At 1526 on 5/26/2010, while operators were increasing power with reactor recirculation flow, an
RPS (
Reactor Protection System) actuation occurred in both channels and all
control rods inserted.
RPV (
Reactor Pressure Vessel) level decreased to 114.5 inches (Low level setpoint is less than 127 inches). Following the
scram, the
PCIS (
Primary Containment Isolation System) groups 2, 3, 4 and 5 received actuation signals and all open valves isolated. Both trains of
standby gas treatment system actuated.
Plant actions taken included entering procedures OT-3100, Reactor Scram on RPS Actuation and EOP-1, RPV Control on Low Level Signal. The EOP-1 was exited per shift manager direction because of no emergency. The operators stabilized the plant and reset both RPS and PCIS. An investigation into the cause of the scram is continuing.
Electrical power is being supplied from offsite sources through the startup transformers.
The licensee notified the NRC Resident Inspector.