Semantic search

Jump to navigation Jump to search
Condition
Printout selection
Options
Parameters [
limit:

The maximum number of results to return
offset:

The offset of the first result
link:

Show values as links
headers:

Display the headers/property names
mainlabel:

The label to give to the main page name
intro:

The text to display before the query results, if there are any
outro:

The text to display after the query results, if there are any
searchlabel:

Text for continuing the search
default:

The text to display if there are no query results
class:

An additional CSS class to set for the table
transpose:

Display table headers vertically and results horizontally
sep:

The separator between results
prefix:

Control display of namespace in printouts
Sort options
Delete
Add sorting condition
 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 4492722 March 2009 20:34:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionUnit 1 Steam Generator Found in an Unanalyzed Condition Related to Gaps on Seismic Washer PlatesAt 1334 on March 22, 2009, while Unit 1 was in Mode 3, replacement steam generator (RSG) 1-3 was conservatively determined to be in an unanalyzed condition in that seismic washer plates were found to have nonconforming gaps on two of the four steam generator support columns. A plant walk down discovered that the two washer plates were not seated in the column adapter due to an interfering weld on the interior recess of the column adapter. Because of this condition, Technical Specification 3.0.3 was entered for Unit 1. At 1536 on March 22, 2009, a shim was installed between the washer plate and the column adapter at each of the two non-conforming locations on RSG 1-3 of sufficient thickness to clear the weld metal interfering with washers. This action brought the support columns for RSG 1-3, support foot joints into compliance with the full design capacity. Technical Specification 3.0.3 was exited for Unit 1 at that time. This issue was discussed with US NRC DCPP Senior Resident.Steam Generator05000275/LER-2009-001
ENS 4546123 October 2009 15:00:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionPost Loca Recirculation Valve Position InterlocksDuring the current Unit 2 fifteenth refueling outage (2R15), with the core off-loaded to the spent fuel pool, the containment recirculation sump valve interlock position switches were found not to perform correctly. Initial investigation has determined that the valve position sensing interlock switches were left incorrectly set during the Unit 2 fourteenth refueling outage (2R14). In the event of a Loss of Coolant Accident, (LOCA) this condition would have prevented Residual Heat Removal (RHR) flow from reaching containment spray, high head and intermediate head safety injection pumps following alignment to long term recirculation from the containment sump without additional operator action. The RHR function, including the long term recirculation from the containment sump, was not adversely affected by this condition. Also, containment spray, high head and intermediate head safety injection from the refueling water storage tank (RWST) was not adversely affected by this condition. Unit 2 containment recirculation sump valve interlock position switches have been correctly set and are being retested during the current 2R15. Unit 1 containment recirculation sump valve interlock position switches have been verified as correctly set to be capable of performing their design function by testing performed during the last refueling outage. This condition will be reported in a Licensee Event Report (LER) within 60 days in accordance with 10 CFR 50.73(a)(2)(ii). The licensee notified the NRC Resident Inspector.Residual Heat Removal
Containment Spray
05000323/LER-2009-003
ENS 4575410 March 2010 03:16:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionPotential Loss of 1E Pumps Due to Degraded Voltage During Postulated AccidentsWhile attempting to analyze the consequences of scenarios (loss of coolant accident (LOCA) and loss of offsite power (LOOP)) postulated during the Component Design Basis Inspection (CDBI), PG&E concluded both units were in an Unanalyzed Condition that significantly degrades plant safety, and therefore, reportable under 10 CFR 50.72(b)(3)(ii)(B). The postulated scenario could result in permanently connected class 1E pump motors tripping over current relays due to sustained degraded voltage on the startup offsite power source. The scenario starts with a safety injection (SI) signal transferring 4160 volt vital buses from auxiliary power to the startup offsite power source. Following bus transfer, the startup source is postulated to degrade to a level above the first level under voltage relay (FLUR) setting of equal to or greater than 2583 volts and below the second level under voltage relay (SLUR) setting of equal to or greater than 3785 volts. Permanently connected class 1E pump motors would experience this degraded voltage for up to the SLUR time delay relay setting of equal to or less than 20 seconds. Prior to reaching the SLUR time delay relay setpoint and transferring loads to the onsite emergency diesel generators (EDGs), operating motors (e.g. auxiliary saltwater (ASW) pump and component cooling water (CCW) pumps) could trip on over current. Operators would be directed by procedures to re-start these motors on an operable power source (EDG). However, since this scenario has not been previously analyzed and could reasonably challenge containment pressure or peak clad temperature limits, it is considered unanalyzed. The postulated scenario had previously been considered non-credible, and therefore, had not been analyzed. PG&E considers this a nonconservative technical specification (TS) since the values in TS surveillance requirement (SR) 3.3.5.3 would not protect permanently connected class 1E loads from damage during degraded voltage conditions." The licensee has notified the NRC Resident Inspector. The condition was discovered by NRC inspectors while performing a CDBI inspection.Emergency Diesel Generator05000275/LER-2010-002
ENS 4653110 January 2011 21:21:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Both Trains of Auxiliary Building Ventilation Became Inoperable

