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 Discovered dateReporting criterionTitleEvent description
ENS 4037131 October 2003 05:00:0010 CFR 50.73(a)(1), Submit an LERInvalid Group Iii Primary Containment Isolation System ActuationThis notification is being made in accordance with 10CFR50.73(a)(2)(iv)(A) to provide the NRC with information pertaining to the Primary Containment Isolation System (PCIS) Group III invalid actuation signals that affected containment isolation valves in more than one system on two separate occasions. On October 31, 2003 and November 9, 2003, with the reactor at full power, an invalid actuation of the 'B' Reactor Building Ventilation Monitor caused Group III isolations of PCIS. A spike that was caused by electronic noise within the detector invoked a spurious High Level Trip to this monitor (RM 17-452B), that resulted in a trip to PCIS logic Channel B1. The PCIS functioned successfully providing a complete Group III isolation. The train actuation was complete. Both trains of the Standby Gas Treatment System started as designed. The PCIS Group III isolation occurred which involves isolation of valves in the following systems: Drywell Air Purge and Vent, Drywell and Suppression Chamber Main Exhaust, Suppression Chamber Purge and Vent, Containment Air Compressor Suction Valve, Exhaust to Standby Gas Treatment, Containment Purge Supply and Makeup, Containment Air Sampling, Air dilution Subsystem Valves, Vent Subsystem Valves, and Containment Air Dilution Vent System MOV VG-22 A/B. It was determined that both of these Group III isolations were invalid, due to the Reactor Building Vent Monitor Radiation Level Trip occurring at 25 millirem/hr on 10/31/03 and 15 millirem/hr on 11/09/03. General area radiation levels in these areas at the time of the event were approximately 2.5 millirem/hr to 6 millirem/hr. The licensee will notify the NRC Resident Inspector.
ENS 4089526 May 2004 20:22:0010 CFR 50.73(a)(1), Submit an LER60 Day Invalid Automatic Actuation Report: Containment Isoaltion Valves in More than One SystemOn May 26, 2004 at 16:22 hours and inadvertent primary containment isolation signal was initiated following restoration from a surveillance test on the 2A Reactor Enclosure ventilation exhaust duct radiation monitor. The isolation was due to a fuse failure that caused isolation signals on Group 6A, 6B, 6C, and 7A primary containment isolation valves (PCIVs). The Unit 2 reactor enclosure ventilation isolated. The 2A standby gas treatment system (SGTS) and 2A reactor enclosure recirculation system (RERS) trains initiated. The instrument gas compressor suction valve and the 2A instrument gas header supply valve closed. The containment nitrogen inerting valve and the 2A instrument gas header supply valve closed. The containment nitrogen inerting block valve closed. The containment atmospheric sample valves received an isolation signal but were in a closed position prior to the event. All system functioned as designed during the event. The laboratory analysis of the fuse determined that the most probable cause of the event was an age related degradation of the fuse that reduced its current carrying capacity. The fuse was operating under steady state conditions for approximately 30 seconds prior to the failure. A fuse replacement plan was in progress prior to the event due to prior age related failures of this type of fuse. The fuse replacement plan will be evaluated to ensure the current schedule is adequate. Component data: Type: Fuse Manufacturer: Bussmann Model number: MIN-5 The NRC Resident Inspector was notified of this event by the licensee.
ENS 4089930 May 2004 14:40:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of Containment Isolation Valves Due to Partial Loss of 120 Vac Modular Power Unit 2 LoadsThis 60-day optional verbal report, as allowed by 10 CFR 50.73(a)(1), is being made to describe an unplanned, invalid actuation of specified systems, specifically the Primary Containment Isolation System. Since this event meets the definition of an invalid actuation, this notification is being made in accordance with 10CFR50.73(a)(2)(iv)(A) in lieu of a Licensee Event Report. On May 30, 2004, at approximately 10:40 am EDT, while the plant was operating at 100% power, a voltage regulator failed on Division 2 120 VAC Modular Power Unit No. 2 (MPU-2) which resulted in blown fuses and the loss of a number of loads from one of the three MPU-2 distribution cabinets. Since only one of the three distribution cabinets was lost, the isolations that occurred were only a portion of the isolations that would have occurred if all of the MPU-2 loads had been lost. This caused containment isolations by Division 2 Drywell Pneumatic supply valves (Primary Containment Isolation Group 18) and by Torus Water Management system outboard isolation valves (Primary Containment Isolation Group 12). Division 2 Secondary Containment Isolation Logic was also actuated, and the reactor building ventilation isolated. The Division 2 Standby Gas Treatment System automatically started. All equipment controlled by the affected circuits was determined to have responded to the loss of MPU-2 Cabinet 2 power as expected. Operators implemented applicable response procedures. The MPU was returned to service, and isolation signals were reset. Reactor power was not affected by this event. The NRC Resident Inspector was notified of this event by the licensee.
ENS 4095715 August 2004 09:05:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Scram Following Partial Loss of Offsite Power

At 0405 on August 15, 2004, River Bend Station had a loss of 230Kv Line #353 (RSS #2, Port Hudson) feeding the plant's switchyard. This resulted in a generator trip and a reactor scram. Feedwater tripped on a Reactor vessel Level 8 signal. RCIC is operating to control reactor vessel level. SRVs were used to manually control pressure. Mechanical vacuum pump (ARC A) would not start to control condenser vacuum. The MSIVs were manually isolated in anticipation of a Group 6 isolation (low vacuum). There was no ECCS initiation. Power was restored to the mechanical vacuum pump ARC B. Vacuum was restored and main steam lanes are in use for pressure control. We are still investigating the root cause. The following ESF actuations occurred: - Division II Diesel Generator - Standby Gas Treatment System - Annulus Mixing System - Control Building Ventilation System. The licensee will inform the NRC Resident Inspector.

  • * * UPDATE ON 8/15/04 AT 1340 EDT FROM JAMES BOYLE TO GERRY WAIG * * *

River Bend Station is currently in Mode 3, Hot Shutdown. During the event, offsite power was maintained through Reserve Station Service Line #1 to Division 1 safety related equipment and 'A' balance of plant (BOP) non-safety related equipment. The 230 KV line from the plant's switchyard (RSS Line #2) that was lost during the event has been recovered and the Division 2 bus has been restored to its normal power supply. The Division 2 diesel generator has been secured from operation (and has been placed in standby) During, the event, main condenser vacuum was restored from the main control room by starting the 'B' mechanical vacuum pump. Feedwater Pump 'A' remained available during the event. The circulating water supply to the main condenser remained in operation throughout the event. RCIC (Reactor Core Isolation Cooling) remains in service for reactor vessel level control. The ESF (Emergency Safety Feature) systems have been secured and placed in standby. A root cause team has been assembled to address the cause of the initial failure of the 230 KV Line #353. The licensee has notified the NRC Resident Inspector Notified R4DO (Linda Smith) and NRR EO (Cynthia Carpenter)

ENS 4100431 July 2004 17:56:0010 CFR 50.73(a)(1), Submit an LERInvalid Pcis ActuationThis notification is being made in accordance with 10CFR50.73(a)(2)(iv)(A) to provide the NRC with information pertaining to the invalid Primary Containment Isolation System (PCIS) Group III actuation signal that affected containment isolation valves in more than one system. On July 31, 2004 at 1356 (EDT) with the reactor at full power, the power supply that provides power to the Reactor Protection System (RPS) Channel 'A' of the Reactor Building Ventilation Exhaust Rad Monitor and RPS Channel 'A' of the Refuel Floor Rad Monitor was momentarily lost causing an invalid PCIS Group III actuation. Operators immediately verified the plant response to the loss of RPS 'A', backed up the Group III actuation manually, walked down the control room panels, shifted RPS 'A' bus to the alternate power supply, secured 'A' RPS MG set and restored the affected plant equipment to a normal line-up. The following systems were observed to have performed as follows: The PCIS functioned successfully providing a complete Group III isolation. Both trains of the Standby Gas Treatment System started and operated as designed. The PCIS Group Ill isolation involved isolation of valves in the following systems: Drywell Air Purge and Vent, Drywell and Suppression Chamber Main Exhaust, Suppression Chamber Purge and Vent, Containment Air Compressor Suction Valve, Exhaust to Standby Gas Treatment, Containment Purge Supply and Makeup, Containment Air Sampling, Air Dilution Subsystem Valves, Vent Subsystem Valves, and Containment Air Dilution Vent System MOV VG-22 A/B. Repairs were subsequently made to the 'A' RPS power supply and the system was returned to normal status. This event has been entered into Entergy Nuclear Vermont Yankee's Corrective Action Program. The licensee will notify the NRC Resident Inspector.
ENS 4118025 September 2004 23:14:0010 CFR 50.73(a)(1), Submit an LERInvalid Primary Containment Isolation System Actuation from Loss-Of-Power to Reactor Protection System (Rps) Bus 3B

This 60-day telephone notification is being made under reporting requirements specified by 10 CFR 50.73 (a)(2)(iv)(A) to describe an invalid actuation of general containment isolation signals affecting more than one system.

On September 25, 2004, with Unit 3 operating at 100% thermal power, at 1814 hours CDT, a voltage regulator problem occurred on RPS motor-generator (MG) set 3B. The associated RPS circuit protectors sensed an undervoltage condition and opened, thereby de-energizing RPS bus 3B. Primary Containment Isolation System (PCIS) logic circuits powered from this bus lost power, and PCIS logic Groups 2, 3, 6, and 8 were actuated. 

The following actuations/isolations occurred: Group 2: Isolation of the Pressure Suppression Chamber head tank pumps, Drywell Floor and Equipment Drains Isolation. Group 3: Isolation of the reactor water clean-up system. Group 6: Initiation of the Standby Gas Treatment System, Initiation of Control Room Emergency Ventilation, Isolation of the reactor zone and refuel zone normal ventilation systems. Group 8: This logic isolates the Traversing Incore Probes (TIP) if they are inserted. The TIPs were not inserted at the time of this event. All equipment responded in accordance with the plant design, with the exception that Unit 2 refuel zone ventilation system supply inboard isolation damper 2-DMP-064-0006 failed to close. The series damper, 2-DMP-064-0005, fully closed, therefore there would have been no impact to secondary containment integrity had this been an actual event. The damper's failure to close resulted from a sticking solenoid valve which was subsequently replaced. There were no safety consequences or impacts on the health and safety of the public. The event was entered into TVA's corrective action program for resolution.

