Semantic search

Jump to navigation Jump to search
 Entered dateSiteRegionReactor typeEvent descriptionTopic
ENS 4488127 February 2009 04:37:00PerryNRC Region 3GE-6

The Perry Nuclear Power Plant will be taking the Plant Computer out of service for scheduled maintenance which will take ERDS out of service. From 0500 hours EST on February 27, 2009 for approximately 15 hours, personnel will be performing inspection and cleaning activities on the Plant Computer power center panel. During the planned maintenance, the Safety Parameter Display System (SPDS) and the automatic mode calculation of the Computer Aided Dose Assessment Program (CADAP) will be unavailable. In the event of an emergency, plant parameter data will be orally transmitted to the facilities through the Status Board Ring Down circuit with back-up by the Private Branch Exchange, the Off Premise Exchange, and various redundant intra-facility circuits throughout the emergency facilities. The dose assessment function will be maintained during the out of service time period by manual input of data into CADAP and, if required, by manual calculation. The ability to open and maintain an 'open line' using the Emergency Notification System will not be affected and will be the primary means of transferring plant data to the NRC as a contingency until the ERDS can be returned to service during the period of unavailability. This event is being reported in accordance with 10 CFR 50.72(b)(3)(xiii), as a condition that results in a major loss of offsite communications capability. A follow-up notification will be made when the maintenance activities are completed and the equipment is restored. The NRC Resident Inspector has been notified.

  • * * UPDATE FROM TOM MORSE TO JOE O'HARA AT 1910 EST ON 2/27/09 * * *

The Perry Plant computer and the ERDS have been restored to service as of 1845 EST this evening. The licensee will notify the NRC Resident Inspector.

ENS 4490513 March 2009 00:42:00PerryNRC Region 3GE-6

The Perry Nuclear Power Plant has taken a portion of the Plant Computer out of service for scheduled maintenance. This has resulted in a portion of ERDS being out of service. From 0025 hours EDT on March 13, 2009 for approximately 36 hours, personnel will be performing maintenance activities which result in a partial loss of the Plant Computer. During this planned maintenance, portions of the Safety Parameter Display System (SPDS) and the automatic mode calculation of the Computer Aided Dose Assessment Program (CADAP) will be unavailable. In the event of an emergency, plant parameter data will be orally transmitted to the facilities through the Status Board Ring Down circuit with back-up by the Private Branch Exchange, Off Premise Exchange, and various redundant intra-facility circuits throughout the emergency facilities. The dose assessment function will be maintained during the out of service time period by manual input of data into CADAP and, if required, by manual calculation. The ability to open and maintain an 'open line' using the Emergency Notification System will not be affected and will be the primary means of transferring plant data to the NRC as a contingency until the ERDS can be returned to service during the period of unavailability. This event is being reported in accordance with 10CFR50.72(b)(3)(xiii), as a condition that results in a major loss of offsite communication capability. A follow-up notification will be made when the maintenance activities are completed and the equipment is restored. The licensee notified the NRC Resident Inspector.

  • * * UPDATE AT 1132 ON 3/14/2009 FROM TONY JARDINE TO MARK ABRAMOVITZ * * *

The plant has extended the expected plant computer outage time by 60 hours (ending 3/16/2009 at 2400). Notified the R3DO (Lara).

  • * * UPDATE AT 1907 EDT ON 3/16/2009 FROM TOM STEC TO BILL HUFFMAN * * *

The licensee has extended the expected outage time for the plant computer maintenance by an additional 24 hours. Repairs are now expected to be completed by 2400 EDT on 3/17/09. The licensee will notify the NRC Resident Inspector. R3DO(Ring) notified.

  • * * UPDATE AT 1723 EDT ON 3/17/2009 FROM ANTHONY JARDINE TO BILL HUFFMAN * * *

The licensee states that that the plant computer and all associated functions (SPDS, CADAP, and ERDS) were returned to service at 1313 EDT on 3/17/09. The licensee has notified the NRC Resident Inspector.