On January 10, 2011, at 1321 PST, Diablo Canyon Power Plant, Unit 2, entered Technical Specification Limiting Condition of Operation (TS LCO) 3.0.3, when both trains of Auxiliary Building Ventilation System (ABVS) became inoperable following closure of damper M-4 and the ensuing loss of both exhaust fans E-1 and E-2. TS LCO 3.0.3 was exited on January 10, 2011, at 1342 following a status reset and selection of fan E-2. This provided a ventilation flowpath and use of both exhaust fans in the Safeguards mode. Both trains of Auxiliary Building Ventilation are operable. This 8-hour non-emergency report is made pursuant to 10 CFR 50.72(b)(3)(v)(D). The unit is not in a TS LCO. All 3 unit EDG's are operable and offsite power is in the normal lineup. The NRC Resident Inspector has been notified.

  • * * UPDATE FROM WES FIANT TO DONALD NORWOOD AT 0021 EST ON 1/14/2011 * * *

On January 13, 2011, at 1603 PST, engineering determined that a single failure design vulnerability exists at Diablo Canyon Power Plant Units 1 and 2. Engineering review of the control logic of the ABVS determined that while in Buildings Only (non-safeguards) alignment or during system realignment from Safeguards Only to Buildings Only alignment, failure of damper M-4A or M-4B (series dampers) could result in the control logic securing both ABVS exhaust fans. This would prevent ABVS actuation on receipt of a valid safeguards actuation signal. When this occurs, a control room alarm is actuated, which requires the operators to reset the control logic from the control room, thereby re-enabling the capability of the ABVS to respond to a safeguards actuation signal. The Unit 2 event on January 10, 2011, at 1321, occurred due to this single failure vulnerability when the control system attempted to restore the ABVS alignment from Safeguards Only to the Buildings Only alignment. This design vulnerability is currently mitigated by maintaining the ABVS in either of the two safeguards alignments (Safeguards Only or Buildings and Safeguards). This single failure design vulnerability is an 8-hour non-emergency report made pursuant to 10CFR50.72(b)(3)(ii)(B) for an event that resulted in the nuclear power plant being in an unanalyzed condition for both Unit 1 and Unit 2. The licensee will notify the NRC Resident Inspector. Notified R4DO (Hagar).

05000275/LER-2011-002
ENS 4722330 August 2011 00:24:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionMaintenance Inadvertently Renders Control Room Ventilation System InoperableOn August 29, 2011, at 1724 PDT, plant operators discovered that the Control Room Envelope (CRE) boundary required by Technical Specification (TS) 3.7.10, 'Control Room Ventilation System (CRVS),' lost its integrity. This was due to maintenance personnel removing a blank flange on the line to Unit 2 CRVS dampers MOD-2 and MOD-2A with the dampers inoperable. On August 29, 2011, at approximately 1400 PDT, plant personnel completed maintenance on Unit 2 control room dampers MOD-2 and MOD-2A and planned to perform static testing of the CRE on the morning of August 30, 2011. Prior to reporting off the clearance, maintenance personnel removed a blank flange from the upstream side of the dampers. This blank flange was maintaining the integrity of the CRE boundary while dampers MOD-2 and MOD-2A were inoperable during the maintenance. Upon completion of maintenance on the dampers, the blank flange was removed with shift foreman authorization. Later, personnel recognized that the flange had been removed prematurely while dampers MOD-2 and MOD-2A were still inoperable. Personnel took required actions associated with TS 3.7.10 and re-installed the blank flange on August 30, 2011, at 0110 PDT. The loss of the CRE boundary rendered the CRVS incapable of performing its specified safety function of mitigating the exposure of control room personnel to the consequences of an accident. The cause of the event was inadequate coordination between maintenance personnel and plant operators to maintain the integrity of the CRE boundary. Plant personnel notified the NRC Resident Inspector.Control Room Envelope
ENS 4725813 September 2011 00:45:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionControl Room Envelope Declared Inoperable

