05000293/FIN-2018002-06
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Finding | |
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Title | Minor Violation |
Description | This violation of minor significance was identified by the licensee and has been entered into the licensees corrective action program and is being treated as a minor violation, consistent with the NRC Enforcement Policy. On June 22, 2015, Entergy submitted a licensee event report in accordance with 10 CFR 50.73 that contained information that was not complete or accurate in all material respects, contrary to the requirements in 10 CFR 50.9. Specifically, the licensee submitted Licensee Event Report 2015-004-00 to communicate the failure during testing of time delay Agastat relay 27A-B1X/TDDO intended to provide under-voltage protection for 480V emergency bus B6 by transferring power from bus B1 to bus B2. In the licensee event report, Entergy incorrectly documented that due to the failure, bus B6 would have continued to receive power from bus B1 with degraded voltage. Upon identifying the issue, on March 8, 2016, Entergy submitted a revised licensee event report with the correct information. Enforcement: 10 CFR 50.9 requires that information provided to the Commission by a licensee shall be complete and accurate in all material respects. Contrary to the above, on June 22, 2015, Entergy provided information to the Commission that was not complete and accurate in all material respects. In the licensee event report, the licensee documented that due to the failure, bus B6 would have continued to receive power from bus B1 with degraded voltage. However, bus B6 would actually have tripped from bus B1 and lost power completely. This information was material to the NRC because the NRC requires timely and accurate reporting of information related to events in order to evaluate the potential safety significance and required NRC response. Entergy identified the inaccuracy and entered the issue into its corrective action program [CR-PNP-2015-9762]. On March 8, 2016, Entergy submitted a revision to the licensee event report (2015-004-01) that corrected the report. This failure to comply with 10 CFR 50.9 constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy. The disposition of this violation closes Licensee Event Report 05000293/2015-004-01. |
Site: | Pilgrim |
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Report | IR 05000293/2018002 Section 4OA3 |
Date counted | Jun 30, 2018 (2018Q2) |
Type: | Violation: Severity level Minor |
cornerstone | No Cornerstone |
Identified by: | Licensee-identified |
Inspection Procedure: | IP 71153 |
Inspectors (proximate) | E Carfang B Pinson P Boguszewski J Ambrosini S Wilson D Kern M Rossi M Mclaughlin A Dimitriadis |
Violation of: | 10 CFR 50.9 10 CFR 50.73 |
INPO aspect | |
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Finding - Pilgrim - IR 05000293/2018002 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Pilgrim) @ 2018Q2
Self-Identified List (Pilgrim)
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