Similar Documents at Salem |
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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0261998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 1.With 990115 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr ML18106A9831998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 2.With 981214 Ltr ML18106A9801998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 1.With 981214 Ltr ML18106A9641998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 2. with 981112 Ltr ML18106A9631998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 1. with 981112 Ltr ML18106A9151998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 2.With 981012 Ltr ML18106A9131998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 1.With 981012 Ltr ML18106A8751998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Generating Station,Unit 2.With 980915 Ltr ML18106A8741998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Unit 1.With 980915 Ltr ML18106A8161998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 1. W/980817 Ltr ML18106A8151998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 2. W/980817 Ltr ML18106A7151998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 2. W/980715 Ltr ML18106A7141998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 1. W/980715 Ltr ML18106A6541998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 1. W/980615 Ltr ML18106A6531998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 2. W/980615 Ltr ML18106A6121998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Generating Station,Unit 1.W/980515 Ltr ML18106A6111998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Unit 2. W/980515 Ltr ML18106A5561998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem,Unit 1. W/980415 Ltr ML18106A4591998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem Unit 2. W/980415 Ltr ML18106A3771998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 1.W/980316 Ltr ML18106A3761998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 2.W/980316 Ltr ML18106A3281998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 2. W/980217 Ltr ML18106A3271998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 1. W/980217 Ltr ML18106A2721997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem,Unit 2. W/980115 Ltr ML18106A2711997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem Generating Station,Unit 1.W/980115 Ltr ML18106A2081997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 1. W/971212 Ltr ML18106A2071997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 2. W/971212 Ltr ML18102B6811997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 2.W/ 971117 Ltr ML18102B6801997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 1.W/ 971117 Ltr ML18102B6271997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Salem,Unit 2. W/971015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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. e OPS~G Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit March 15, 1995 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Attn.: Document Control Desk MONTHLY OPERATING REPORT SALEMNO. 2 DOCKET NO: 50-311 In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original copy of the monthly operating reports for the month of February are being sent to you.
Sincerely yours, 1ftfu.__,
John C. Summers General Manager -
Salem Operations RH:vls Enclosures C Mr. Thomas T. Martin Regional Administrator USNRC, Region I 631 Park Avenue King of Prussia, PA 19046 8-1-7.R4
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~ OPERATING DATA REPORT ~
Docket No: 50-311 Date: 03/10/95 Completed* by: Mike Morroni Telephone: 339-2122 Operating Status
- 1. Unit Name Salem No. 2 Notes
- 2. Reporting Period February 1995
- 3. Licensed Thermal Power (MWt) 3411
- 4. Nameplate Rating (Gross MWe) 1170
- 5. Design Electrical Rating (Net MWe) 1115
- 6. Maximum Dependable Capacity(Gross MWe) 1149
- 7. Maximum Dependable Capacity (Net MWe) 1106
- 8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason NA
- 9. Power Level to Which Restricted, if any (Net MWe) N/A
- 10. Reasons for Restrictions, if any NA This Month Year to Date Cumulative
- 11. Hours in Reporting Period 672 1416 117289
- 12. No. of Hrs. Rx. was Critical 266 266 75881. 2
- 13. Reactor Reserve Shutdown Hrs. 0 0 0
- 14. Hours Generator On-Line 89.2 89.2 73057.1
- 15. Unit Reserve Shutdown Hours 0 0 0
- 16. Gross Thermal Energy Generated (MWH) 136886.4 13886.4 181110670.6 Gross Elec. Energy Generated (MWH) 30350 30350 76480358
- 18. Net Elec. Energy Gen. (MWH) 12090 - 5777 72717767
- 19. Unit Service Factor 13.3 6.3 62.3
- 20. Unit Availability Factor 13.3 6.3 62.3
- 21. Unit Capacity Factor (using MDC Net) 1. 6 0 56.1
- 22. Unit Capacity Factor (using DER Net) 1.6 0 55.6
- 23. Unit Forced Outage Rate 85.1 85.1 22.2
- 24. Shutdowns scheduled over next 6 months (type, date and duration of each)
We are presently in a maintenance outage.
- 25. If shutdown at end of Report Period, Estimated Date of Startup:
3 07 95.
8-1-7.R2
.ERAGE DAILY UNIT POWER LE. .
