05000324/FIN-2012005-03
From kanterella
Revision as of 14:04, 30 September 2017 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Finding | |
---|---|
Title | Inadequate Maintenance Procedure for the EDG Jacket Water Pump Wear Ring Tolerances |
Description | A self-revealing Green NCV of Technical Specification (TS) 5.4.1a, Procedures, was identified because the licensee did not have an adequate maintenance procedure to perform work on the emergency diesel generator (EDG) 3 engine-driven jacket water pump (JWP). Specifically, between July 25, 1992 and November 15, 2012, Procedure 0CM-ENG528, Gould Engine Driven Jacket Water Pump Model 3736, did not provide the correct tolerances for the EDG JWP wear rings, resulting in the JWP seizure. The licensees corrective actions included replacing the casing wear rings with wear rings with the correct tolerance and revising Procedure 0CM-ENG528. The licensee entered this issue into the corrective action program (CAP) as nuclear condition report (NCR) 572546. The performance deficiency associated with this finding was the failure of the licensee to have an adequate procedure for maintenance on the EDG 3 engine-driven JWP. The finding was more than minor because it was associated with the procedure quality attribute of the Mitigating Systems Cornerstone and affects the cornerstone objective of ensuring the availability and reliability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the inadequate procedure resulted in reduced availability of EDG 3 to repair the engine-driven JWP and reduced reliability of the jacket water system during operation. Using IMC 0609, Appendix A, issued June 19, 2012, The Significance Determination Process (SDP) for Findings At-Power, the inspectors determined the finding was of very low safety significance because the finding did not affect the design or qualification of a mitigating structure, system and component (SSC), the finding did not represent a loss of system and/or function, the finding did not represent an actual loss of a function of a single train for greater than the TS allowed outage time, the finding did not represent an actual loss of a function of one or more non-TS trains of equipment, and did not screen as potentially risk-significant due to a seismic, flooding, or severe weather initiating event. The finding does not have a cross-cutting aspect since the performance deficiency is not indicative of current plant performance. Procedure 0CM-ENG528 included the incorrect tolerances since July 25, 1992. |
Site: | Brunswick |
---|---|
Report | IR 05000324/2012005 Section 1R19 |
Date counted | Dec 31, 2012 (2012Q4) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71111.19 |
Inspectors (proximate) | A Nielsen D Lanyi J Laughlin J Montgomery M Bates M Catts M Schwieg P Niebaum R Baldwin R Musser R Rodriguez |
INPO aspect | |
' | |
Finding - Brunswick - IR 05000324/2012005 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
Finding List (Brunswick) @ 2012Q4
Self-Identified List (Brunswick)
| |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||