R3DO(Ring) notified.
ENS 4494530 March 2009 23:04:00PerryNRC Region 3GE-6

On March 30, 2009, at approximately 1843 hours EDT, the control room reported a loss of power to non-safety 480 volt busses F1C and F1D. Initial investigation revealed an instantaneous ground over-current (50G) relay had actuated. This relay actuation resulted in the supply breaker tripping and all associated loads being de-energized. This resulted in a loss of 120 VAC non-essential electrical power to a portion of the Emergency Response Data System (ERDS). In the event of an emergency, plant parameter data will be orally transmitted to the facilities through the status Board Ring Down circuit with back-up by the Private Branch Exchange, Off Premise Exchange, and various redundant intra-facility circuits throughout the emergency facilities. The ability to open and maintain an open line using the Emergency Notification System will not be affected and will be the primary means of transferring plant data to the NRC as a contingency until the ERDS can be returned to service during the period of unavailability. This event is being reported in accordance with 10 CFR 50.72(b)(3)(xiii) as a condition that results in a major loss of emergency offsite communications capability. A follow-up notification will be made when the equipment is restored. The NRC Resident Inspector has been notified." The unit is currently defueled.

  • * * UPDATE FROM TOM STEC TO JOE O'HARA AT 1600 EDT ON 3/31/09 * * *

Last evening, power was restored to ERDS following maintenance. ERDS is capable of performing its intended function. Notified R3DO(Orth)

ENS 4498914 April 2009 14:18:00PerryNRC Region 3GE-6On April 14, 2009, at approximately 0743 hours, electrical power was lost to 480 volt busses V-1-F and V-2-F. These busses supply electrical power to the Emergency Response Data System (ERDS). The electrical power loss caused the ERDS, the Safety Parameter Display System (SPDS), and the automatic mode calculation of the Computer Aided Dose Assessment Program (CADAP) to be disabled. Preliminary investigation indicates that a failed inverter caused the power loss. Contingency plans have been established to transmit plant parameter data and perform the dose assessment function in the event of an emergency while ERDS is unavailable. The ERDS, SPDS and CADAP were restored at 1110 hours. This event is being reported in accordance with 10 CFR 50.72(b)(3)(xiii), as a condition that results in a major loss of offsite communications capability." The NRC Resident Inspector has been notified.
ENS 4502528 April 2009 00:55:00PerryNRC Region 3GE-6

On April 27, 2009, at approximately 1730 hours, with the plant in Mode 5 during refueling outage (RFO) 12, RHR 'A' pump tripped while operating in shutdown cooling. RHR 'A' was the primary decay heat removal shutdown cooling system. RHR 'B' was the backup decay heat removal shutdown cooling system. Preliminary investigation shows that jumper installation activities associated with plant testing resulted in a blown fuse and closure of the RHR shutdown cooling outboard common suction isolation valve (1E12F008). Closure of the 1E12F008 valve tripped the RHR 'A' pump and prevented the RHR 'B' pump from being used to initiate shutdown cooling from the control room. Operators were preparing to manually open 1E12F008 in parallel with activities to restore control from the control room. The plant entered Technical Specification 3.9.9, 'RHR - Low Water Level', Conditions A and C due to 1E12F008 isolating causing the loss of shutdown cooling. Action A.1 calls for verification of an alternate method of decay heat removal available for each inoperable RHR shutdown cooling subsystem in 1 hour and once per 24 hours thereafter. This was completed with the fuel pool cooling and cleanup system's two pumps and two heat exchangers cooled by NCC (Nuclear Closed Cooling System) (available due to the ability to reflood the upper pools with a hotwell pump through normal cavity reflood path) being one alternate system. A second alternate system was the utilization of the low pressure core spray to flood the vessel, returning to the suppression pool through safety relief valves, and a loop of RHR in suppression pool cooling. Actions for Condition C, to verify reactor coolant circulation by an alternate method and to monitor reactor coolant temperature were not met due to no reactor coolant flow past a valid temperature monitoring point. Approximate reactor coolant temperature was being trended using the reactor water cleanup system. The blown fuse was identified and replaced at approximately 1816 hours. The RHR 'B' pump was started at approximately 1834 hours. From the time that the RHR 'A' pump tripped (approximately 1730), until the RHR 'B' pump was started, the reactor temperature increased from 94 degrees F to 97 degrees F. Pre-determined time to boil had been calculated to be 9 hours. At approximately 1835 hours, TS 3.9.9 Condition C was exited due to the RHR 'B' shutdown cooling loop being placed in operation. This event is being reported as an event or condition that at the time of discovery could have prevented fulfillment of a safely function of structures or systems that are needed to remove residual heat under 10 CFR 50.72 (b)(3)(v)(B). The NRC Resident Inspector has been notified.