The NRC senior resident inspector has been notified.
ENS 4118128 September 2004 18:02:0010 CFR 50.73(a)(1), Submit an LERInvalid Primary Containment Isolation System Actuation from Loss-Of-Power to Reactor Protection System (Rps) Bus 2AThis 60-day telephone notification is being made under reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) to describe an invalid actuation of general containment isolation signals affecting more than one system. On September 28, 2004, with Unit 2 operating at 100% thermal power, at 1302 hours CDT during maintenance work associated with protective relaying on 480 VAC Shutdown Board 2A, the board was inadvertently tripped. Associated RPS motor-generator (MG) set 2A lost power, and RPS bus 2A, which is powered from this MG set, was de-energized. Primary Containment Isolation System (PCIS) logic circuits powered from this bus lost power, and PCIS logic Groups 2, 3, 6, and 8 were actuated. The following actuations/isolations occurred: Group 2: Isolation of the Pressure Suppression Chamber head tank pumps (and) Drywell Floor and Equipment Drains Group 3: Isolation of the reactor water cleanup system. Group 6: Initiation of the Standby Gas Treatment System (and) Initiation of Control Room Emergency Ventilation (and) Isolation of the reactor zone and refuel zone normal ventilation system. Group 8: This logic isolates the Traversing Incore Probes (TIP) if they are inserted. The TIPs were not inserted at the time of this event. All equipment responded in accordance with the plant design. There were no safety consequences or impacts on the health and safety of the public. The event was entered into TVA's corrective action program for resolution. The NRC senior resident inspector has been notified.
ENS 4144125 February 2005 03:11:0010 CFR 50.72(b)(3)(iv)(A), System ActuationEsf Actuation Following Trip of Reactor Protection Motor-Generator SetA trip of the "A" RPS M-G set resulted in an "A" Group 2 isolation and startup of the standby gas treatment system. There was a preliminary report of a possible fire/smoke smell in the vicinity of the M-G set. However, when an operator reported to the location there was no observed fire. The fire brigade was also dispatched but found no fire or smoke in the M-G set area. The licensee is preparing to place the RPS on its alternate power supply. This will allow the Group 2 isolations and standby gas treatment system actions to be reset. The cause of the M-G set trip is still under investigation. The licensee will be notifying the NRC Resident Inspector as well as state and local authorities.
ENS 4150017 March 2005 22:55:00Other Unspec ReqmntOther Unspecified Requirement - License Condition 2.FThe following information was obtained from the licensee via facsimile (licensee text in quotes): This notification is being made in accordance with License Condition 2.F for Nine Mile Point Unit 2 which states in part 'report any violations of the requirements contained in Section 2.C of this license in the following manner: initial notification shall be made within 24 hours to the NRC Operations Center via the Emergency Notification System, with written follow-up within 30 days in accordance with the procedures described in 10 CFR 50.73(b), (c), and (e).' License condition 2.C (2) states in part 'Nine Mile Point Nuclear Station, LLC shall operate the facility in accordance with the Technical Specifications.' Earlier this year Operations was notified by Engineering that a portion of the procedural guidance contained in the Operating Procedure for Standby Gas Treatment System (SGTS) would render an operating SGTS sub-system inoperable during certain evolutions (e.g. Primary Containment Purge). Specifically when the filter train's recirculation valves are taken out of the automatic mode of operation, the subsystem's ability to drawdown the Secondary Containment within the required time and maintain less than 1/4" W.C. vacuum cannot be assured. In accordance with the guidance provided in NUREG-1022, an extensive review of the operation of the SGTS system over the past 3 years was performed. This review identified two (2) instances where, if a SGTS subsystem(s) had been declared inoperable as required, one or more Technical Specifications would have been violated. For example: on 3/15/2002 one SGTS subsystem was being utilized for Primary Containment Purge evolutions (and as such inoperable) and the opposite Division's EDG was simultaneously inoperable for pre-planned maintenance for greater than 4 hours. Technical Specification 3.8.1 Condition B.2 requires declaring required feature(s), supported by the inoperable DG, inoperable when the redundant required feature(s) are inoperable (i.e. the non-running SGTS subsystem). This was not recognized and the requirement to initiate a plant shutdown per LCO 3.0.3 was not performed. The second instance occurred in November of 2002 and was similar to the first occurrence. Following the identification of these occurrences Engineering performed an analysis of actual plant data to confirm inoperability of SGTS. The example noted above and the others identified will be explained in detail in the follow-up LER that will be submitted as required by 10CFR 50.73(a)(2)(i)(B) - 'Any operation or condition which was prohibited by the plant's Technical Specifications.' The licensee has notified the NRC Resident Inspector.
ENS 4221515 November 2005 14:05:0010 CFR 50.73(a)(1), Submit an LERInvalid Primary Containment Isolation System (Pcis) Actuation

This 60-day telephone notification is being made under reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) to describe an invalid actuation of general containment isolation signals affecting more than one system. On November 15, 2005, while operating at 100% thermal power, at 08:05 hours CST, Browns Ferry Unit 2 incurred an inadvertent, invalid actuation of the PCIS Group 6 logic. One reactor zone ventilation exhaust radiation monitor (the B channel) was indicating downscale due to a pre-existing maintenance issue, and, during activities to formally place the channel in a tripped status in accordance with the applicable Technical Specifications, the PCIS logic fuse for the opposite (A channel) radiation monitor was inadvertently removed rather than the fuse for the B channel. The PCIS logic responded as designed to the condition of both radiation monitors being downscale, and a Group 6 logic actuation resulted. The actuation was invalid because it resulted from an error related to an equipment tagging activity; there were no actual plant conditions which required the associated equipment actuations/isolations to occur. The following equipment actuations/isolations occurred: Unit 2 Group 6

  • Initiation of the Standby Gas Treatment System
  • Initiation of Control Room Emergency Ventilation
  • Isolation of the following equipment:
  * reactor zone and refuel zone normal ventilation systems
  * drywell-torus differential pressure compressor
  * drywell-torus Hydrogen/Oxygen analyzers
  * drywell radiation continuous air particulate monitor

All equipment responded in accordance with the plant design. There were no safety consequences or impacts on the health and safety of the public. The event was entered into TVA's corrective action program for resolution. The NRC senior resident inspector has been notified.