On September 12, 2011, at 1745 PDT operators declared the control room envelope (CRE) inoperable and entered Technical Specification (TS) 3.7.10 Action B. This was due to discovery of inadequately documented CRE in-leakage test data. On September 12, 2011, DCPP (Diablo Canyon Power Plant) personnel reviewing the CRE testing dated February 3, 2005 determined that the test report provided inadequate information to conclude that the most limiting alignment for control room pressurization would result in zero cubic feet per minute (CFM) in-leakage into the CRE, contrary to the Final Safety Analysis Report (FSAR) accident analysis for the most limiting design basis accident. Three of the four ventilation alignments tested had reported values of in-leakage greater than zero CFM. Plant staff implemented compensatory measures by placing the control room ventilation system into its pressurization accident alignment at 1828 PDT using the alignment from the test which had a reported value of zero CFM in-leakage. Additionally, administrative controls are being established to maintain post-Loss of Coolant Accident Emergency Core Cooling System leakage at a rate that would ensure operator doses are maintained less than the FSAR accident analysis results for the highest in-leakage rate reported by the test. Plant personnel notified the NRC Resident Inspector.

  • * * UPDATE FROM MICHAEL KENNEDY TO JOHN KNOKE AT 1816 EDT ON 09/16/2011 * * *

On 9/13/11 procedure revisions were approved with reduced limits for post-Loss of Coolant Accident Emergency Core Cooling System (ECCS) leakage. These reduced limits ensure operator doses are maintained less than the FSAR accident analysis results for the highest in-leakage rate reported by the CRE in-leakage test. Plant staff have since determined that the potential benefit of operating the control room ventilation system in its pressurization alignment was unnecessary with the ECCS leakage restriction and on 9/16/11 operators restored the control room ventilation system into its normal operating alignment. The licensee has notified the NRC Resident Inspector. Notified R4DO (Greg Pick)

  • * * UPDATE FROM SHANE GUESS TO DONALD NORWOOD AT 0042 EDT ON 10/19/2011 * * *

This is an update to EN #47258 reported on 9/13/11 where it was reported that operators had declared the Control Room Envelope inoperable. (This report was subsequently) updated on 9/16/2011. On 10/18/11 at 16:45 PDT, plant staff determined that the CRE testing dated February 3, 2005 was not performed using a bounding configuration which would result in greatest consequence to the control room operators. The recorded in-leakage from the test was therefore considered to be non-bounding. (As a result of this determination, plant staff have) implemented additional compensatory measures by issuing a shift order requiring the use of self-contained breathing apparatus and potassium iodide tablets under certain accident conditions in accordance with Regulatory Guide 1.196 and NEI 99-03. Plant personnel notified the NRC Resident Inspector. Notified R4DO (Campbell).

Emergency Core Cooling System
Control Room Envelope
ENS 474143 November 2011 22:50:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionUnanalyzed Condition - Control Room Ventilation Single Point VulnerabilityOn November 3, 2011, at 1550 PDT, operators determined that control room ventilation system (CRVS) contained a single failure vulnerability whereby unfiltered air supplied to the control room could exceed the flowrates used in the licensing basis analyses of design basis accident (DBA) consequences. This vulnerability was discovered during performance of control room inleakage testing required by TS SR 3.7.10.5. It was determined that the control room pressurization system airflow could bypass the supply filter if the CRVS booster fan in the associated train was not operating. This would allow as much as 800 cubic feet per minute of unfiltered air to be delivered to the control room following an accident that results in initiation of the CRVS pressurization mode. Operators would correct the condition approximately 10 minutes after a safety injection by manually selecting the train's redundant booster fan in accordance with existing proceduralized actions specified in the DCPP emergency procedure E-0 Appendix E. This period of unfiltered air supply to the control room due to a single failure of a CRVS booster fan had not been previously analyzed and could have potentially resulted in operator dose greater than contained in plant analyses. Plant staff verified that all components and redundant components in each ventilation train are currently OPERABLE. Plant staff has implemented additional compensatory measures by issuing a shift order to require that TS Action 3.7.10.A be entered for unavailability of either of the two CRVS booster fans in each CRVS train. Additionally, evaluation of the new unfiltered inleakage may result in more restrictive administrative controls to ensure operator doses are maintained less than the FSAR accident analyses. The licensee informed the NRC Resident Inspector.
ENS 4756431 December 2011 10:00:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionFire Barrier Rating of Vital Swtichgear Walls May Not Meet Standards