* * * RETRACTION FROM C. ELBERFELD TO P. SNYDER AT 1727 ON 6/25/09 * * * 

The purpose of this call is to retract Event Number 45025. On April 28, 2009, at 0055 hours, notification was made to the NRC Operations Center by the Perry Nuclear Power Plant (PNPP) reporting a condition that at the time of discovery could have prevented the fulfillment of the safety function of a system that is needed to remove residual heat (10 CFR 50.72(b)(3)(v)(B)). Jumper installation activities associated with plant testing resulted in a blown fuse and closure of the Residual Heat Removal (RHR) shutdown cooling outboard common suction isolation valve. Closure of the valve resulted in the RHR A pump tripping, as designed. The blown fuse was replaced and the valve reopened. The RHR B subsystem was then started as the primary decay heat removal shutdown cooling system. Additionally, it was initially questioned whether Technical Specification Limiting Condition for Operation 3.9.9 Required Actions were met to verify reactor coolant circulation by an alternate method and to monitor reactor coolant temperature. Based on further evaluation, it was determined that there was not a reasonable expectation of the loss of safety function of a system needed to remove residual heat (i.e., the RHR System). The redundant RHR B subsystem was manually aligned and operated in a timely manner to continue to meet the system requirements to fulfill the safety function. Since the condition reported in Event Number 45025 would not have prevented the fulfillment of the safety function of a system that is needed to remove residual heat, the condition is not reportable, and this notification is retracted. Additionally, it was determined that verification of reactor coolant circulation by an alternate method (i.e., Reactor Water Cleanup System) was performed and that monitoring of reactor coolant temperature was appropriate. Therefore, based on not meeting any 10 CFR 50.73 reporting criteria, no Licensee Event Report is required. The evaluations (i.e., Reportability Reviews) for this condition are documented in Condition Report 09-58110 and Condition Report 09-58123. The licensee notified the NRC Resident Inspector.

  • * * UPDATE FROM JOHN PELCIC TO CHUCK TEAL AT 1515 EST ON 3/10/10 * * *

The Residual Heat Removal (RHR) system common suction isolation valve 1E12-F008 received an invalid isolation signal resulting in the operating RHR A pump tripping while the system was in the shutdown cooling mode of operation. The event was reported to the NRC Operations Center on April 28, 2009 in accordance with 10 CFR 50.72(b)(3)(v)(B). The event notification was subsequently retracted on June 25, 2009. This event was reevaluated for reportability via Condition Report 10-71293 using additional guidance and enforcement history related to safety system functional failure reporting. Based on results of this evaluation, the April 27, 2009, loss of shutdown cooling event is reportable as a Licensee Event Report (LER) under 10 CFR 50.73(a)(2)(v)(B), 'Any event or condition that could have prevented the fulfillment of the safety function of structures, or systems that are needed to remove residual heat.' Perry LER 2010-001 will be submitted to report this event. The NRC Resident Inspectors have been notified.