ENS 422353 November 2005 00:01:0010 CFR 50.73(a)(1), Submit an LERInadvertent Containment Isolation Signal Affecting Containment Isolation ValvesThis report is being made in accordance with 10CFR50.73(a)(2)(iv)(A) to provide the NRC with information pertaining to an invalid Primary Containment Isolation System (PCIS) Group 3 actuation signal that affected containment isolation valves in more than one system. On 11/02/05 with the reactor shutdown for a refueling outage, an invalid PCIS Group 3 actuation occurred while cycling a breaker during a tagging clearance activity. The invalid actuation occurred when the circuit was de-energized. This is an expected result of opening the breaker. The PCIS functioned successfully providing a complete Group 3 isolation. The train actuation was complete. Both trains of the Standby Gas Treatment System started as designed. The PCIS Group 3 isolation involves valves in the following systems: Drywell Air Purge and Vent Drywell and Suppression Chamber Main Exhaust Suppression Chamber Purge and Vent Containment Air Compressor Suction Valve Exhaust to Standby Gas Treatment Containment Purge Supply and Makeup Containment Air Sampling Air Dilution Subsystem Valves Vent Subsystem Valves Containment Air Dilution Vent System The licensee will notify the NRC Resident Inspector.
ENS 4242810 February 2006 16:20:0010 CFR 50.73(a)(1), Submit an LERInvalid Specified System ActuationsThe following information is provided as a 60 day telephone notification to NRC under 10 CFR 50.73(a)(1) in lieu of submitting a written LER to report a condition that resulted in an invalid actuation of a 10 CFR 50.73(a)(2)(iv)(B) system. NUREG1022 Revision 2 identifies the information that needs to be reported as discussed below. (a) The specific train(s) and system(s) that were actuated: On February 10, 2006, at 1120 EST, a surveillance was in progress to calibrate the Division 2 Fuel Pool Ventilation Exhaust Radiation Monitor D11-K611D. During jumper removal an adjacent terminal was contacted by the jumper while still connected to a 24 VDC power source resulting in a blown power supply fuse. The loss of the power supply resulted in the following automatic actions: Primary Containment Isolation Valve Group 14; Drywell and Suppression Chamber Ventilation System; and Group 16, Nitrogen Inerting System received an isolation signal. All primary containment isolation valves in both groups were previously in their safety function position (closed). Secondary containment isolated resulting in a trip of the Reactor Building Heating and Ventilation System and Division 2 Standby Gas Treatment System automatically started. The Control Center Heating, Ventilating and Air Conditioning System automatically shifted into the Recirculation mode. The initiation signal was invalid because it did not result in response to an actual high radiation condition, nor did it trip as a result of any other requirement for initiation of the safety function, such as a downscale or inoperable trip, for example. (b) Whether each train actuation was complete or partial. The Division 2 Standby Gas Treatment System automatically started, secondary containment fully isolated, Reactor Building Heating and Ventilation System tripped, and the Control Center Heating, Ventilating and Air Conditioning System automatically shifted into the Recirculation mode. These were complete actuations. The primary containment isolation valves Group 14 and 16 remained in their safety function (closed) position. This was a complete actuation. (c) Whether or not the system started and functioned successfully. The above systems functioned successfully. The licensee will notify the NRC Resident Inspector.
ENS 4248911 March 2006 09:32:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of Containment Isolation ValvesOn 03/11/06 at approximately 0432 hours, with Susquehanna Unit 1 in the Refueling Mode (0% power), the Unit experienced a partial isolation of Primary Containment isolation valves. The actuation occurred when a blown fuse disrupted power to a containment isolation logic relay. The inboard isolation valve to the 'B' Drywell Floor Drain Sump and the Containment Instrument Gas purge supply valve to the TIP indexer both closed. The 'A' Standby Gas Treatment system fan and the 'A' Reactor Building Recirculation fan successfully auto started during the event. This event constitutes an invalid system actuation and is reportable under 10CFR 50.73(a)(2)(iv)(A). The condition meets the criteria of 10CFR 50.73(a)(2)(iv)(B)(2) because a general containment isolation signal affected containment isolation valves in more than one system. This notification is being provided via a 60-day optional phone call as permitted under 10CFR 50.73(a)(1) in lieu of a written LER. As stated above, both valves affected by the invalid signal fulfilled their isolation function by successfully closing. At the time of the event, no other Primary Containment isolation valve was being maintained in a manner that required re-positioning. There were no challenges to the Reactor as a result of this event. The plant responded as expected. Following replacement of the subject fuse, the isolation logic was successfully reset and affected equipment was restored to the desired status. The licensee notified the NRC Resident Inspector.
ENS 4278719 August 2006 16:05:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Scram of Unit 3 Due to the Loss of Both Reactor Recirculation PumpsAt 1105 CST both Reactor Recirculation pumps tripped on Unit 3. In accordance with procedure 3-AOI-68-1, a manual scram was initiated. Reactor water level lowered to Reactor Pressure Vessel Level 3, resulting in the automatic actuation of the Primary Containment Isolation System as expected: Group 2 (RHR Shutdown Cooling), Group 3 (Reactor Water (Clean Up), Group 6 (Ventilation), and Group 8 (Traversing Incore Probe) along with the automatic start of Control Room Emergency Ventilation and all 3 trains of the Standby Gas Treatment System. Reactor water level was recovered to normal levels with the reactor feedwater system. During this time Unit 2 was at 100% power and was unaffected by the event. This event is reportable as a 4-hour and 8-hour notification along with a 60-day written report in accordance with 10 CFR 50.72(b)(2)(iv)(B), 10 CFR 50.72(b)(3)(iv)(A) and 10 CFR 50.73(a)(2)(iv)(A). All control rods fully inserted on the scram. Decay heat is being removed with normal feedwater and the turbine bypass valves. No relief valves lifted during this event. Electrical power to the plant is aligned for the normal shutdown lineup. The cause of this event is under investigation. The licensee notified the NRC Resident Inspector.
ENS 4283718 July 2006 09:47:0010 CFR 50.73(a)(1), Submit an LERInvalid Primary Containment Isolation System Actuation Due to Loss of Power to One Reactor Protection System BusThis 60-day telephone notification is being made under reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of general containment isolation signals affecting more than one system. On July 18, 2006, at 0447 hours CDT, with Unit 2 operating at 100% thermal power, the electrical power to reactor protection system (RPS) bus 2A was interrupted during the performance of surveillance testing on RPS circuit protectors 2A1 and 2A2. The RPS buses 2A and 2B are normally powered from motor-generator (MG) sets 2A and 2B, respectively. During testing or maintenance intervals affecting either the MG set or the normal supply circuit protectors, the affected RPS bus is powered from a transformer supply through alternate power circuit protectors 2C1 and 2C2. Power to RPS bus 2A, which was being powered through the alternate power circuit protectors via a temporary transformer, was interrupted when circuit protector 2C1 actuated on a sensed undervoltage condition. The Primary Containment Isolation System (PCIS) logic circuits powered from RPS bus 2A were de energized, and PCIS logic Groups 2, 3, 6, and 8 were actuated. None of the plant conditions which require PCIS Groups 2, 3, 6, or 8 actuation (e.g., low reactor water level, high drywell pressure, abnormal area radiation levels, high area temperature, etc.) existed, therefore these actuations are considered invalid. The following actuations/isolations occurred: Group 2: Isolation of the Pressure Suppression Chamber head tank pumps; and Drywell Floor and Equipment Drains Isolation Group 3: Isolation of the reactor water clean-up system Group 6: Initiation of the Standby Gas Treatment System; Initiation of Control Room Emergency Ventilation; and Isolation of the reactor zone and refuel zone normal ventilation systems. Group 8: This logic isolates the Traversing Incore Probes (TIP) if they are inserted. The TIPs were not inserted at the time of this event. All equipment responded in accordance with the plant design. Upon loss of power from the alternate source, the surveillance testing was suspended, and RPS Bus 2A was re energized from RPS MG set 2A. The affected logic was reset, and equipment was realigned as appropriate. There were no safety consequences or impacts on the health and safety of the public. The event was entered into TVA's corrective action program for evaluation and resolution. The NRC senior resident inspector has been notified of this report. Reference corrective action document PER 106999.
ENS 4287719 August 2006 00:58:0010 CFR 50.73(a)(1), Submit an LERInvalid Primary Containment Isolation System (Pcis) ActuationThis 60-day telephone notification is being made under reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of general containment isolation signals affecting more than one system. On August 18, 2006, at 1958 hours CDT, with Unit 2 operating at 100% thermal power, the electrical power to reactor protection system (RPS) bus 2B was interrupted during the performance of surveillance testing on RPS circuit protectors 2B1 and 2B2. The RPS buses 2A and 2B are normally powered from motor-generator (MG) sets 2A and 2B, respectively. During testing or maintenance intervals affecting either the MG set or the normal supply circuit protectors, the affected RPS bus is powered from a transformer supply through alternate power circuit protectors 2C1 and 2C2. Power to RPS bus 2B, which was being powered through the alternate power circuit protectors via a temporary transformer, was interrupted when circuit protector 2C1 actuated on a sensed under voltage condition. The Primary Containment Isolation System (PCIS) logic circuits powered from RPS bus 2B were de-energized, and PCIS logic Groups 2, 3, 6, and 8 were actuated. None of the plant conditions which require PCIS Groups 2, 3, 6, or 8 actuation (e.g., low reactor water level, high drywell pressure, abnormal area radiation levels, high area temperature, etc.) existed; therefore, these actuations are considered invalid. The following actuations/isolations occurred: Group 2: Isolation of the Pressure Suppression Chamber head tank pumps and Drywell Floor and Equipment Drains Isolation; Group 3: Isolation of the reactor water clean-up system; Group 6: Initiation of the Standby Gas Treatment System, Initiation of Control Room Emergency Ventilation, and Isolation of the reactor zone and refuel zone normal ventilation systems; Group 8: This logic isolates the Traversing In-core Probes (TIP) if they are inserted. The TIPs were not inserted at the time of this event. All equipment responded in accordance with the plant design. At the time of the loss of power from the alternate source, the surveillance testing had already been completed and activities were in progress to transfer the RPS bus back to its normal supply. These actions were completed and RPS Bus 2B was re-energized from RPS MG set 2B. The affected logic was reset, and equipment was realigned as appropriate. There were no safety consequences or impacts on the health and safety of the public. The event was entered into TVA's corrective action program for evaluation and resolution. The NRC Senior Resident Inspector has been notified of this report. Reference corrective action document PER 109090. Also see similar NRC event number 42837.
ENS 4309720 November 2006 02:28:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of Primary Containment Isolation System

This telephone report is being made in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event or condition caused by an invalid signal that resulted in an automatic actuation on November 19, 2006 at 2028 CST of the following Primary Containment Isolation System (PCIS) groups:

  • Group 2, Primary Containment isolations (partial) including Shutdown Cooling (SDC) valve isolation with no loss of SDC function.
  • Group 6, Secondary Containment isolation, and initiation of Standby Gas Treatment System and Control Room Emergency Filtration System (complete).

The systems above functioned as designed. Reactor Protection System (RPS) bus 'B' had lost power from its Motor Generator (MG) and was found de-energized which caused the actuations. Power was restored to the RPS bus 'B' from auxiliary power, and plant systems were recovered. In addition to the actuations reported above, the following actuations also occurred and functioned as designed.

  • RPS half-scram on B channel (no rods moved);
  • Half-group isolations of the following PCIS Groups;
         *  Group 1,  Main Steam Isolation Valves (valves were already shut), 
         *  Group 3,  Reactor Water Clean-up (one valve shut),
         *  Group 7,  Recirculation Loop Sample Lines (valves were already shut),

The cause of the invalid signal was 'B' RPS MG set high voltage condition produced by a faulty voltage adjust potentiometer in the voltage regulator. This caused a protective relay to trip the RPS MG exciter field which caused the subsequent low voltage and loss of the 'B' RPS bus. The licensee notified the NRC Resident Inspector.