Docket No.: 50-311 Unit Name: Salem #2 Date: 03-10-95 Completed* by: Mike Morroni Telephone: 339-2122 Month February 1995 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 0 17 339 2 ,o 18 401 3 0 19 239 4 0 20 0 5 0 21 0 6 0 22 0 7 0 23 0 8 0 24 0 9 0 25 0 10 0 26 0-11 0 27 0 12 0 28 0 13 0 29 14 0 30 15 0 31 16 128 P. 8.1-7 Rl
UNIT SHUTDOWN AND POWER REDUCTIONS REPORT MONTH FEBRUARY 1995 DOCKET NO. 50-272 UNIT NAME Salem #2 DATE 3-10-95 COMPLETED BY Mike Morroni TELEPHONE 339-5142
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'I METHOD OF
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SHUTTING LICENSE
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! " DURATION r DOWN I EVENT .\ SYSTEM .*COMPONENT CAUSE AND CORRECTIVE ACTION
'NO.**_;, f:: 1.:DATE *'
TYPE 1 I'. (HOURS)* !' REASON 2 REACTOR *REPORT # CODE 4 CODE 5 TO PREVENT RECURRENCE
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. 02/01/95. ,,.*, s.: _': 72 I
l*, c ', 4 ------------ RC FUELXXXXXX NORMAL REFUELING i :
. 2346 02/03/95 I... F- 291.3. '. D 4 .. ...................... IA xxxxxxxxxx SSPS DESIGN INADEQUACY 2371 02/19/95 . . ,
F .. 236 A 1 ------------ CB PUMPXXXXXX 21 RCP SEAL 1----------- :
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1 2 3 4 5 F: Forced ... :.*c Reason
- Method: Exhibit G - Instructions Exhibit 1 - Same S: Scheduled .:: .A-Equipment Failure (explain) *1-Manual for Preparation of Data Source
'. ,,. B-Maintenance or Test ' * *
- 2-Manual Scram Entry Sheets for Licensee
- . ,,*.*:C-Refuel ing - .* ..' 3-Automatic Scram Event Report CLER) File
- ~* D-Requlatory Restriction ,,, 4-Continuation of CNUREG-0161)
E-Operato~:Training & License Examination Previous outage
-: **'-' F-Admini strative 5-Load Reduction G-Operational Error (Explain) 9-0ther H-Other (Explain)
10CFRS0.59 EVALUATIONS DOCKET NO: 50-311 MONTH: FEBRUARY 1995 UNIT NAME: SALEM2 DATE: 03/10/95 COMPLETED BY: R. HELLER TELEPHONE: 609-339-5162 The following items were evaluated in accordance with the provisions of the Code of Federal Regulations 10CFR50.59. The Station Operations Review Committee has reviewed and concurs with these evaluations.
- 1. Design Change Packages (DCP) 2EC-3323, Pkg. 1 "Revision of Rod Control System Auctioned Ave Lead/Lag Module and Filter Module Time Constants" Rev. 0 - The purpose of this DCP is to implement a recommendation from the primary vendor to PSE&G that the filter time constant (module 2TM-412P be revised to 10 seconds, the lead/lag time constant (module 2TM-412Q) be revised to 40/10. These changes are being made to eliminate false rod stepping. Operation of the plant with the revised rod control system compensation parameters does not adversely affect any physical parameters or conditions which are addressed in the Technical Specifications. The FSAR accident analysis remains bounding. Therefore, the margin of safety, as defined in the bases to the Technical Specifications is not reduced. (SORC 95-013) 2EC-3351, Pkgs.1&2 "SSPS Turbine Building Inputs" Rev. 0 - This modification reconfigures the SSPS input bay wiring such that the logic power supplies will not be affected by a postulated short to ground of the SSPS input wiring that interfaces with contacts in the turbine building. The new configuration moves the 120 V AC power feed for the SSPS logic power supplies upstream of existing 15 amp fuses such that fuses feed only the input relays through contacts located in the turbine building. The power supplies are individually fused.
The modification also replaces existing 15 amp fuses with 5 amp fuses to properly coordinate with the upstream breaker.
These modifications only correct a condition which was not previously thought to be credible, that is, a loss of the SSPS functionality due to a Design Basis Event. These modifications do not, in any way, alter
- 10CFRS0.59 EVALUATIONS DOCKET NO: 50-311 MONTH: FEBRUARY 1995 UNIT NAME: SALEM 2 DATE: 03/10/95 COMPLETED BY: R. HELLER TELEPHONE: 609-339-5162 the function of SSPS. There is no reduction in the margin of safety as defined in the bases for any Technical Specification. (SORC 95-017) 2EE-0088, Pkg. 1 No. 22 Charging Safety Injection Pump Inboard Mechanical Seal Housing Replacement" Rev. 0 - This modification entails the replacement of a leaking inboard mechanical seal assembly and seal housing on No. 22 Charging Safety Injection (C/SI) pump. The seal housing of the new mechanical seal assembly, which is a later design, does not have the jacket water cooling connections or a design requirement for these cooling connections. As noted in Dresser Pacific (pump manufacturer) letter dated 8/24/84, the later design seal housings were revised to eliminate the cooling water jackets in 1976 and all pumps manufactured since have no seal housing water jackets. Nos. 11, 12 and 21 C/SI pumps have already been updated with new mechanical seals and housing and the component cooling connections have been cut back and capped. Unlike the other pumps, at this time, the proposed change to No. 22 C/SI pump will not change the outboard mechanical seal, which still has active connections for cooling the seal housing. The operability and reliability of the charging pump is not affected by the installation of a replacement seal assembly. The acceptance criteria for the design basis accidents continue to be met and the margin of safety as defined in the Technical Specifications is unchanged.