Time of Discovery
Time to boil
ENS 4514721 June 2009 20:58:00PerryNRC Region 3GE-6On June 21, 2009, at approximately 1750 hours, an automatic Reactor Protection System (RPS) actuation occurred at the Perry Nuclear Power Plant, Unit 1. At the time of the event, the plant was in Mode 1 at 100% power. All control rods are inserted into the core and the plant is currently stable, in Mode 3 (Hot Shutdown) with reactor pressure at approximately 930 psig. No Emergency Core Cooling Systems were required or utilized to respond to the event and there were no other reportable actuations. Reactor coolant level is being maintained in its normal band by the feedwater system and decay heat is being removed by the condenser. The plant is in a normal electrical line-up with all three Emergency Diesel Generators operable and available if needed. The cause of the reactor scram is currently under investigation. Preliminary indications are that the cause of the RPS actuation is related to a main turbine trip. The NRC Resident Inspector has been notified. No safety relief valves lifted during the event and a reactor cooldown is in progress.
ENS 454239 October 2009 18:07:00PerryNRC Region 3GE-6On October 9, 2009, at approximately 1544 hours EDT, notification of an oil spill was made to the U.S. Environmental Protection Agency (EPA), National Response Center. At the time of the event, the plant was in Mode 1 at 100% power. The oil spill was the result of delivery activities related to a backhoe that was delivered to the Perry Nuclear Power Plant in the owner controlled area. The spill was initially estimated to be approximately 3 to 5 gallons of a red colored oil resembling hydraulic fluid. With current rainy weather conditions, the resultant sheen covered an area of approximately 20 to 25 feet by 100 feet of gravel and asphalt. The spill drained into two storm drains. The backhoe was moved inside of a building with a concrete floor. Absorbent material and oil selective soak mulch were placed on the area of the spill. Clean Harbors Incorporated (CHI) was contacted for clean up assistance. CHI representatives are providing assistance for clean-up remediation. Additionally, the Ohio EPA: State Emergency Response Commission, Perry Township Fire Department, Lake County Emergency Planning committee, and the U.S. Coast Guard were notified in accordance with plant procedures. This event is also being reported in accordance with the Operating License, Appendix B, Environmental Protection Plan, which states in part, 'Any occurrence of an unusual or important event that indicates or could result in significant environmental impact causally related to plant operation shall be recorded and reported to the NRC within 24 hours followed by written report. Specifically, unanticipated or emergency discharge of waste water or chemical substances.' The licensee has notified the NRC Resident Inspector.
ENS 4543415 October 2009 14:47:00PerryNRC Region 3GE-6This event is being reported in accordance with 10CFR50.72(b)(2)(i). On October 15, 2009, at approximately 1225 hours, the Perry Nuclear Power Plant commenced a Technical Specification required plant shutdown. On October 14, 2009, At 1747 hours, the Division 2 Emergency Service Water (ESW) system was declared inoperable and unavailable for planned work. The plant entered Technical Specification (TS) 3.7.1 Action A for one inoperable ESW Division. Other supported TSs were also entered (TS 3.8.1 for the Division 2 diesel generator, TS 3.6.1.7 for Containment Spray 'B', TS 3.6.2.3 for Suppression Pool Cooling 'B', TS 3.7.10 for Emergency Closed Cooling 'B', TS 3.5.1 for LPCI 'B' & 'C', among others). On October 15, 2009, at 0601 hours, the ESW 'B' pump was started for a planned pump run. At 0718 hours, the ESW 'B' pump tripped for unknown reasons. The determination was made to commence a controlled plant shutdown and power reduction commenced at 1225 hours. This decision was based on the anticipated investigation and repair time of ESW 'B' pump exceeding the TS 3.7.1 Action A 72 hour LCO completion time, and therefore, Action B requires the plant to be in MODE 3 within 12 hours and in MODE 4 in 36 hours. The TS 3.7.1 Action A 72 hour LCO completion time coincides with October 17, 2009, at 1747 hours. Currently, the plant is expected to be in MODE 3 at approximately 2300 hours on October 15, 2009. The NRC Resident Inspector has been notified. The State and Counties will also be notified.
ENS 4544016 October 2009 01:48:00PerryNRC Region 3GE-6On October 16, 2009 at 0048 a manual reactor scram was inserted at the Perry Nuclear Plant. The plant was conducting a planned shutdown due to the Division 2 Emergency Service Water inoperability. While shifting reactor recirculation pumps to slow speed the 'A' pump failed to transfer and tripped off. Following stabilization from this event a manual reactor scram was inserted from approximately 30% power. This was different from the initial planned shutdown sequence. Following the scram all systems operated as expected. The plant is stable in Mode 3. The plant will transition to Mode 4 in accordance with Technical Specification 3.7.1 (Emergency Service Water Inoperability) required actions. All control rods fully inserted and the plant electrical power is in a normal line-up. The licensee notified the NRC Resident Inspector.
ENS 4559125 December 2009 19:18:00PerryNRC Region 3GE-6

EMERGENCY RESPONSE DATA SYSTEM OUT OF SERVICE

On December 25, 2009, at approximately 1540 hours EST, the plant computer system (ICS) experienced a lockup due to a loss of electrical power to the meteorological tower. This resulted in a loss of most Emergency Response Data System (ERDS) information points, the Safety Parameter Display System (SPDS), and the automatic mode calculation of the Computer Aided Dose Assessment Program (CADAP). The Computer Aided Dose Assessment Program remained available in manual data entry mode.