ENS 4372915 September 2007 04:00:0010 CFR 50.73(a)(1), Submit an LERInvalid Primary Containment IsolationThis notification is being made in accordance with 10CFR50.73(a)(2)(iv)(A) to provide information pertaining to an invalid Primary Containment Isolation System (PCIS) Group 3 actuation signal that affected containment isolation valves in more than one system. On 09/15/07, with the reactor at 100% power, an invalid PCIS Group 3 actuation occurred from a momentary spike of the 'A' Refuel Floor radiation monitor which reached the instrument's high radiation trip setpoint. Radiation protection technicians dispatched to the refuel floor verified dose rates in the vicinity of the 'A' radiation monitors detector to be normal and below the alarm set points. The radiation monitor was verified to be indicating normally to expected radiation levels. Subsequent visual inspection and functional checks of the radiation monitor were completed satisfactory and the instrument channel was returned to service. The cause of the spurious spike is attributed to an unknown source of electrical noise. Both trains of the Standby Gas Treatment System started as designed and Reactor Building ventilation isolated. The train actuation was complete. The PCIS functioned successfully providing a complete Group 3 isolation. The PCIS Group 3 isolation involves the following systems and isolation valves: Drywell and Suppression Chamber air purge and vent: V16-19-6, 6A, 6B, 7, 7A, 7B, 8, 9, 10, 23 Containment Makeup: V16-20-20, 22A, 22B Containment Air Sampling: VG-23, 26, V109-76A, 76B Containment Air compressor suction: V72-38A, 38B Containment Air Dilution: VG-9A, 9B, 22A, 22B, NG-11A, 11B, 12A, 12B, 13A, 13B In accordance with 10CFR50.73(a)(i) a telephone notification is being made instead of submitting a written Licensee Event Report. The licensee will notify the NRC Resident Inspector.
ENS 4385022 October 2007 23:30:0010 CFR 50.73(a)(1), Submit an LERInvalid System ActuationThe following information is provided as a 60 day telephone notification under 10 CFR 5O.73(a)(l) in lieu of submitting a written LER to report a condition that resulted in an invalid actuation of a 10 CFR 50.73(a)(2)(iv)(B) system. NUREG 1022, Revision 2, identifies the information that is to be reported as discussed below. On October 22. 2007, at 1830 hours, Division 2 of Residual Heat Removal (RHR) was being placed in Shutdown Cooling (SDC) following completion of a SDC outage. The plant was in Mode 5, Refueling. Reactor Protection System (RPS) A was deenergized for maintenance. RPS B was being supplied by the alternate supply because the B RPS Motor Generator was removed from service for maintenance. Upon start of the RHR D pump motor the RPS B Alternate Supply Electrical Protection Assembly (EPA) breakers tripped due to sensed undervoltage. The loss of the power supply to RPS B resulted in the following: A reactor scram (all rods were already fully inserted), RHR SDC outboard valve isolation, trip of the Reactor Water Cleanup System (RWCU), outboard valve isolation of the Torus Water Management System (TWMS). A secondary containment isolation also occurred resulting in a trip of Reactor Building Heating Ventilation and Air Conditioning (HVAC), auto start of Division 2 of Standby Gas Treatment System (SGTS), and shift of the Control Center HVAC system to recirculation mode. All actuations and isolations were as expected for existing plant conditions. The initiation signal was invalid because it did not result in response to an actual plant parameter, nor did it trip as a result of any other requirement for initiation of a safety function. Due to the actuation of equipment in multiple systems that were not removed from service or otherwise prevented from changing states, this event is reportable under 50.73(a)(2)(iv) as an invalid actuation of one of the specified systems. The reactor scram actuation was complete because a half scram was already present due to RPS A being deenergized for maintenance. The Division 2 SGTS system automatically started, secondary containment fully isolated, Reactor Building HVAC system tripped, and the Control Center HVAC fully shifted into the recirculation mode. The following were partial isolations due to loss of RPS B, Division 2: RHR SDC isolation and TWMS isolation. All systems functioned properly in response to the RPS power loss based on refuel outage system configurations. The licensee believes that the cause of the undervoltage was a result of the start of the RHR pump which caused an in-rush current. The licensee is considering a design change, and captured this event in their corrective action program system as CARD 07-26537. The licensee will notify the NRC Resident Inspector.
ENS 442113 April 2008 11:25:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of a Sbgt During Annunciator TestMonticello Nuclear Generating Plant is making a telephone report in accordance with 10 CFR 50.73(a)(2)(iv)(A) Invalid Partial Actuation of the Standby Gas Treatment and Secondary Containment Isolation Systems due to an inappropriate operator action. This report is being made in lieu of a written Licensee Event Report. At 0825 on 04/03/2008, an operator was performing an annunciator test of the Control Room panels and inappropriately pushed the 'A' Standby Gas Treatment system 'Test' pushbutton instead of the 'Lamp Test' pushbutton. He then immediately pushed the 'Reset' pushbutton which reset the Standby Gas Treatment train. The inappropriate actuation of the 'A' Standby Gas Treatment System resulted in the 'A' train momentarily starting, causing ventilation fans V-EF-10 and V-MZ-6 to trip. The immediate resetting of the system by depressing the 'Reset' pushbutton prevented a full secondary containment isolation. All systems started and functioned successfully. The cause of the invalid signal was the operator actuating the system by depressing the 'Test' pushbutton instead of the 'Lamp Test' pushbutton. The NRC Resident Inspector was notified of this event report. After the invalid actuation was completed, all systems affected were reset and returned to normal lineup.
ENS 4489920 January 2009 16:10:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of Secondary ContainmentMonticello Nuclear Generating Plant is making a telephone Report in Accordance with 10 CFR 50.73(a)(2)(iv)(A) Invalid Actuation of the Standby Gas Treatment and Secondary Containment Isolation Systems due to high resistance resulting from inadequate contact wipe of a relay. This report is being made in lieu of a written Licensee Event Report. SPECIFIC TRAINS AND SYSTEMS THAT WERE ACTUATED The 'A' Standby Gas Treatment system actuated and Secondary Containment isolated. DESCRIPTION OF WHETHER EACH TRAIN ACTUATION WAS COMPLETE OR PARTIAL On January 20, 2009, during performance of Step 29 of Procedure 0003, Drywell High Pressure Scram and Groups 2, 3, & Secondary Containment Isolation Test and Calibration, the Standby Gas System automatically initiated and Secondary Containment isolated due to high contact resistance on a Drywell High Pressure HFA relay. This resulted in increased steam chase temperatures, entry into Action Statement TS 3.3.6.2.A for Secondary Containment Isolation Instrumentation, entry into Action Statement TS 3.6.4.1.A for Secondary Containment, entry into Action Statement TS 3.6.4.3.A for Standby Gas Treatment, and 10CFR50.73 reportability. DESCRIPTION OF WHETHER OR NOT THE SYSTEM STARTED AND FUNCTIONED SUCCESSFULLY All systems started and functioned successfully. The cause of the initiation of SBGT and isolation of Secondary Containment during performance of Step 29 of Procedure 0003 was the presence of high resistance at relay 16A-K60A, contacts 5-6. The cause of high resistance at relay 16A-K60A, contacts 5-6, was inadequate contact wipe. The cause of the inadequate contact wipe was inadequate contact wipe adjustment after replacement of HFA coils with the new Century series coil. The NRC Resident Inspector was notified of this event report.
ENS 4500924 March 2009 17:26:0010 CFR 50.73(a)(1), Submit an LERPrimary Containment Isolation System (Pcis) Group 3 Invalid ActuationThis sixty day notification is being made in accordance with 10 CFR 50.73(a)(2)(iv)(A) to provide the NRC with information pertaining to an unplanned invalid actuation of specific systems, specifically, a Primary Containment Isolation System (PCIS) Group 3 actuation signal that affected containment isolation valves in more than one system. On March 24, 2009, at approximately 1326 hours, Vermont Yankee Nuclear Power Station (VYNPS) experienced an invalid PCIS Group 3 isolation associated with personnel error during quarterly calibration of the Refuel Floor Zone Radiation Monitors. VYNPS had removed the East Refuel Floor Zone Radiation Monitor from service for calibration. The technician, in the field, had completed a phone communication with the control room and was dispatched to the East Refuel Floor Zone Radiation Monitor to perform the calibration activity. However, the technician incorrectly went to the inservice West Refuel Floor Zone Radiation Monitor and removed the detector from service. This incorrect action caused a momentary invalid high radiation signal containment isolation signal and the Subsequent PCIS Group 3 isolation. The following actuations resulted: Both trains of the Standby Gas Treatment System started as designed. The PCIS functioned properly providing a complete Group 3 isolation valves in the following system actuated as a result of the PCIS Group 3 isolation: Drywell Air Purge and Vent, Drywell and Suppression Chamber Main Exhaust, Suppression Chamber Purge and Vent, Containment Air Compressor Suction, Exhaust to Standby Gas Treatment, Containment Purge Supply and Makeup, Containment Air Sampling, Air Dilution Subsystem, (and) Containment Air Dilution Vent System. This event has been entered into VYNPS's corrective action program. The licensee has notified the NRC Resident Inspector.
ENS 451199 June 2009 23:52:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentDoor for Secondary Containment Boundary Left Open

This notification is being made pursuant to NRC regulation 10 CFR 50.72(b)(3)(v)(D), any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. At 1852 (CDT) on June 9, 2009, River Bend Station personnel discovered that a normally closed auxiliary building door was open. This door serves as part of the secondary containment boundary. At discovery, immediate action was taken to close the door. This action restored the secondary containment to the design configuration. Investigation determined that the door was last accessed at 1242 on June 9 and was most probably left open at that time. Further action is being taken to investigate the cause of the event. Secondary containment leak tightness is required to ensure that the release of radioactive materials from the primary containment is restricted to those leakage paths and associated leakage rates assumed in the accident analysis, and that fission products entrapped within the secondary containment structures will be treated by the Standby Gas Treatment System prior to discharge to the environment. With the subject door being open, the function of secondary containment would be impacted. A second door is located in the same exterior passage way as the secondary containment door found open. This door was closed during the period of time the secondary containment door was open. This second door serves a security function. However, it potentially could serve to perform the secondary containment function. An evaluation is being performed to determine the actual impact of the condition on the secondary containment function. However, based on the identified condition, this report is being made as a condition that could have prevented fulfillment of a safety function. The licensee has notified the NRC Resident Inspector.

  • * * RETRACTION FROM D. WILLIAMSON TO D.PARK AT 1325 ON 6/29/09 * * *

(This event was reported by River Bend Station on 6/10/09 at 0102 (EDT). This update is being provided for the purpose of retracting that notification.) Subsequent investigation determined that the secondary containment door was left open for unknown reasons some time after 0800 on the morning of June 9. At the 1242 observation by the persons exiting the building, the door was open and it was left in that condition. However, a separate exterior door in that same passageway serves the security function, and it has been confirmed that, other than for routine access, the security door remained closed and locked during the time that the interior pressure boundary door was open. An engineering analysis has determined that the as-found condition did not defeat the function of secondary containment. While the security door is not air-tight, the maximum potential leakage past it under postulated accident conditions has been evaluated. An existing engineering calculation provides a means to determine the maximum size of a breach in the auxiliary building boundary such that the draw-down requirement prescribed by Technical Specifications is maintained. That calculation uses the additional flow area of an identified breach, in addition to the most recent test results of the standby gas treatment system (that system establishes and maintains a negative pressure in the building as part of the its design). Measurements taken on the door found that the potential flow area around it totaled 35 square inches. The current test results indicate that the standby gas treatment system can support the safety function of the auxiliary building with an analytical breach size of 230 square inches. As there is significant margin between the measured gap around the security door and the analytical value, this event was well bounded by the assumptions of the design basis of the building. As such, this event did not constitute a loss of the safety function of secondary containment. The licensee notified the NRC Resident Inspector. Notified the R4DO (D.Powers).

ENS 4531631 August 2009 15:14:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Boundary Door Inoperable

During normal entry / exit through secondary containment boundary door 1A401, it was discovered that the door would not latch closed due to interferences between the door and its frame. The door was unable to be latched closed for approximately 5 minutes which represented a possible path for uncontrolled release of radioactive material. No release of radioactive material occurred as a result of this event. The time during which the door would not latch was spent diligently troubleshooting to determine why the door would not secure. When discovered, the interference was immediately removed and the door was secured (latched). Door 1A401 is now operable as a secondary containment boundary but is currently deactivated and posted by security to prevent use as a conservative measure until further inspection and maintenance can be preformed on the door to prevent this issue from reoccurring. At this time secondary containment is operable with boundary door 1A401 closed and latched. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE FROM MICHAEL J. LARSON TO DONALD NORWOOD AT 1042 EDT ON 10/30/09 * * *

Retraction of Notification EN# 45316. The event was reported by Grand Gulf Nuclear Station on 08/31/2009 at 1014 CDT. This update is being provided for the purpose of retracting that notification. On August 31, 2009, during normal entry/exit through secondary containment boundary door 1A401, it was discovered that the door would not latch closed due to interferences between the door and its frame. The door was unable to be latched closed for approximately 5 minutes which represented a possible loss of safety function since it could have provided a path for uncontrolled release of radioactive material. No release of radioactive material occurred as a result of this event. As part of the event investigation, the malfunction (inability to close and latch) of door 1A401 was simulated under controlled conditions. Data was obtained under normal ventilation conditions and under the condition with one train of Standby Gas Treatment System (SGT) operating. Analysis of the data determined that the SGT system was able to drawdown the secondary containment enclosure building pressure to greater than 0.311 inch of vacuum water gauge (for no assumed failures) which is above the Technical Specification (TS) 3.6.4.1 surveillance minimum requirement of 0.266 inch of vacuum water gauge (following a postulated accident with assumed failures) using one SGT subsystem.