On December 31, 2011 at 0200 PST, a plant employee indentified the fire barrier material in each unit was potentially not qualified as a 3 hour rated fire barrier as specified by the Diablo Canyon power plant fire protection program. The fire barrier material in question is installed between the block wall portion of the barrier and the door frames in the walls separating three of the 480 Volt switchgear buses and separating the three vital instrument AC inverters. The condition was discovered by a plant employee who questioned the configuration while performing a routine tour of that area. Operators confirmed existing fire watches were in place and established additional fire watches as compensatory measures as required by the Diablo Canyon fire protection program. A review of the Appendix R fire protection analysis is in progress to confirm the rating of the installed configuration. The licensee has notified the NRC Resident Inspector.

  • * * RETRACTION FROM CRAIG HARVEY TO DONALD NORWOOD At 1955 EST on 1/4/2012 * * *

This is an update to EN 47564 reported on 12/31/11 where it was reported that plant personnel had identified rated fire barriers were not qualified as a three hour rated barrier as required by the DCPP Fire Protection Program. On 1/3/12 plant personnel provided barrier design drawings to the manufacturer of the DCPP fireproofing material. The manufacturer reviewed the design detail and confirmed that the barrier design depicted on the drawing is qualified as a 3 hour barrier. Therefore no unanalyzed condition that significantly degraded plant safety existed. This event is being retracted. The licensee notified the NRC Resident Inspector. Notified R4DO (Vasquez).

ENS 4824629 August 2012 00:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Mitigating Actions Implemented for Inoperable Control Room Envelope

On August 28, 2012, 17:00 PDT, Pacific Gas and Electric Company (PG&E) identified additional release pathways that could affect the control room (CR) operator dose following a Large-Break Loss-of-Coolant Accident (LBLOCA). Consequently, PG&E declared the control room envelope (CRE) inoperable and is establishing mitigative actions in accordance with TS 3.7.10, Action B.1, 'Initiate action to implement mitigating actions' immediately, and Action B.2, 'Verify mitigating actions ensure CRE occupant exposures to radiological hazards will not exceed limits, and CRE occupants are protected from smoke and chemical hazards' within 24 hours. PG&E is establishing mitigative actions in accordance with TS 3.7.10 and RG 1.196. These mitigative actions are for operations control room personnel to administer potassium iodide and don self-contained breathing apparatus equipment in a timely fashion should a LBLOCA occur. They will be communicated and controlled by a standing order to the control room staff. PG&E previously established controls on other release pathways that offset the potential increases to the maximum predicted offsite dose due to the new release pathways. No increase in maximum predicted offsite dose is expected from the new release pathways. Diablo Canyon (DCPP) is making this 8-hour, non-emergency notification under 10 CFR 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(D). Plant personnel notified the NRC Resident Inspector.

* * * UPDATE AT 1600 EDT ON 9/8/12 FROM GLEN GOELZER TO PETE SNYDER * * * 

PG&E is retracting EN 48246, based on the results from a new dose analysis coupled with compensatory measures implemented to ensure that the analysis input parameters and assumption will not be inadvertently exceeded. The analysis concluded that the CRE was operable and that CR doses remained below regulatory limits. Plant personnel notified the NRC resident inspector. Notified R4DO (Gaddy).