At 1758 hours, the ICS computer system operation was restored to normal. All SPDS and ERDS information points are now functioning properly. Power restoration activities to the meteorological tower are in progress. This event is being reported in accordance with 10 CFR 50.72(b)(3)(xiii) as a condition that results in a major loss of emergency offsite communications capability. The NRC Resident Inspector has been notified."

ENS 4576815 March 2010 14:45:00PerryNRC Region 3GE-6On March 15, 2010, at approximately 0810 hours EDT, the plant computer system (ICS) was taken out of service for a planned outage to set the computer time to Eastern Daylight Time. During the time change adjustment, the ICS experienced a hard memory fault which required additional efforts to recover the ICS. At approximately 1205 hours EDT, the ICS was restored to normal operation. During the time ICS was out of service, the Safety Parameter Display System (SPDS), the Emergency Response Data System (ERDS), and the automatic mode calculation of the Computer Aided Dose Assessment Program (CADAP) were unavailable. This event is being reported in accordance with 10 CFR 50.72(b)(3)(xiii), as a condition that results in a major loss of offsite communications capability. The NRC Resident Inspector has been notified.
ENS 4579828 March 2010 22:13:00PerryNRC Region 3GE-6

At 1818 , the control room was notified of a lube oil fire on Reactor Feed Pump Turbine B. The fire brigade was toned out, and the Perry Township Fire Department was notified for assistance. Reactor Feed Pump Turbine B was manually tripped to allow removing the turbine lube oil system from service. The Motor Feed Pump started as expected, and the Reactor Recirculation system lowered reactor power as designed. Currently the reactor is at 68% reactor power following rod line adjustments after the transient was complete. The fire was reported to be out by the fire brigade leader at 2122. Damage assessment is currently in progress. Two fire brigade members were transported by ambulance to Tri-Point Medical Center with signs of heat exhaustion. Both individuals were verified to be free of contamination prior to transport. A news release will be made due to local media interest for this event. The NRC Resident Inspector has been notified.

  • * * UPDATE FROM CHARLES ELBERFELD TO DONALD NORWOOD AT 1636 EDT ON 3/29/2010 * * *

The purpose of this call is to update Event Number 45798. In the notification made on 3/28/10, it was stated that a news release would be made due to local media interest for this event. After further review, it was determined that discussions with the media adequately addressed the interest and that a new release will not be made. The NRC Resident Inspector has been notified. Notified R3DO (Duncan).

ENS 458156 April 2010 06:11:00PerryNRC Region 3GE-6

At 2145 (EDT) hours on April 5, 2010, a loss of electrical power to the Division 1 Loss of Coolant Accident (LOCA) initiation logic occurred. Control room annunciators for 'Residual Heat Removal (RHR) Out of Service', 'Reactor Core Isolation Cooling (RCIC) Out of Service', and 'RCIC/RHR D2 to D1 00 File Power Loss' were received. At 2250 hours, the Control Room staff determined a loss of isolation function existed. The operators entered Technical Specification (TS) action statements for Emergency Core Cooling System Instrumentation (TS 3.3.5.1), RCIC Instrumentation (TS 3.3.5.2), and Primary Containment and Drywell Isolation Instrumentation (TS 3.3.6.1). The power loss was caused by a blown fuse which occurred during surveillance testing. The surveillance test was suspended and plant personnel commenced troubleshooting and investigation efforts. A recovery plan is being developed to back out of the surveillance test and replace the fuse to re-energize the logic, while ensuring the plant does not experience an undesirable actuation of the logic. The power loss caused five containment isolation valves to lose automatic isolation function. These valves have no associated inboard automatic isolation valve powered by Division 2. As a result of the power loss, the valves cannot automatically close on demand to isolate and therefore cannot perform their automatic function to isolate the containment. This event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(C) as an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material. The NRC Resident Inspectors have been notified. The licensee entered a 12-hour shutdown action statement for the loss of containment isolation function as a result of the power failure.