Therefore, this event did not constitute a loss of the safety function of secondary containment and this event is not reportable. The licensee notified the NRC Resident Inspector. Notified R4DO (Powers).

ENS 4583523 February 2010 14:50:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of Standby Gas Treatment SystemThis report is being made under 10CFR50.73(a)(2)(iv)(B)(2). On February 23, 2010 at 1050 EST procedure 52PM-C71-001-0, RPS M/G Set System Preventative Maintenance, was being performed. During restoration of RPS Buses on Unit 1, only the Unit 1 required logic was reset. The Unit 2 logic was also required to be reset but was not. Procedure 52PM-C71-001-0, RPS M/G Set System Preventive Maintenance, did not clearly require the reset of both Unit 1 and Unit 2 logic. The procedure has been revised to make this requirement clear. Continuation of steps in the procedure required links to be closed which resulted in SBGT starting on Unit 1 and Unit 2 from Unit 2 logic. Unit 1 and Unit 2 Reactor Building ventilation isolated. This was not due to a valid signal. The automatic actuation of the standby gas treatment system (SBGT) and the isolation of Unit 1 and 2 secondary containment isolation dampers is considered an invalid actuation since the parameters that cause this actuation to occur had not been exceeded. For this reason the actuation is considered invalid and a report to the NRC is not required by 10CFR50.72(b)(3)(iv); however, because the secondary containment isolation signals affected containment isolation valves in more than one system (Unit 1 and 2 components affected) the event is reportable as required by 10CFR50.73(a)(2)(iv)(B)(2). A licensee event report (LER) is required, but can be a telephone notification as allowed by 10CFR50.73. In the case of an invalid actuation reported under 10CFR50.73(a)(2)(iv), other than actuation of the reactor protection system (RPS) when the reactor is critical, the licensee may, at its option, provide a telephone notification to the NRC Operations Center within 60 days after discovery of the event instead of submitting a written LER. The four Standby Gas Treatment (SBGT) fans auto started and both Unit 1 and Unit 2 reactor building and refueling floor normal ventilation systems automatically shutdown and isolated. The SBGT Initiation and the ventilation system shutdown were both complete actuations. The licensee notified the NRC Resident Inspector.
ENS 4595726 May 2010 19:26:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Scram While Increasing PowerAt 1526 on 5/26/2010, while operators were increasing power with reactor recirculation flow, an RPS (Reactor Protection System) actuation occurred in both channels and all control rods inserted. RPV (Reactor Pressure Vessel) level decreased to 114.5 inches (Low level setpoint is less than 127 inches). Following the scram, the PCIS (Primary Containment Isolation System) groups 2, 3, 4 and 5 received actuation signals and all open valves isolated. Both trains of standby gas treatment system actuated. Plant actions taken included entering procedures OT-3100, Reactor Scram on RPS Actuation and EOP-1, RPV Control on Low Level Signal. The EOP-1 was exited per shift manager direction because of no emergency. The operators stabilized the plant and reset both RPS and PCIS. An investigation into the cause of the scram is continuing. Electrical power is being supplied from offsite sources through the startup transformers. The licensee notified the NRC Resident Inspector.
ENS 459753 June 2010 15:50:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Secondary Containment Briefly DegradedOn June 3rd, 2010, at 1050 CST, both doors in Airlock 413 from Secondary Containment (SCT) to the Rad Waste 985' Pump Room were opened simultaneously for approximately five seconds and subsequently re-closed. This condition caused an unplanned entry into Technical Specification 3.6.4.1.A for SCT. The condition could have prevented the Standby Gas Treatment system from developing a negative pressure within SCT following a design basis accident. This negative pressure is required to prevent ground level releases of radioactivity and minimize onsite and offsite dose consequences following an accident, The Standby Gas Treatment system remained operable throughout the event. The site continues to assess the situation. The licensee has notified the NRC Resident Inspector and will also notify State authorities.
ENS 4604627 April 2010 22:37:0010 CFR 50.73(a)(1), Submit an LERInvalid Group 6 Containment IsolationThis notification is being made in lieu of a written report under the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a Group 6 containment isolation signal affecting more than one system. On April 27, 2010, at 1737 hours Central Daylight Time, with Unit 3 operating at 100 percent thermal power, Unit 3 received a Group 6 ventilation system isolation signal during the performance of a maintenance activity on a Unit 3 Reactor/Refuel Zone Radiation Monitor, 3 RM-90-141/143. This resulted in isolation of the reactor and refuel zone ventilation systems, initiation of Standby Gas Treatment system (Trains A, B, and C) and the Control Room Emergency Ventilation system (Train A). All equipment responded to the Group 6 ventilation system isolation signal in accordance with the plant design. However, during the recovery effort, one of the Unit 3 Reactor Building Ventilation dampers failed to indicate fully closed. Operations personnel verified by inspection that the damper was fully closed. There were no safety consequences or impact on the health and safety of the public as a result of this event. The event was entered into the Corrective Action Program (CAP) as PER 227125. From PER 227125, trouble shooting determined a relay coil had been installed upside down when the coils were recently replaced. The NRC Senior Resident Inspector has been notified.
ENS 461555 August 2010 16:45:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Momentary Loss of Secondary Containment Due to Personnel Passing Through Open AirlocksOn August 5, 2010 at 1145 CDT, both doors in Airlock 413 from Secondary Containment (SCT) to the 985 ft Radwaste Pump Room were simultaneously open for a period of approximately five (5) seconds and subsequently reclosed. This condition caused an unplanned entry into Technical Specification 3.6.4.1.A for SCT. The condition could have prevented the Standby Gas Treatment system from developing a negative pressure with SCT following a design basis accident. This negative pressure is required to prevent ground level release of radioactivity and to minimize onsite and offsite dose consequences following an accident. The Standby Gas Treatment system remained operable throughout the event. The licensee will inform the State and has notified the NRC Resident Inspector.
ENS 4636731 August 2010 22:37:0010 CFR 50.73(a)(1), Submit an LERInvalid Primary Containment Isolation System Actuation Due to a Voltage TransientThis telephone report is being made in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event or condition caused by an invalid signal that resulted in an automatic Group 6 isolation. On August 31, 2010 at 1737 CDT, Group 6 of Primary Containment Isolation System (PCIS) actuated. This resulted in completion of Secondary Containment isolation, initiation of the Standby Gas Treatment System and Control Room Emergency Filtration System. An invalid signal occurred apparently as a result of a voltage transient on the Nebraska City 345kV line. This was from a 3-phase fault to ground due to a structural failure during a severe thunder storm with high winds. The equipment associated with the Group 6 isolation functioned successfully and the isolation was complete. The Group 6 PCIS was reset. Cooper Nuclear Station operators reviewed the parameters that would cause a Group 6 trip signal (i.e. reactor water level, drywell pressure, reactor building radiation) and determined there were no valid conditions that would have caused the isolation. This event was most likely due an act of nature, thus no corrective actions were required. The NRC Resident Inspector will be notified.
ENS 463944 November 2010 05:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Containment Air Lock Doors Not Operated ProperlyOn November 4, 2010, at 11:28 AM both doors in airlock 124 from secondary containment to access control were simultaneously open for a period <5 seconds. The doors were immediately closed. This condition resulted in an unplanned entry into Technical Specification 3.6.4.1.A for secondary containment. The condition could have prevented the Standby Gas Treatment System from developing a negative pressure within secondary containment following a design basis accident. This negative pressure is required to prevent ground consequences following an accident. The Standby Gas Treatment System remained operable throughout the event. The licensee was decreasing power at the time of the report for a condition unrelated to the report. The licensee will notify the Minnesota Duty Officer. The licensee notified the NRC Resident Inspector.
ENS 4649620 December 2010 09:57:0010 CFR 50.72(b)(3)(iv)(A), System ActuationFuel Pool/Reactor Building Exhaust Plenum Primary Power Supply FailedAt 0357 December 20, 2010 the 'A' division Fuel Pool/Reactor Building Exhaust Plenum Primary Power Supply failed, resulting in upscale readings on both the Fuel Pool and Reactor Building Ventilation Plenum radiation monitors. This condition resulted in closure of the Group II Primary Containment Isolation Valves (PCIV), isolation of Secondary Containment (SCT), initiation of the Standby Gas Treatment System (SBGT), and a transfer of the Control Room Ventilation (CRV) and Control Room Emergency Filtration (CREF) systems to the High Radiation Mode. Conditions and Required Actions were entered for Technical Specification 3.3.6.2 (SCT Instrumentation), 3.3.7.1 (CREF Instrumentation), and 3.4.5 (RCS Leakage Detection - CAM). Radiation levels were verified to be normal in the affected areas. Isolations signals were reset and Secondary Containment ventilation systems were restored to a normal lineup. Repairs are currently in progress to replace the high voltage power supply to the affected radiation monitors and are expected to complete within the required action time limits of the applicable technical specifications. The licensee is in a 24 hour LCO. The licensee has notified the NRC Resident Inspector.
ENS 4697221 April 2011 20:10:0010 CFR 50.73(a)(1), Submit an LERInvalid Primary Containment Isolation System Actuation Due to Conflicting Work Activities

This event is reportable under 10 CFR 50.73(a)(2)(iv)(A) as an automatic actuation of general containment isolation signals affecting containment isolation valves in more than one system. This 60-day telephone notification is being made in accordance with 10 CFR 50.73(a)(1) for invalid actuations reported under 10 CFR 50.73(a)(2)(iv)(A). This actuation was invalid since it was caused by maintenance activities and not by any actual plant condition warranting containment isolation. On April 21, 2011, at 1310 hours, upon de-energization of the Reactor Protection System (RPS) Bus A for maintenance, an unexpected actuation of the Groups 3 and 4 outboard containment isolation valves occurred. Outboard isolations occurred in the reactor building drain and ventilation systems, and reactor closed cooling systems. Control room emergency ventilation and standby gas treatment systems also started. All systems functioned as designed, excluding those components that were already removed from service. Following the event, the RPS Bus A was re-energized and the plant was restored to normal operating condition for the current configuration per plant procedures.

The subsequent investigation found that personnel involved with work planning and control did not recognize that de-energizing RPS Bus A would create a condition which completed the Nuclear Steam Supply Shutoff System outboard isolation logic. An associated relay for the second channel had been previously de-energized to support ongoing maintenance. The cause of allowing this conflicting work to occur was determined to be inadequate procedural guidance. Planned corrective actions will enhance procedures to identify logic impacts, conflicting equipment and recommended protection schemes. There were no actual safety consequences associated with this event since all affected equipment responded as designed. The NRC Resident Inspectors have been notified.