(SORC 95-025)
- 2. Temporary Modifications (T-Mods)95-020 "Blind Flange Installation at Relief Valves 21-23CN141/142 and 21 and 22BF82" Rev. 0 - The purpose ofthis T-Mod is to remove reliefvalves 21-23CN141/142 and 21 and 22BF82 and install blind flanges to restore the leak tight integrity of the condensate and feedwater systems
10CFRS0.59 EVALUATIONS DOCKET NO: 50-311 MONTH: FEBRUARY 1995 UNIT NAME: SALEM 2 DATE: 03/10/95 COMPLETED BY: R. HELLER TELEPHONE: 609-339-5162 (Cont'd) respectively. The subject valves which are currently leaking through the valve seats, were installed to provide thermal relief protection for sections of piping/components in the condensate and feed water system, which if isolated during system heatup or power operations, could be ovepressurized. The subject relief valves were not designed/ installed to provide overall system overpressurization protection during normal system operations or transient conditions. The piping/components being temporarily modified are classified as non-safety related/non-seismic and perform no safety function.
Therefore, this modification will have no impact on any systems or equipment required for safe shutdown. There is no reduction in the margin of safety as defined in the bases for any Technical Specification. (SORC 95-020)93-140 "Salem Unit 2 Fuel Handling Crane Upgrade for Spent Fuel Pool Reracking - Revision to Ambient Temperature Requirement in Fuel Handling Building and Installation of Heater Plates on Top of Rack Handling Trolley" Rev. 1 -
To increase the spent fuel storage capacity of the Spent Fuel Pool (SFP), the existing nine Exxon racks will be removed and replaced with nine new Holtec racks. Due to the weight of the racks, the Fuel Handling Crane capacity needs to be increased from 5 tons to 20 tons. This T-Mod will install a new trolley and hoist for the removal and installation of racks. The existing trolley and hoist will be used for moving the spent fuel. The purpose of this revision is to add heater strips to the fracture critical members of the new trolley to maintain a temperature above 45°F when the ambient temperature falls below that level. This upgrading is in compliance with the provisions ofNUREG-0554, and in accordance with Appendix C to NUREG-0612. There is no reduction in the margin of safety as defined in the bases for any Technical Specification. (SORC 95-020)
- 10CFRS0.59 EVALUATIONS DOCKET NO: 50-311 MONTH: FEBRUARY 1995 UNIT NAME:* SALEM 2 DATE: 03/10/95 COMPLETED BY: R. HELLER TELEPHONE: 609-339-5162
- 3. Deficiency Reports (Use-As-Is) 950131128 "Justification For Allowing Uninsulated Portion of Pipe on 2PR3, 4 & 5 Inlet to Remain Uninsulated Until Next Outage" Rev. 0 - This proposal allows a small portion of the pressurizer safety relief valve (SRV) inlet piping to remain uninsulated until the next refueling outage. This proposal does not add, delete or modify any safety related equipment or components. The lack of insulation on a small portion of the SRV inlet piping does not compromise the safety related function of any safety related electrical equipment, the SRVs, or their associated piping. As such, this proposal does not impact any anticipated operational transients or design basis accidents previously evaluated in the UFSAR. There is no reduction in the margin of safety as defined in the basis for any Technical Specification.
(SORC 95-016)
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REFUELING INFORMATION
- 50-311 MONTH: FEBRUARY 1995 UNIT NAME: SALEM2 DATE: 03/10/95 COMPLETED BY: R. HELLER TELEPHONE: 609-339-5162 MONTH: FEBRUARY 1995
- 1. Refueling information has changed from last month: YES X'NO
- 2. Scheduled date for next refueling: April 6. 1996 Scheduled date for restart following refueling: June 5. 1996
- 3. a. Will Technical Specification changes or other license amendments be required?
YES_ NO NOT DETERMINED TO DATE X
- b. Has the reload fuel design been reviewed by the Station Operating Review Committee?
YES NO X If no, when is it scheduled? April 1996
- 5. Scheduled date(s) for submitting proposed licensing action: _ _ ____,.N~/~A=_ _ __
- 6. Important licensing considerations associated with refueling:
- 7. Number ofFuel Assemblies:
- a. Incore 193
- b. In Spent Fuel Storage 556
- 8. Present licensed spent fuel storage capacity: 1632 Future spent fuel storage capacity: 1632
- 9. Date of last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity: March 2012 8-1-7.R4
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SALEM GENERATING STATION MONTHLY OPERATING
SUMMARY
- UNIT 2 FEBRUARY 1995 SALEM UNIT NO. 2 The Unit began the period shutdown as the refueling outage activities continued. The Unit entered Mode 2 (Startup) on February 10, 1995, and was synchronized to the grid on February 16, 1995. During the subsequent power escalation, problems developed with No. 21 Reactor Coolant Pump (RCP) seal leakoffflow and on February 19, 1995, the Unit was removed from service. The Unit remained shutdown throughout the rest of the period while the RCP seal replacement was in progress.
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