* * * RETRACTION FROM LLOYD ZERR TO PETE SNYDER ON 6/4/2010 AT 1126 * * * 

On April 6, 2010, at 0611 hours, notification was made to NRC Operations Center of an event that at the time of discovery, could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material (10 CFR 50.72(b)(3)(v)(c)). A blown fuse during surveillance testing caused a loss of electrical power to the Division 1 Loss of Coolant Accident initiation logic. The power loss caused five containment isolation valves to lose their automatic isolation function. These valves have no associated inboard automatic isolation valve powered by Division 2. As a result of the power loss, the valves could not automatically close on demand and therefore, could not perform their automatic function to isolate containment. Following further evaluation, it was determined that a loss of safety function of structures or systems that are needed to control the release of radioactive material did not occur. Based on review of valve leak rate test history and compliance with 10 CFR 50, Appendix A, General Design Criteria, the penetrations and Containment were capable of performing their intended design function. The associated inboard valves and/or water seals were capable of automatically isolating containment. Additionally, all required Technical Specifications Limiting Conditions for Operation were complied with for the identified issue, and therefore, no operation or condition prohibited by the plant's Technical Specifications existed. Since the event or condition reported in Event Notification 45815 would not have prevented the fulfillment of the safety function needed to control the release of radioactive material, this event or condition is not reportable and the notification is retracted. Additionally, based on not meeting any 10 CFR 50.73 reporting criteria, no Licensee Event Report is required. The evaluation (i.e., Reportability Determination) for this event or condition is documented in Condition Report 10-74904. The NRC Resident Inspector has been notified. Notified the R3DO (Pelke).

Time of Discovery
ENS 4588029 April 2010 08:31:00PerryNRC Region 3GE-6

Beginning at approximately 0830 hours EDT on April 29, 2010, Perry Plant personnel will be taking the plant Integrated Computer System (ICS) out of service for planned maintenance. During the time ICS is out of service, the Safety Parameter Display System (SPDS), the Emergency Response Data System (ERDS), and the automatic mode calculation of the Computer Aided Dose Assessment Program (CADAP) will be unavailable. The computer outage is scheduled for six hours. In the event of an emergency, plant parameter data will be orally transmitted to the facilities through the Status Board Ring Down circuit with back-up by the Private Branch Exchange, Off-Premise Exchange, and various redundant intra-facility circuits throughout the emergency facilities. The dose assessment function will be maintained during the out of service time period by manual input of data into CADAP and, if required, by manual calculation. The ability to open and maintain an 'open line' using the Emergency Notification System will not be affected and will be the primary means of transferring plant data to the NRC as a contingency until the ERDS can be returned to service during the period of unavailability. This event is being reported in accordance with 10 CFR 50.72(b)(3)(xiii), as a condition that results in a major loss of offsite communications capability. A follow-up notification will be made when the maintenance activities are completed and the equipment is restored. The NRC Resident Inspector has been notified.

  • * * UPDATE AT 1036 EDT ON 04/29/10 FROM DOUGLAS SHORTER TO CHARLES TEAL * * *

The plant ICS has been returned to service and the system is functioning normally. The NRC Resident Inspector has been notified. Notified R3DO (Hills).