ENS 4697723 April 2011 15:14:0010 CFR 50.73(a)(1), Submit an LERInvalid Primary Containment Isolation System Actuation Due to Unrecognized Design ConflictThis event is reportable under 10 CFR 50.73(a)(2)(iv)(A) as an automatic actuation of general containment isolation signals affecting containment isolation valves in more than one system. This 60-day telephone notification is being made in accordance with 10 CFR 50.73(a)(1) for invalid actuations reported under 10 CFR 50.73(a)(2)(iv)(A). This actuation was invalid since it was caused by maintenance activities and not by any actual plant condition warranting containment isolation. On April 23, 2011, at 0814 hours, during implementation of a clearance order for ongoing work, Reactor Protection System (RPS) Bus A was transferred from the normal to alternate power supply. The power transfer functions as a break before make, and the momentary loss of power caused an unexpected actuation of the Groups 3 and 4 outboard containment isolation valves. Outboard isolations occurred in the reactor building drain and ventilation systems, and reactor closed cooling systems. Control room emergency ventilation and standby gas treatment systems also started. All systems functioned as designed, excluding those components that were already removed from service. Following the event, the RPS Bus A was re-energized and the plant was restored to normal operating condition for the current configuration per plant procedures. The unexpected actuation was due to a latent design conflict between a new design modification and existing equipment that was not discovered until during the implementation phase of the modification. The subsequent investigation cited inadequate review and engagement in the design process by station personnel of the vendor supplied design change modification package as the cause. As part of the implementation of the modification package an interposing relay was introduced into the Nuclear Steam Supply Shutoff System (NSSSS) logic circuit. The work for this modification was performed on the two days prior to this event, April 21st and 22nd. The new design was such that the source of power for the added relay was the same power supply which supplied the alternate logic channel. The resulting condition created a scenario where loss of the RPS-A power supply would complete both halves of the NSSSS outboard trip logic. The design has been revised such that loss of RPS-A or RPS-B power supply will not result in loss of both halves of the NSSSS trip logic circuit. Planned corrective actions will enhance procedures to ensure key design parameters and performance objectives are established early in the design process. There were no actual safety consequences associated with this event since all affected equipment responded as designed. The NRC Resident Inspectors have been notified.
ENS 4745019 September 2011 16:00:0010 CFR 50.73(a)(1), Submit an LERInvalid Group 6 Isolation Signal

This 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation signal affecting more than one system. On September 19, 2011, at 1000 hours Central Daylight Time (CDT), during the performance of a maintenance activity on the Reactor/Refueling Zone Ventilation Radiation Monitor BFN-3-RM-090-0141/143, Browns Ferry Unit 3 received a Primary Containment Isolation System (PCIS) Group 6 isolation. This resulted in isolation of the reactor and refuel zone ventilation systems, initiation of the Standby Gas Treatment System (Trains A, B and C), and the initiation of the Control Room Emergency Ventilation System (Trains A and B). All plant systems responded as designed.

There are two divisions of Reactor/Refueling Zone Ventilation Radiation Monitors: BFN-3-RM-090-0140/142 and BFN-3-RM-090-0141/143. A downscale or inoperable signal in both divisions will initiate the PCIS Group 6 isolation. Prior to the performance of the maintenance activity, BFN-3-RM-090-0140/142 was functional. However, during a field walkdown after the PCIS Group 6 isolation, relay BFN-3-RLY-064-16AK62A for BFN-3-RM-090-0140/142 was discovered to be chattering. A chattering relay could cause momentary loss of continuity between the contacts which would effectively generate a spurious isolation signal from that division. Thus, when 3-RM-090-0141/143 was made inoperable by the surveillance, the PCIS Group 6 logic was made-up. The PCIS Group 6 isolation was reset at 1008 CDT. This event was entered in the Corrective Action Program as Problem Evaluation Report (PER) 434799. There were no safety consequences or impact on the health and safety of the public as a result of these events. The NRC Senior Resident Inspector was notified.

ENS 477992 April 2012 19:52:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Initiation of Reactor Shutdown Required by Technical Specifications (Ts) 3.8.1.FOn April 2, 2012, at 1452 hours, Unit 1 received Panel 901-8 A7 U1 Emergency Diesel Generator (EDG) Trouble alarm. Equipment Operators were dispatched and the Unit 1 EDG was found running unloaded, without a generator field flash, and no auto start signal received. Troubleshooting identified that a 125 VDC ground had caused the Unit 1 EDG to start. As a result, the Unit 1 EDG was declared inoperable. At this time Unit 2 is in a refueling outage and the Unit 2 EDG is currently inoperable for repairs. Due to the inoperability of the Unit 1 and Unit 2 EDGs, at 2000 hours a Reactor Shutdown was initiated on Unit 1 in accordance with TS 3.8.1.F. In addition, since the EDGs supply emergency power to both Unit's Standby Gas Treatment Systems (SBGTS), emergency power was unavailable to SBGTS; however, normal power supplies remained available. This notification is being made in accordance with 10 CFR 50.72(b)(2)(i), and in accordance with 10 CFR 50.72(b)(3)(v)(D). At 2151 hours, the Unit 1 EDG was declared operable following repairs and successful operability testing. The NRC Resident Inspector has been informed.
ENS 478882 May 2012 11:24:0010 CFR 50.72(b)(3)(iv)(A), System ActuationManual Initiation of Secondary Containment IsolationIn response to a trip of Unit 1 reactor enclosure (secondary containment) HVAC and subsequent loss of reactor enclosure delta-p, a Unit 1 manual secondary containment isolation was initiated per station procedures. This manual initiation also resulted in an isolation signal to containment atmosphere control (CAC) system valves and primary containment instrument gas (PCIG) system valves. System responses were as expected. Unit 1 secondary containment delta-p was restored via standby gas treatment system (SGTS), and Unit 1 secondary containment integrity remains intact and operable. Investigation of the trip of Unit 1 reactor enclosure HVAC is ongoing. This is being reported under 50.72(b)(3)(iv) for containment isolation signal affecting containment isolation valves in more than one system. The licensee notified the NRC Resident Inspector.
ENS 4794522 May 2012 17:11:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationManual Reactor Scram Due to Degrading Condenser VacuumOn Tuesday, May 22, 2012 at 1311 hours (EDT), with the reactor at approximately 35% core thermal power, during a planned power reduction to support thermal backwash of the main condenser, a manual reactor scram was inserted due to degrading main condenser vacuum. The cause of the degraded vacuum is currently under investigation. Following the reactor scram, all rods were verified to be fully inserted and the Primary Containment Isolation System Group II (Reactor Building) and Group VI (Reactor Water Cleanup System) actuations occurred as designed due to the expected reactor water level shrink associated with the scram signal. Standby Gas Treatment System Train 'B,' which is designed to shutdown 65 seconds after the Group II signal is received if the Standby Gas Treatment Train 'A' is in service, continued to operate until manually secured. With this exception, all other plant systems responded as designed. Currently reactor pressure is being maintained at 920 psig with the Mechanical Hydraulic Control System (turbine by-pass valves). Reactor water level is being maintained in normal bands with the Condensate and Feedwater System. Off-Site power is being supplied to the station by the Start-up Transformer (normal power supply for shutdown operations). This event had no impact on the health and/or safety of the public. The NRC Senior Resident Inspector has been notified." The licensee has notified the Massachusetts Emergency Management Agency.
ENS 482693 September 2012 03:04:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Transfer of Emergency Reserve Auxiliary Transformer Isolating Fuel Pool Cooling and Cleanup System, and Fuel Building Ventilation System

At 22:04 CDT on 9/02/2012, the Emergency Reserve Auxiliary Transformer (ERAT) transferred unexpectedly to the Reserve Auxiliary Transformer (RAT). During this transfer, the Fuel Pool Cooling and Cleanup (FC) system pump 'A' tripped and the Fuel Building Ventilation (VF) system isolated. Upper containment pool level dropped below the minimum required level per Technical Specifications (TS) 3.6.2.4 and Secondary Containment differential pressure increased above 0.25 inches vacuum per TS 3.6.4.1. Upper Containment Pool level was restored above the minimum level at 01:27 CDT on 9/3/2012 within the 4 hour completion time. The Upper Containment Pool is a part of the suppression pool makeup system used to ensure the Primary Containment function. Secondary Containment differential pressure was restored at 22:19 on 9/2/2012 when the Standby Gas Treatment System was started. Maintaining secondary containment differential pressure helps to control the release of radioactive material. This event is being reported as a condition that could have prevented the fulfillment of a safety function per 10 CFR 50.72(b)(3)(v)(B) and 10 CFR 50.72(b)(3)(v)(C). The station is currently in a 72-hour action to restore the ERAT to an operable status per TS LCO 3.8.1 Required Action A.2. Plant conditions are stable and actions are underway to repair the ERAT. The NRC Resident (Inspector) has been notified.

  • * * RETRACTION ON 10/26/12 AT 1322 EDT FROM KEN LEFFEL TO DONG PARK * * *

Upper Containment Pool level dropped below the normal pool level of 827 feet-3 inches when the Fuel Pool Cooling and Cleanup system pump 'A' tripped, and was initially reported as dropping below the minimum level (825 feet-6 inches) required by Technical Specification (TS) 3.6.2.4. However, subsequent reports from the field confirmed that the lowest level reached was 827 feet 0 inches, which is greater than the minimum required TS level. Therefore, no loss of safety function occurred for the Upper Containment Pool level as a result of this event, and the event is not reportable under 50.72 (b)(3)(v)(B). The NRC Resident (Inspector) has been notified." Notified R3DO (Pelke).

