ENS 42489
ENS Event | |
---|---|
09:32 Mar 11, 2006 | |
Title | Invalid Actuation of Containment Isolation Valves |
Event Description | On 03/11/06 at approximately 0432 hours0.005 days <br />0.12 hours <br />7.142857e-4 weeks <br />1.64376e-4 months <br />, with Susquehanna Unit 1 in the Refueling Mode (0% power), the Unit experienced a partial isolation of Primary Containment isolation valves. The actuation occurred when a blown fuse disrupted power to a containment isolation logic relay. The inboard isolation valve to the 'B' Drywell Floor Drain Sump and the Containment Instrument Gas purge supply valve to the TIP indexer both closed. The 'A' Standby Gas Treatment system fan and the 'A' Reactor Building Recirculation fan successfully auto started during the event.
This event constitutes an invalid system actuation and is reportable under 10CFR 50.73(a)(2)(iv)(A). The condition meets the criteria of 10CFR 50.73(a)(2)(iv)(B)(2) because a general containment isolation signal affected containment isolation valves in more than one system. This notification is being provided via a 60-day optional phone call as permitted under 10CFR 50.73(a)(1) in lieu of a written LER. As stated above, both valves affected by the invalid signal fulfilled their isolation function by successfully closing. At the time of the event, no other Primary Containment isolation valve was being maintained in a manner that required re-positioning. There were no challenges to the Reactor as a result of this event. The plant responded as expected. Following replacement of the subject fuse, the isolation logic was successfully reset and affected equipment was restored to the desired status. The licensee notified the NRC Resident Inspector. |
Where | |
---|---|
Susquehanna Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+745.05 h31.044 days <br />4.435 weeks <br />1.021 months <br />) | |
Opened: | Grant Fernsier 09:35 Apr 11, 2006 |
NRC Officer: | Bill Gott |
Last Updated: | Apr 11, 2006 |
42489 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 42489\u003C/a\u003E - \u003Ca href=\"/Susquehanna\" title=\"Susquehanna\"\u003ESusquehanna\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003EInvalid Actuation of Containment Isolation Valves\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 42489 - Susquehanna\n","link":"","lat":41.09256666666667,"lon":-76.14176944444445,"icon":"/w/images/c/c7/Talen_Energy_icon.png"}],"imageoverlays":null} | |
WEEKMONTHYEARENS 541032019-04-18T05:10:00018 April 2019 05:10:00
[Table view]10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification Due to Invalid Specified System Actuation ENS 527722017-04-03T01:27:0003 April 2017 01:27:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification of Invalid Specified System Actuation ENS 480922012-05-14T13:28:00014 May 2012 13:28:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification for an Invalid Emergency Service Water Actuation ENS 457262010-02-25T19:18:00025 February 2010 19:18:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Valves ENS 435552007-06-09T09:11:0009 June 2007 09:11:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of the 'C' Emergency Diesel Generator ENS 424892006-03-11T09:32:00011 March 2006 09:32:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Valves ENS 407662004-04-04T18:57:0004 April 2004 18:57:00 10 CFR 50.73(a)(1), Submit an LER 60 -Day Report: Invalid Actuation of the "E" Emergency Diesel Generator ENS 407332004-03-21T16:32:00021 March 2004 16:32:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Signals in More than One System ENS 401732003-08-29T14:25:00029 August 2003 14:25:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Valves 2019-04-18T05:10:00 | |