ENS 4591812 May 2010 03:12:00PerryNRC Region 3GE-6On May 11, 2010, at approximately 2318 hours, a manual Reactor Protection System (RPS) actuation was initiated as required by Technical Specification (TS) Limiting Condition for Operation (LCO) 3.1.5 'Control Rod Scram Accumulators.' Control Rod Drive (CRD) charging water header pressure was less than 1520 psig (i.e., no CRD pumps operating) and there were multiple accumulator faults on withdrawn control rods. At the time of the event, the plant was in Mode 1 at 100% power. All control rods are inserted into the core and the plant is currently stable, in Mode 3 (Hot Shutdown) with reactor pressure at approximately 930 psig. No Emergency Core Cooling Systems were required or utilized to respond to the event and there were no other 10 CFR 50.72 reportable actuations. Reactor coolant level is being maintained in its normal band by the feedwater system and decay heat is being removed by the condenser. The plant is in a normal electrical line-up with all three Emergency Diesel Generators operable and available if needed. The cause of the event initiator, an invalid Division 2 Loss of Coolant Accident (LOCA), i.e., High Drywell Pressure/Low Reactor Vessel Water Level, signal, is currently under investigation. Prior to the manual RPS Actuation, the invalid LOCA signal resulted in invalid actuations of Division 2 equipment and systems including, the Division 2 Emergency Diesel Generator (EDG), (which started but did not load onto the bus), Low Pressure Coolant Injection B and C subsystems (which started the pumps but did not inject into the vessel), discharge of the Suppression Pool Makeup subsystem B into the suppression pool, startup of the Control Room Emergency Recirculation subsystem B, and isolation of Group 2B Containment isolation valves which included the Nuclear Closed Cooling System Containment Return Isolation valve that was not already closed. The affected equipment is being restored in accordance with plant procedure. The NRC Resident Inspector has been notified. The licensee experienced an instrumentation rack loss of power which appears to have resulted in the inadvertent Division 2 initiation. The initiator of this event also and led to a loss of power to both control rod drive charging water header pumps resulting in charging water header pressure less than required and related accumulator faults which placed the licensee in a technical specification required shutdown condition. The action statement allows only 20 minutes to restore the condition which was insufficient time for the licensee to correct the condition so a manual scram was initiated from 100% power. The scram was characterized as an uncomplicated scram and all system responses (not related to the initial instrument fault) functioned as required.Reactor Vessel Water Level
ENS 4637028 October 2010 07:59:00PerryNRC Region 3GE-6

Beginning at approximately 0800 hours EDT on October 28, 2010, Perry Plant personnel will be taking the plant Integrated Computer System (ICS) out of service for planned maintenance. During the time ICS is out of service, the Safety Parameter Display System (SPDS), the Emergency Response Data System (ERDS), and the automatic mode calculation of the Computer Aided Dose Assessment Program (CADAP) will be unavailable. The computer outage is scheduled for six hours. In the event of an emergency, plant parameter data will be orally transmitted to the facilities through the Status Board Ring Down circuit with back-up (using) the Private Branch Exchange, Off-Premise Exchange, and various redundant intra-facility circuits throughout the emergency facilities. The dose assessment function will be maintained during the out of service time period by manual input of data into CADAP and, if required, by manual calculation. The ability to open and maintain an 'open line' using the Emergency Notification System will not be affected and will be the primary means of transferring plant data to the NRC as a contingency until the ERDS can be returned to service during the period of unavailability. This event is being reported in accordance with 10 CFR 50.72(b)(3)(xiii), as a condition that results in a major loss of offsite communications capability. A follow-up notification will be made when the maintenance activities are completed and the equipment is restored. The NRC Resident Inspector has been notified.

  • * * UPDATE AT 1301 EDT ON 10/28/10 FROM GLENDON BURNHAM TO DONG PARK * * *

At 1100 EDT, the plant ICS has been returned to service and functioning normally. The NRC Resident Inspector has been informed. Notified R3DO (Skokowski).

