety nor do they affect any equipment important to safety. In addition, the loading on the alternate power source (2HL) will be limited to ensure overload/overcurrent conditions do not develop. The IHL/2HL
. 208/I20V AC busses are not covered by the Technical Specifications. Neither the busses nor the equipment supplied by the busses affect the margin of safety as defined in the bases of the Technical Specifications. (SORC 95-100)
Sl.MD-FR.230-000I(Q) "IF-IH 230 Volt Bus Crossfeed," Rev. 0 - This procedure provides the instructions necessary to install temporary power cables between IH 230 Volt group bus and IF 230 Volt group bus during respective Station Power Transformer (SPT) outages or 4I60-240/139V transformer outages. During I2SPT outage or 4160-240/139V Transformer lXFRlFSDBY outage, breaker lHY is closed and breaker lFY is open, resulting in IF 230 Volt bus being powered from lH 230 Volt bus. During I ISPT outage or 4160-240/139V Transformer IXFRIHSDBY outage, breaker IFY is closed and breaker lHY is open, resulting in lH 230 Volt bus being powered from IF 230 Volt bus. Busses lH and IF (230V AC group busses) are not covered by Technical Specifications. Neither the busses nor the equipment supplied by the busses affect the margin of safety as defined in the bases of the Technical Specifications.
(SORC 95-100)
10CFR50.59 EVALUATIONS DOCKET NO: 50-272 MONTH: SEPTEMBER 1995 UNIT NAME: SALEM 1 DATE: 10/10/95 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5162 Security Procedure 9 "Control of Packages and Materials," Rev. 0 - The revision deletes the requirement for controlling personnel and material access to the primary reactor containment from within the adjacent vital area. Personnel access control will continue to be applied for access from the protected area to Salem's containments through the equipment hatches. The proposal involves no plant equipment and does not reduce the quality of oversight of the Security Program. There is no reference to the security control of primary reactor containment. There is no reduction in the margin of safety _as defined in the basis for any Technical Specification. (SORC 95-101)
Security Procedure SP7 "Personnel Access Control," Rev. 7 - Security Procedure SP7 is being revised in response to a change to the Federal Regulations
- deletion of 10CFR73.55(d)(8). This has eliminated the requirement for controlling personnel and material access to primary reactor containment from within an adjacent vital area.
Personnel access control will continue to be applied for access from the protected area to Salem's containments through the equipment hatches. The proposal involves no plant equipment and does not reduce the quality of oversight of the Security Program. There is no reference to the security control of primary reactor containment. There is no reduction in the margin of safety as defined in the basis for any Technical Specification. (SORC 95-110)
- 4. Updated Final Safety Analysis Report (UFSAR) Change Notice SCN 95-36 "Sections 17 .2.2 & Table 17.2-1 J .1.1 a" - The purpose of this submittal is to change the station's UFSAR by deleting the security program (administrative procedures) from the Q-List in Table 17.2.1, and reference to Regulatory Guide 1.17, Protection of Nuclear Plants Against Industrial Sabotage, (which has been revoked by the NRC) from Section 17.2.2.
Regulatory Guide 1.33 Appendix A cites Security & Visitor Control as activities that should be covered by written administrative procedures. There is no reference to the security
10CFR50.59 EVALUATIONS DOCKET NO: 50-272 MONTH: SEPTEMBER 1995 UNIT NAME: SALEM 1 DATE: 10/10/95 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5162 system. Quality requirements applicable to Security are contained in 10CFR73.55 and in the Security Plan (UFSAR Section 13.6). Therefore the Q-Listing of the Security Program is redundant. Its removal from the Q-List will have no effect on the quality or oversight of the Security Program. The proposal involves no plant equipment and does not reduce the quality of oversight of the Security Program. There is no reduction in the margin of safety as defined in the basis for any Technical Specification. (SORC 95-101)
REFUELING INFORMATION DOCKET NO: 50-272 MONTH: SEPTEMBER 1995 UNIT NAME: SALEM 1 DATE: 10/10/95 COMPLETED BY: R.HELLER TELEPHONE: 609-339-5162 MONTH : SEPTEMBER 1995 .
Refueling information has changed from last month: YES X. NO _ _
Scheduled date for next refueling: 07/10/95 Scheduled date for restart following refueling: 1st quarter 1996
- a. Will Technical Specification changes or other license amendments be required?
YES NO~_
NOT DETERMINED TO DATE _X_
- b. Has the reload fuel design been reviewed by the Station Operating Review Committee?
YES NO X If no, when is it scheduled? (to be determined)
Scheduled date(s) for submitting proposed licensing action: ---~N~/_A_____
Important licensing considerations associated with refueling:
Number of Fuel Assemblies:
- a. Incore 0
- b. In Spent Fuel Storage 1005 Present licensed spent fuel storage capacity: 1632 Future spent fuel storage capacity: 1632 Date of last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity: September 2008 8-1-7.R4
SALEM GENERATING STATION MONTHLY OPERATING
SUMMARY
- UNIT 1 OCTOBER 1995 SALEMUNITNO. 1 The Unit is in a refueling outage and remained shutdown for the entire period. According to commitments from PSE&G and a subsequent confirmatory action letter from the NRC, both Units will remain shutdown pending completion of the following actions:
- Appropriately address long standing equipment reliability and operability issues
- After the work is completed, conduct a restart readiness review to determine for ourselves the ability of each Unit to operate in a safe, event free manner
- After the restart review, meet with the NRC and communicate the results of that review