Control Room Envelope
ENS 483954 October 2012 01:15:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionUnanalyzed Fire Protection Deficiencies

On 10/9/12, at 16:30 PDT control room operators were questioned whether recently identified fire protection program deficiencies should have been reported to the NRC. On October 3 and October 8, 2012, DCPP (Diablo Canyon Power Plant) staff reviewing NFPA 805 Nuclear Safety Capability Assessment (NSCA) Variance From Deterministic Requirements (VFDRs) identified fire areas that neither conformed to Appendix R requirements nor had established, proceduralized and practiced compensatory measures in place. The issues were identified in the DCPP corrective action program and compensatory measures were established in accordance with the DCPP fire protection program requirements. Event: 10/3/12 Fire areas containing cables associated with startup transformers 1-2 and 2-2 could result in loss of startup power and also prevent the emergency diesels from performing their Appendix R safe shutdown function. Event: 10/8/12 Fire areas containing reactor coolant pump (RCP) breakers could result in loss of RCP seal cooling and prevent the credited local manual trip of the RCPs, contrary to the specified method of performing the Appendix R safe shutdown function. Event: 10/8/12 Fire areas containing cables for the ventilation systems of the 480V switchgear, DC panels, and battery chargers could require unproceduralized use of portable fans to maintain adequate cooling of the electrical equipment necessary to perform the Appendix R safe shutdown function. Operators established fire watches as compensatory measures as required by the DCPP fire protection program requirements. The above late notification of discovery of the unanalyzed conditions has been entered into the DCPP corrective action program. NRC Resident Inspector has been notified.

          • UPDATE AT 0028 EDT ON 11/01/12 FROM GLENN GOELZER TO S. SANDIN*****

This is an update to EN #48395 reported on October 10, 2012, at 0032 EDT. During the NRC's Fire Protection Triennial Inspection the NRC identified that several Alternate Compensatory Measures (ACMs) were not in the current post-fire procedure CP M-10. The ACMs address potential Appendix R non-conformance issues identified via the initiative to convert the DCPP fire protection program to NFPA 805. PG&E has established compensatory measures for all the identified areas in accordance with the DCPP fire protection program requirements. (The) NRC Resident Inspector has been notified. Notified R4DO (Deese).

  • * * UPDATE FROM D. BAHNER TO V. KLCO ON 11/30/12 AT 1618 EST * * *

This is an update to EN #48395 reported on October 9, 2012, at 2132 PST. During the ongoing evaluation of the issues previously identified in this event notification, PG&E (Pacific Gas & Electric) has concluded that a fire in the fire areas containing cables associated with startup transformers 1-2 and 2-2 would not result in loss of startup power or prevent the emergency diesels from performing their Appendix R safe shutdown function. This issue was reported as an unanalyzed condition. However, it is analyzed and controlled in plant procedure CP M-10, 'Fire Protection of Safe Shutdown Equipment.' PG&E retracts the initial event documented on October 3, 2012, thus making the date on which the first unanalyzed condition was discovered October 8, 2012. Therefore, PG&E will submit the 60-day Licensee Event Report by December 7, 2012. The NRC Resident Inspector has been notified. Notified the R4DO(Whitten).

  • * * UPDATE AT 1944 EST ON 1/30/13 FROM KLINE TO TEAL* * *

This is an update to EN #48395 reported on October 9, 2012, at 2132 PDT. On October 31, 2012, at 2128 PDT, PG&E provided an update to this event notification identifying that several alternate compensatory measures (ACMs) were not in plant procedure, CP M-10, 'Fire Protection of Safe Shutdown Equipment.' PG&E has evaluated this further and concluded that ACMs had been adequately implemented in CP M-10, and therefore retracts the EN update of (November 1, 2012 at 0028 EDT). NRC resident inspector has been notified. Notified R4DO (Walker).