ENS 482826 September 2012 18:14:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLoss of Secondary Containment Ventilation for Eight SecondsOn September 6, 2012, at 1314 hours, the reactor building ventilation system was being restored to service following planned maintenance and surveillance activities. During the reactor building pressure transition when restoring reactor building ventilation (from the Standby Gas Treatment System), an employee entered a secondary containment interlock and identified a door leading to the environment had opened. The employee immediately secured the door and notified Operations personnel. A review of the door alarm history determined the door was open for approximately eight seconds. Given the temporary breech in secondary containment, this event is reportable under 50.72(b)(3)(v)(C) as an event or condition that could have prevented the fulfillment of a safety function. The licensee notified the NRC Resident Inspector.
ENS 483706 August 2012 01:25:0010 CFR 50.73(a)(1), Submit an LERRps Sub-Component Failure Caused Half Scram with Group 2 Pciv ActuationOn August 5, 2012, at 21:25 EDT, Unit 1 received a Reactor Auto SCRAM System 'A' Trip signal in the main control room. The annunciator was initially reset by operators, but the operating crew noted that some white SCRAM lights and some Group 2 PCIV indication lights were flickering in the control room. This anomaly coupled with the ability to reset the annunciated condition immediately indicated an issue with fluctuating voltage on the power supply for RPS (Reactor Protection System) 'A'. Approximately 30 seconds after the annunciator was reset, the 'A' RPS bus tripped, causing a half SCRAM in conjunction with the automatic actuation of the Standby Gas Treatment system (SGT) and isolation of PCIVs in multiple systems, both of which are normal responses to this loss of the 'A' RPS bus. The crew entered the appropriate abnormal operating procedures and confirmed the actuations automatically occurred as required given the loss of the RPS bus. They investigated the 'A' RPS Motor/Generator (M/G) set, placed the 'A' RPS bus on its alternate supply, reset the SGT and PCIV actuation logic, and returned the PCIVs to their normal position. Upon investigation, the 'A' RPS M/G set was found running, but the Over Voltage Relay in the power monitoring cabinet was chattering. The field investigation team determined that the RPS trip was caused by the failure of its voltage regulator which was then replaced. The 'A' RPS M/G set was consequently returned to service as the primary RPS power source on August 6, 2012. Maintenance personnel subsequently determined that a voltage regulator subcomponent was defective. Because the malfunctioning subcomponent caused the loss of RPS 'A' as the initiating event rather than a valid SGT or PCIV actuation signal, the resulting actuation of SGT and the isolation of multiple PCIVs are considered invalid actuations. Based on that information, 10CFR50.73(a)(2)(iv) allows this event to be reported via a telephone notification within 60 days instead of submitting a written LER. The licensee has notified the NRC Resident Inspector.
ENS 4846631 October 2012 18:41:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Both Trains of Standby Gas Treatment System InoperableOn Wednesday, October 31, 2012 at 1200 hours, with the reactor at approximately 100% core thermal power and steady state conditions, Standby Gas Treatment (SBGT) System Train 'B' was removed from service (made inoperable) for surveillance testing. At 1441 hours, the control room staff declared the Standby Gas Treatment System Train 'A' inoperable as a result of an engineering analysis that determined that 480 VAC feed, Motor Control Center (MCC) B15, had the potential to exceed its trip set point under worst case bus loading. The inoperability of both SBGT System Trains 'A' and 'B' could have prevented the fulfillment of the safety functions to 'control the release of radioactive material' and 'mitigate the consequences of an accident.' At 1510 hours, a compensatory measure was taken to preclude the overload condition on MCC B15 and the SBGT System Train 'A' was restored to operable status. At the time of submittal of this notification, the SBGT System Train 'B' remains inoperable for replacement of an overload relay. SBGT System Train 'B' is expected to be returned to service this evening. This event had no impact on the health and/or safety of the Public. The USNRC Senior Resident Inspector has been notified.
ENS 4850312 November 2012 21:51:0010 CFR 50.72(b)(3)(iv)(A), System ActuationReactor Building Isolation with Standby Gas Treatment System Actuation During Radioactive Material MoveAt 1551 EST on 11/12/12, the 'A' Refuel Floor Process Radiation Monitor reached 62 mR/hr during movement of the old steam dryer in the plant reactor building. This resulted in the isolation of the drywell containment air monitor and the oxygen analyzer primary containment isolation valves. The signal also resulted in a reactor building isolation (Secondary Containment), start of 'A' Standby Gas Treatment, and transfer of the control room ventilation to the High Radiation Mode. All automatic isolation valves have been reset. Reactor building and control room ventilation have been reset. Standby gas treatment has been secured. There were no challenges to the health and safety of the general public. The NRC Resident Inspector has been notified.
ENS 4853324 November 2012 02:08:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Inadvertent Loss of Instrument AirOn 11/23/2012 at approximately 1956 CST, it was reported that the Control Room (VC) B Chiller breaker was cycling open and closed. In order to stop the cycling, Control Building Unit Sub B was manually tripped causing the following isolations/actuations: loss of power to instrument air (IA) system containment isolation valves causing the Division 2 valves to isolate; loss of power to the low pressure switch that resulted in an automatic start of Division 2 Shutdown Service Water (SX) system; and loss of power to fuel building (VF) system ventilation Division 2 dampers resulting in a trip of the VF system. High Pressure Core Spray (HPCS) became inoperable based on inoperability of the room cooler for the associated Division 4 inverter and battery charger. Operations entered the Loss of AC Power and Automatic Isolation off-normal procedures. Following the loss of power to the VF system ventilation, at 2008, secondary containment differential pressure became positive. At 2009, power was restored to Control Building Unit Sub B and HPCS was restored to operable. At 2011, the standby gas treatment system (VG) was started and at 2013, secondary containment differential pressure was restored. Following re-energization of Unit Sub B, the IA containment isolation valves were re-opened, VG was secured, VF restarted and the Division 2 SX pump was secured. The loss of secondary containment differential pressure is reportable under 10 CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material An unplanned inoperability of HPCS reportable under 10 CFR 50.72(b)(3)(v)(D) as HPCS is a single train safety system The cause of the breaker cycling is unknown at this time. The NRC Resident has been informed.
ENS 485658 October 2012 22:09:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification of Invalid System ActuationOn October 8, 2012, at 1709 EDT, Unit 2 received a Reactor Auto SCRAM System 'B' Trip signal in the main control room. The power monitoring breaker in RPS panel 2C71P003D tripped, causing a half-SCRAM in conjunction with the automatic actuation of the Unit 2 standby gas treatment system (SGT) and isolation of CIVs (Containment Isolation Valves) in multiple systems, both of which are normal responses to this loss of the 'B' RPS bus. The crew entered the appropriate abnormal operating procedures and confirmed the actuations automatically occurred as required given the loss of the RPS bus. They investigated the 'B' RPS Motor/Generator (M/G) set, placed the 'B' RPS bus on its alternate supply, reset the SGT and CIV actuation logic, and returned the CIVs to their normal position. Upon investigation, the 'B' RPS M/G set was found running with a steady output of 120 VAC. The breaker in RPS panel 2C71P003B stayed closed in. Further troubleshooting did not identify a cause for the failure of RPS breaker 2C71B003D. The breaker was replaced and the power monitoring relays were rebuilt. The 'B' MG Set was left running unloaded for 8 days with no trips observed. On October 26, 2012, approximately 20 seconds after returning the RPS 'B' M/G Set to service, RPS breaker 2C71B003D tripped again. At this time, investigators determined that 2C71B003B had no output voltage present when load was increased to 25 amps or greater. 2C71B003D tripped because 2C71B003B was not supplying load to it. A lug mounting screw was subsequently found to be loose on 2C71B003B. After tightening the screw, maintenance personnel determined that continuity existed and the 2C71B003B indicated closed with output voltage present as expected. Review of the six-month surveillances on 2C71B003B and the more-detailed 5-year surveillance that took place in August 2010 revealed no previous problems with the breaker. It is unknown when the lug mounting screw became loose or if repeated cycles of operation caused it to loosen. For broadness, thermography testing is being completed on 2C71P003 A, C, D, E, F and 1C71P003 A, B, C, D, E, F. When the second trip of 2C71B003D occurred on October 26, 2012, U1 SGT trains started and CIVs in multiple systems closed. This was an expected actuation with radiation monitor 2D11K634C already out of service and in the tripped condition at the time of the RPS 'B' trip. The RPS 'B' trip caused radiation monitor 2D11K634D to also trip thereby completing the logic to start U1 SGT trains and to close associated CIVs. The second event is included in this report since the failures are related as a result of having the same general cause and since they occurred over a reasonably short period of time. Because a malfunctioning subcomponent caused the loss of RPS 'B' rather than a valid CIV actuation signal, the resulting isolation of CIVs in multiple systems is considered an invalid actuation in both cases. Based on that information 10CFR50.73(a)(2)(iv) allows these events to be reported via a telephone notification within 60 days instead of submitting a written LER. The licensee will notify the NRC Resident Inspector.
ENS 4868922 January 2013 06:13:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Pressure Positive for 12 SecondsOn 01/22/2013 at 00:30 Reactor building HVAC tripped due to low outside air temperature and Standby Gas Treatment system was manually started and maintained Reactor Building differential pressure negative. At 01:13 secondary containment pressure went positive during restart of the Center Reactor Building HVAC Train. This is a loss of secondary containment function. In a 12 second time span secondary containment pressure went above 0 inches WC (Water Column) to +0.17 inches WC and then decreased to < 0 inches WC remaining stable during the Reactor Building HVAC restart. The Center Reactor Building HVAC Exhaust Fan Discharge Damper opened after the Supply Fan discharge damper; this condition would produce the indications noted. The System was returned to normal with two Reactor Building HVAC trains running and the Standby Gas Treatment System shutdown and in standby. Reactor building pressure is stable with differential pressure negative < - 0.30 inches WC. The loss of Secondary Containment function is reportable under 10 CFR 50.72 (b)(3)(v)(C) as an event or condition that could have prevented the fulfillment of a safety function needed to control the release of radioactive material. The licensee notified the NRC Resident Inspector.
ENS 4893917 April 2013 20:11:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Notification of Unusual Event Declared Due to Loss of Offsite Power from a Lightning Strike

LaSalle Unit 1 and LaSalle Unit 2 have both experienced an automatic reactor scram, in conjunction with a loss of offsite power. This was caused by an apparent lightning strike in the main 345kV/138kV switchyard during a thunderstorm. 138kV line 0112 has been inspected in the field, and heavy damage has been noted on the insulators on two of the three phases on a line lightning arrestor line side. The plant systems have all responded as expected. All five diesel generators started, and have loaded on to their respective buses as designed. All rods went full in on both units during the respective scrams. HPCS (High Pressure Core Spray) system was started on each unit and automatically aligned for injection for initial level control. The MSIVs (Main Steam Isolation Valves) are shut on both units with decay heat being removed via the safety relief valves. Suppression pool cooling is in progress. The licensee will notify the NRC Resident Inspector and has notified the State. Notified DHS, FEMA, USDA, HHS, DOE, NICC, EPA, and Nuclear SSA via email.