ENS 487266 February 2013 23:24:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionUnanalyzed Condition for Control Room Ventilation

On February 06, 2012, at 1524 PST, engineers reviewing dose analyses for non-LOCA, non-fuel handling accident analyses identified deficiencies in the analyses. The analyses of concern include a locked reactor coolant pump rotor, a control rod ejection accident, main steam line break, and steam generator tube rupture. These deficiencies brought into question whether the 30 day control room operator dose received following one of these accidents would meet the station licensing basis limits of up to 5 rem whole body or its equivalent. In response to this concern, plant operators placed the control room ventilation system in its safeguards alignment, thereby ensuring the events would continue to be bounded by the analysis of the large break loss of coolant accident. The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM DAVID BAHNER TO CHARLES TEAL ON 02/28/13 AT 1815 EST * * *

Pacific Gas and Electric Company (PG&E) is correcting the event date in the above Description to February 06, 2013, and is retracting EN 48726 based on the results from reanalysis of each affected non-loss-of-coolant accident (LOCA) event (i.e., steam generator tube rupture, main steam line break, control rod ejection, and reactor coolant pump locked rotor) for potential impact on control room operator dose. The new dose assessment determined that control room dose consequences from a large-break LOCA bound the non-LOCA events as assumed in the original analyses. Accordingly, PG&E concludes the Diablo Canyon Power Plant control room ventilation system remains capable of maintaining control room dose limits within General Design Criteria-19. Plant personnel notified the NRC resident inspector. Notified R4DO (Allen).

Steam Generator
Main Steam Line
Control Rod
ENS 4914724 June 2013 23:15:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionEmergency Diesel Generators Unavailable for Auto-StartAt 16:15 PDT on 6/24/13, an operator performing a post-event annunciator alarm review of the event reported in EN #49143 identified that the operators the previous night had momentarily disabled all three Unit 1 emergency diesel generators, prior to restoring them to their automatic standby control alignment. Between 22:01:10 PDT and 22:02:54 PDT, on 6/23/13, less than the required minimum two diesel generators were available to automatically respond to a design basis accident. Due to the event reported in EN #49143, the start-up 230 kV power source was also unavailable at this time. At the time of this event the operators were in the procedurally guided process of placing the running diesel generator controls to manual, shutting down the running diesel generators, and returning them to the automatic standby control alignment. In this event the operators placed all the diesel generators in manual and shut them down before returning them to automatic control. During this time the operators would have responded to a plant event by returning the affected diesels to auto, whereupon the normal starting and loading sequence would have resumed in accordance with existing accident analyses. At the time of discovery all offsite and onsite power sources were operable. The licensee notified the NRC Resident Inspector.Emergency Diesel Generator
ENS 4914826 June 2013 04:58:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Plant Shutdown Required Due to Rhr System Socket Weld Leak

At 2158 PDT, plant personnel identified a through-wall leak in a Diablo Canyon Power Plant Unit 1 socket weld inside containment that provides a flow path to a relief valve that protects a common portion of both trains of the Residual heat Removal (RHR) system. The as-found condition did not comply with the requirements of equipment control guideline 7.6 and the ASME acceptance criteria. PG&E accordingly declared both Unit 1 trains of RHR inoperable and initiated plant shutdown at 2237 PDT in accordance with requirements of Technical Specification 3.0.3. PG&E will complete shutdown to Mode 4 and will perform repairs to restore compliance with ASME code requirements. The licensee notified the NRC Resident Inspector.

* * * UPDATE AT 1303 EDT ON 6/26/13 FROM WESLEY FIANT TO PETE SNYDER * * * 

Pacific Gas and Electric Company is submitting an update based on a press release issued at 0915 PDT detailing the above information to local television, newspaper, and radio media outlets. San Luis Obispo County and State of California Offices of Emergency Services have already been notified. The licensee notified the NRC Resident Inspector. Notified R4DO (Pick).

Residual Heat Removal
ENS 4963414 December 2013 23:03:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionUnanalyzed Condition Affecting Unit 1 Emergency Diesel Generator

At 1503 PST on December 14, 2013, Pacific Gas and Electric Company identified that, if atmospheric conditions were to develop that had both sustained high winds exceeding 60 miles per hour from the NW to NNE direction, and ambient air temperature exceeding 97 degrees Fahrenheit, the combination of these conditions could result in inadequate heat removal to support continuous operation of the Unit 1 emergency diesel generators. Upon identification of this condition, shift orders were issued requiring implementation of existing procedural guidance to open plant doors to allow additional air flow that would provide adequate emergency diesel generator cooling to support continuous operation of the U1 emergency diesel generators.

This report addresses a condition as described in 10 CFR 50.72(b)(3)(ii)(B).

The NRC Resident Inspector has been notified of this condition. This condition was discovered during a license basis verification review.

Emergency Diesel Generator
ENS 4966319 December 2013 15:52:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Two of Three Emergencey Diesel Generators Inoperable at the Same TimeOn 12/19/13 Unit 1 Emergency Diesel Generator (EDG) 1-2 was inoperable for scheduled maintenance. During an operational walk-down of the Unit 1 EDG 1-3, the associated fuel oil priming pump discharge fitting and pump housing were inadvertently damaged. Pacific Gas and Electric Company declared EDG 1-3 inoperable on 12/19/13 at 0752 PST. Since both Unit 1 EDGs were inoperable at the same time, this condition is reportable in accordance with 10 CFR 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(D). The NRC Senior Resident Inspector has been notified.Emergency Diesel Generator
ENS 498796 March 2014 17:06:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Unanalyzed Condition Regarding Potential Tornado Missile Damage to Emergency Diesel Exhaust Plenum

The condition described below is being reported as an unanalyzed condition per 10 CFR 50.72(b)(3)(ii)(B) and per the guidance of NUREG-1022, Rev. 3. On 03/06/2014 at 0906 PST, Diablo Canyon Power Plant (DCPP) identified a nonconforming condition involving the Emergency Diesel Generator (EDG) ventilation exhaust plenums installed in Unit 1 and Unit 2. Specifically, the radiator exhaust plenums and exhaust piping need to be re-evaluated to ensure adequate protection against flying debris that could be generated by a tornado. The occurrence of such an event is highly unlikely and there is no imminent concern regarding severe weather involving tornados. The EDGs are located inside the power plant structure and are capable of performing their safety function. Compensatory measures are being developed to address the associated nonconformance. This event does not adversely affect the health and safety of the public. The licensee informed the NRC Resident Inspector."

  • * * UPDATE PROVIDED BY RUSS CRUZEN TO JEFF ROTTON AT 2245 EDT ON 09/09/2014 * * *

This condition does not adversely affect the health and safety of the public. Based on an extent of condition review being performed for this event, the issue identified in the original event notification 49879 has also been determined to similarly affect the ventilation systems associated with the Unit 1 and 2 Vital 480 volt AC switchgear and battery/inverter equipment. The condition described in this update is being reported as an unanalyzed condition per 10 CFR 50.72(b)(3)(ii)(B) and as an event or condition that could have prevented the fulfillment of a safety function per 10 CFR 50.72(b)(3)(v)(A). Compensatory measures are being developed to address the associated condition. The licensee informed the NRC Resident Inspector. Notified R4DO (Azua)

Emergency Diesel Generator
ENS 503341 August 2014 00:29:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Unanalyzed Condition

On 07/31/2014 at 1729 PDT, Diablo Canyon Power Plant (DCPP) identified an unanalyzed condition involving the three class 1E 4160 volt buses on Unit 1 and on Unit 2. Following a postulated main steam line High Energy Line Break (HELB) in the Turbine Building, steam could enter the 4160 volt bus rooms through ventilation ducts that exhaust to the turbine deck where the steam lines are located. New analysis identified that the relative humidity (RH) of the 4160 volt bus rooms could reach 100%, which exceeds the design RH used in the analyses for the protective devices in the room. The high-humidity could possibly prevent the protective devices from operating as intended and could therefore result in the unavailability of the 4160 volt buses to supply power to engineered safety feature systems. This concern is being reported as an unanalyzed condition per 10 CFR 50.72(b)(3)(ii)(B) and as a condition that could have prevented fulfillment of a safety function per 10 CFR 50.72(b)(3)(v). Compensatory measures were taken to isolate the ventilation ducts between the 4160 volt bus rooms and the turbine deck, thereby preventing steam entry into the 4160 volt bus rooms, assuring the protective devices would not be subjected to conditions exceeding the design RH. With this compensatory measure all three 4160 buses on each unit are assured of performing their expected design function following the postulated main steam line break. This concern did not result in any adverse affect on the health and safety of the public. The licensee informed the NRC Resident Inspector. In addition to the 10 CFR sections listed in the header of this event notification, the licensee is also reporting this under 10 CFR 50.72(b)(3)(v)(D).