  • * * UPDATE FROM DON PUCKETT TO VINCE KLCO AT 2113 EDT ON 4/17/2013 * * *

In addition to information (previously provided), LaSalle Unit 2 received a high drywell pressure signal (1.77 psig) due to loss of containment cooling from the loss of power. At the time of this high drywell pressure signal, high pressure core spray pump and 2B residual heat removal (RHR) pump was already in operation, the low pressure core spray system and 2A residual heat removal system was secured and (placed) in pull to lock. When the signal was satisfied the ECCS (Emergency Core Cooling Systems) signal was processed but only the 2C RHR pump would have started. In this case, the 2C RHR pump tripped when the signal was received. There is no evidence of reactor coolant leakage. There was no additional ECCS systems discharging into the RCS (Reactor Coolant System). As (initially stated), level was controlled using High Pressure Core Spray and level control is now being maintained using the Reactor Core Isolation Cooling (RCIC) systems. The 2C RHR pump trip is under investigation. Due to the initial loss of offsite power for both Unit 1 and Unit 2 reported at 1511 (CDT), multiple containment isolation valves isolated and closed as expected. Once initial containment isolations were verified, two Unit 2 primary containment vent and purge valves were opened to vent the Unit 2 containment. Once Unit Two containment pressure reached 1.77 (psig), these two vent valves isolated as expected. Due to the loss of offsite power, the Station Vent Stack Wide Range Gas Monitor (WRGM) and the Standby Gas Treatment Wide Range Gas Monitor (VGWRGM) also lost power. Manual sampling has been implemented and power is restored to the VGWRGM, however the VGWRGM has not been declared operable yet. Normal radiation levels have been reported from the manual sampling. (This is being reported in accordance with 10CFR50.72(b)(3)(xiii).) The licensee notified the NRC Resident Inspector and the State of Illinois. Notified the R3 IRC, NRR EO(Skeen), IRD MOC (Grant).

  • * * UPDATE AT 0057 EDT ON 04/18/13 FROM MIKE LAWRENCE TO S. SANDIN * * *

After the Unit 2 primary containment vent and purge system isolated on the Unit 2 containment High Pressure signal, Venting of the Unit 1 primary containment was commenced. At 2005 CDT, Unit 1 primary containment pressure reached the Group 2 primary containment isolation system setpoint (1.77 PSIG) causing the primary containment vent and purge valves being used to vent the Unit 1 containment to isolate. Unit 1 primary containment venting was being performed through the Standby Gas Treatment system which is a filtered system. In addition to the primary containment isolation signal on high drywell pressure, an ECCS initiation on high drywell pressure also occurred. The ECCS signal resulted in an auto start of the 1C RHR system. The 1B RHR system was already running in suppression pool cooling mode. 1A RHR and LPCS had been secured to prevent overloading the common diesel generator for division 1. The common diesel generator supplies both Unit 1 and Unit 2 division 1 ESF busses. The licensee informed the NRC Resident Inspector. Notified NRR EO (Skeen), IRD MOC (Grant) and R3IRC (Louden).

  • * * UPDATE AT 0947 EDT ON 04/18/13 FROM JUSTIN FREEMAN TO PETE SNYDER * * *

LaSalle has terminated the unusual event which was initiated at 1511 on 4/17/13 and reported under EN 48939. This unusual event has been terminated based on meeting the following established criteria. This report is being made in accordance with 10CFR50.72.(c)(1)(iii). 1) Off-site power has been restored to all ESF busses 2) Fuel Pool Cooling has been restored on both units 3) Primary Containment Chillers have been restored on both units 4) Drywell pressure is less than ECCS initiation setpoint 5) ECCS signals cleared to allow diesels to be placed in stand by Recovery of remaining plant systems will be managed through the Outage Control Center (OCC)." The licensee informed the NRC Resident Inspector. Notified R3DO (Orth), NRR EO (Chernoff), IRD (Grant), DHS, FEMA, USDA, HHS, DOE, NICC, EPA, and Nuclear SSA via email.

  • * * UPDATE AT 1711 EDT ON 4/21/2013 FROM GREG LECHTENBERG TO MARK ABRAMOVITZ * * *

In addition to the 10 CFR 50.72 Sections initially identified, the Loss of Offsite Power was also reportable under 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented the fulfillment of the safety function of systems needed mitigate the consequences of an accident. This event is considered a safety system functional failure for both Units 1 and 2. The licensee will notify the NRC Resident Inspector. Notified the R3DO (Orth).

ENS 4921114 June 2013 22:06:0010 CFR 50.73(a)(1), Submit an LERInvalid Primary Containment Isolation System Actuation Due to a Radiation Monitor SpikeThis notification is being made in accordance with 10CFR50.73(a)(2)(iv)(A) to provide information pertaining to an invalid Primary Containment Isolation System (PCIS) Group 3 actuation signal that affected containment valves in more than one system. On 6/14/2013, and again on 7/11/2013, with the reactor at 100% power, an invalid PCIS Group 3 actuation occurred from a momentary spike of the 'A' Refuel Floor radiation monitor which reached the instrument's high radiation trip setpoint. A radiation protection technician was dispatched to the refuel floor and dose rates in the vicinity of the 'A' radiation monitor detector were verified to be normal and below the alarm setpoints. The radiation monitor was verified to be indicating normal expected radiation levels. Subsequent visual inspection and functional checks of the radiation monitors were completed satisfactory and the instrument channel was returned to service. The cause of the spurious spikes is attributed to an unknown source of electrical noise. The issue with spurious spiking has been entered into the station's corrective action program. Both trains of Standby Gas Treatment System started as designed and Reactor Building ventilation isolated. The train actuation was complete. The PCIS functioned successfully providing a complete Group 3 isolation. The PCIS Group 3 isolation involves the following systems. Drywell and Suppression Chamber air and vent: V16-19-6A, 6B, 7, 7A, 7B, 8, 9, 10, 23 Containment Makeup: V-16-20-20, 22A, 22B Containment Air Sampling: VG-23, 26, V109-76A, 76B Containment Air compressor suction: V72-38A, 38B Containment Air Dilution: VG-9A, 9B, 22A, 22B, NG-11A, 11B, 12A, 12B, 13A, 13B In accordance with 10CFR50.73(a)(1) a telephone notification is being made instead of submitting a written Licensee Event Report. The licensee has notified the NRC Resident Inspector and will notify the State and local agencies.
ENS 4935823 July 2013 04:00:0010 CFR 50.73(a)(1), Submit an LERInvalid Primary Containment Isolation System Group 3 ActuationThis notification is being made in accordance with 10CFR50.73 (a)(2)(iv)(A) to provide information pertaining to an invalid Primary Containment Isolation System (PCIS) Group 3 actuation signal that affected containment valves in more than one system. On 7/23/2013, and again on 7/24/2013, with the reactor at 100% power, an invalid PCIS Group 3 actuation occurred from a momentary spike of the 'B' Reactor Building ventilation radiation monitor which reached the instrument's high radiation trip set point. A radiation protection technician was dispatched and radiation levels in the vicinity of the 'B' radiation monitor were verified to be normal and below the alarm set points. The radiation monitor was verified to be indicating normal expected radiation levels. Subsequent visual inspection and functional checks of the radiation monitors were completed satisfactory and the instrument channel was returned to service. At the recommendation from the vendor, the detectors were replaced in both of the Reactor Building ventilation monitors as well as the Refuel Floor radiation monitors. On 8/19/2013, 9/12/2013, and 9/13/2013, with the reactor at 100% power, invalid PCIS Group 3 actuations occurred from a momentary spike of the 'A' Refuel Floor radiation monitor which reached the instrument's high radiation trip set point. A radiation protection technician was dispatched to the refuel floor and dose rates in the vicinity of the 'A' radiation monitor detector were verified to be normal and below the alarm set points. The radiation monitor was verified to be indicating normal expected radiation levels. Subsequent visual inspection and functional checks of the radiation monitors were completed satisfactory and the instrument channel was returned to service. Both trains of Standby Gas Treatment System started as designed and Reactor Building ventilation isolated as a result of the invalid PCIS actuation. The PCIS functioned successfully providing a complete Group 3 isolation. The PCIS Group 3 isolation involves the following systems: Drywell and Suppression Chamber air and vent: V16-19-6A, 6B, 7, 7A, 7B, 8, 9, 10, 23 Containment Makeup: V-16-20-20, 22A, 22B Containment Air Sampling: VG-23, 26, V109-76A, 76B Containment Air compressor suction: V72-38A, 38B Containment Air Dilution: VG-9A, 9B, 22A, 22B, NG-11A, 11B, 12A, 12B, 13A, 13B Since no actual high radiation condition existed which required the PCIS Group 3 isolation, and the actuation was not in response to actual plant conditions satisfying the requirements for isolation, this event has been classified as an invalid actuation. This event did not result in any adverse impact to the health and safety of the public. In accordance with 10CFR50.73(a)(1) a telephone notification is being made instead of submitting a written Licensee Event Report. The licensee has notified the NRC resident inspector.
ENS 4953113 November 2013 07:26:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Zone II Differential Pressure Lost During Recovery from Ventilation Drawdown Test

On November 13, 2013 at 0226 (EST), Secondary Containment Zone II (Unit 2 Reactor Building) differential pressure was lost during restoration of a ventilation drawdown test. During restoration Unit 2 'A' Train Reactor Building Ventilation fans tripped. The 'B' Train fans were placed in service and secondary containment was restored. Zone I (Unit 1 Reactor Building) and III (Common Refuel Floor Area) ventilation remained in service and stable. Zone II differential pressure recovered within a few minutes and was verified to be stable. LCO 3.6.4.1 was exited for both units at 0257 (EST). Tech Spec Secondary Containment Operability requires a negative pressure of at least 0.25 inches water gauge. There have been no further perturbations in differential pressure and secondary containment remains operable. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022 Rev 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The cause of the Unit 2 "A" Train Reactor Building ventilation fans tripping is still under investigation. The licensee has notified the NRC Resident Inspector.

  • * * RETRACTION ON 1/10/14 AT 1657 EST FROM DOUG LAMARCA TO NESTOR MAKRIS * * *

NUREG-1022, Revision 3 states, ' reports are not required when systems are declared inoperable as part of a planned evolution for maintenance or surveillance testing when done in accordance with an approved procedure and the plant's TS (unless a condition is discovered that would have resulted in the system being declared inoperable).' The event reported in this event notification occurred during a pre-planned evolution for surveillance testing that was done in accordance with an approved procedure and the Susquehanna Technical Specifications. The loss of differential pressure occurred during restoration from the surveillance test and occurred prior to completing the planned evolution and declaring the system OPERABLE. Specifically, the trip of the fans occurred when restoring the Reactor Building normal ventilation after a Zone 1, 2, and 3 isolation (returning back to normal ventilation from the Standby Gas Treatment System). The secondary containment boundary and standby gas treatment system were unaffected. This event occurred as a result of the testing process and would not have occurred during normal operation of the system. There was no discovered condition that would have resulted in the safety function of the system being declared inoperable under normal, non-testing conditions. Based on the above additional information, PPL is retracting this report. Susquehanna was in a planned evolution and did not discover a condition that could have prevented performing a safety function. The licensee has notified the NRC Resident Inspector. Notified the R1DO (Schmidt).