  • * * RETRACTION RECEIVED FROM BOB KLINE TO JOHN SHOEMAKER AT 1839 EDT ON 09/24/14 * * *

Diablo Canyon Power Plant is retracting this event notification based on the following: Subsequent to the identification of this event, PG&E conducted additional analysis and testing to support a past operability evaluation. Testing and analysis was completed successfully, demonstrating that the full population of associated components would perform their design safety function in 100% relative humidity conditions during a postulated high energy line break. Based on these analysis and testing results, PG&E concludes that the associated equipment remained operable, and did not represent an unanalyzed condition per 10 CFR 50.72(b)(3)(ii)(B) or a condition that could have prevented fulfillment of a safety function per 10 CFR 50.72(b)(3)(v). Therefore, PG&E retracts its notification of 7/31/2014. The licensee has notified the NRC Resident Inspector. Notified the R4DO (Drake).

Main Steam Line
ENS 5226021 September 2016 03:47:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionSteam Line Pipe Whip Restraint Coupling Sleeve Found Not Engaged

On 9/20/2016, a coupling sleeve on a pipe whip restraint located on the 119 foot elevation of the turbine building associated with Unit 2 main steam line 4 was found to be not engaged. As a result of the detached coupling, the restraint was not capable of performing its restraint function for a postulated pipe whip event on the main steam line. The coupling was reconnected on 9/20/2016, restoring its functionality. An extent of condition walkdown was subsequently performed for the other Unit 1 and Unit 2 steam line restraints and no similar issues were identified. This concern did not result in any adverse effect on the radiological health and safety of the public. The purpose of this whip restraint is to restrain the steam line for a postulated loss at the G-line anchor (east side of Turbine Building above the 104 foot elevation). The restraint protects the floor slab at the 104 foot elevation, which extends over the Unit 2 component cooling water heat exchangers. With the detached coupling, equipment in the area may have been vulnerable to damage if a pipe whip event occurred. Further analysis is needed to conclude whether the heat exchangers and other equipment would have remained protected in such an event and whether this would have significantly affected the designed plant response to a pipe event. Based on the need for further analysis, this event is being reported as an unanalyzed condition that may have significantly degraded plant safety in accordance with 10 CFR 50.72(b)(3)(ii)(B). The NRC Senior Resident Inspector was notified.

  • * * RETRACTION FROM FRANK LEE TO DONALD NORWOOD AT 1953 EST ON 11/18/2016 * * *

The purpose of this notification is to retract a previous report made on EN #52260, reported 9/23/2016. NRC notification was initially made as a result of a condition that required further analysis to determine whether the condition would have significantly degraded plant safety in accordance with 10 CFR 50.72(b)(3)(ii)(B). Further analysis of the condition concluded that PG&E Design Class I equipment located inside the Turbine Building would have remained undamaged and capable of performing their safety functions. The Turbine Building would not have experienced failure of major structural elements or adverse impact to the overall building stability. Therefore, the coupling sleeve on a pipe whip restraint located on the 119 foot elevation of the Turbine Building associated with Unit 2 main steam line 4 that was found to be not engaged did not constitute an unanalyzed condition that may have significantly degraded plant safety in accordance with 10 CFR 50.72(b)(3)(ii)(B). The NRC Resident Inspector has been notified. Notified R4DO (Azua)

Main Steam Line
ENS 5441730 November 2019 19:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Both Trains of Containment Spray Removed from ServiceOn November 30, 2019, at 1100 PST, with Unit 2 in Mode 4, Operations identified that both trains of containment spray had been removed from service earlier at approximately 0217 hours as part of preparations for a planned Mode 5 entry. The containment spray pumps are required to be operable (along with the containment fan cooler units) in Modes 1 through 4 in accordance with Technical Specification 3.6.6. With both containment spray pumps inoperable, TS 3.6.6 Action F requires the Unit to be shut down in accordance with TS 3.0.3. At 1125 hours, both trains of containment spray were returned to operable and the required actions of TS 3.6.6 and TS 3.0.3 were exited. The five containment fan cooler units remained operable for the duration of the occurrence. This notification is being made in accordance with the requirement of 10 CFR 50.72(b)(3)(v) as an event or condition that could have prevented fulfillment of a safety function, and 10 CFR 50.72(b)(3)(ii) as an event or condition that may have resulted in the plant being in an unanalyzed condition. The NRC Senior Resident Inspector has been notified.Containment Spray