ENS 4637428 October 2010 20:25:00PerryNRC Region 3GE-6On October 28, 2010, at 1740 hours, the plant entered the Off-Normal Instruction for spills and unauthorized discharges. At 1751 hours, notification of a sodium hypochlorite spill was made to the U.S. Environmental Protection Agency (EPA), National Response Center. At the time of the event, the plant was in Mode 1 at 100% power. The sodium hypochlorite spill is believed to be the result of a leak in an underground piping supply line to the Emergency Service Water pump house. The leak is estimated to be approximately 130 gallons of a 12.5% Sodium Hypochlorite (Bleach) solution (80 gallons in a 24 hour period is the reportable quantity). The associated chlorination systems have been isolated, and current storage tank level is stable, indicating no more leakage in progress. Additionally, the Ohio EPA: State Emergency Response Commission, Perry Township Fire Department, Lake County Emergency Planning Committee, and the U.S. Coast Guard were notified in accordance with plant procedures. This event is also being reported in accordance with the Operating License, Appendix B, Environment Protection Plan, which states in part, 'Any occurrence of an unusual or important event that indicates or could result in significant environmental impact causally related to plant operation shall be recorded and reported to the NRC within 24 hours followed by a written report ..' Specifically, ' ..unanticipated or emergency discharge of waste water or chemical substances.' The NRC Resident Inspector has been notified.
ENS 4680329 April 2011 13:29:00PerryNRC Region 3GE-6On April 29, 2011, at approximately 1100 hours, a contract employee was found unresponsive in a vehicle, off the road, inside the Perry Nuclear Power Plant owner controlled area. At 1120 hours, it was confirmed by the Perry Fire Department that the individual was deceased. Notification has been made to the Lake County Sheriffs department and the Lake County Coroner. The death does not appear to be work related or the result of an accident. A preliminary diagnosis by the coroner is the individual suffered a heart attack. The Lake County Coroner is conducting a routine investigation into the death. A press release is not planned at this time. The individuals name has not yet been released pending notification of next-of-kin. A notification to OSHA per 29CFR1904.39 will be made for this event. The plant is currently in MODE 5 (Refuel) for a refueling outage. This event is being reported in accordance with 10 CFR 50.72(b)(2)(xi) as an event or situation, related to the health and safety of the public or on-site personnel, for which notification to other government agencies has been or will be made. Such an event may include an on-site fatality. The NRC Senior Resident Inspector has been notified.Fatality
ENS 4697420 June 2011 17:10:00PerryNRC Region 3GE-6On June 20, 2011, at approximately 0945 hours, electrical power was lost to non-essential 120 volt busses V-1-F and V-2-F. The busses supply electrical power to the plant integrated computer system (ICS). As a result of the power loss, the Safety Parameter Display System (SPDS), the Emergency Response Data System (ERDS), and the automatic mode calculation of the Computer Aided Dose Assessment Program (CADAP) were unavailable. Preliminary investigation indicates the power loss was caused by receipt of a spurious high temperature alarm (greater than 95 degrees F) in the Technical Support Center (TSC) facility where the electrical busses are located. The alarm signal is believed to be invalid because the high temperature alarm came in for two minutes and reset, and the ambient temperature in the TSC remained steady at 65 degrees F. Electrical busses V-1-F and V-2-F were re-energized and restored to service at 1505 hours. The ICS, SPDS, ERDS, and CADAP systems were fully restored at 1652 hours on June 20, 2011. In the event of an emergency while these systems were unavailable, contingency plans were in place to transmit plant parameter data and perform the dose assessment function. This event is being reported in accordance with 10 CFR 50.72(b)(3)(xiii), as a condition that results in a major loss of emergency assessment and communications capability. The NRC Resident Inspector has been notified.
ENS 470245 July 2011 20:35:00PerryNRC Region 3GE-6On July 5, 2011, at 1815 hours, it was determined that a design deficiency at the Perry Nuclear Power Plant (PNPP) constituted a fire protection program concern which could adversely affect the ability to achieve and maintain safe shutdown of the plant in the event of a control room fire. (Reference event notification numbers 46811 and 46997). In the event of a postulated control room fire, the potential exists that two 4160 VAC breakers could trip open under a hot-short condition. PNPP's Appendix R design vulnerability only affects Breakers EH1106, which supplies the Emergency Service Water Pump A and EH1107, which supplies the Control Complex Chiller A. Specifically, the current transformers used in these breakers for the 50/51 instantaneous and time over current protective relays are in line with the component control room ammeters. Therefore, a hot-short-to-ground in the associated control room ammeters could actuate the 50/51 relays and trip the component breaker. Actions are in progress to isolate the control room ammeters for the Emergency Service Water Pump A in breaker EH1106 and the Control Complex Chiller A in breaker EH1107. Isolating these ammeters would isolate the affected circuitry from the described Appendix R failure mechanism. Control room amperage indication for the pump and chiller would be lost while this Temporary Modification is installed. PNPP will pursue a permanent resolution to the hot-short-to-ground fault for the EH1106 and EH1107 breakers. This event is being reported in accordance with 10 CFR 50.72(b)(3)(ii)(B), as a condition that results in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety. A follow-up licensee event report will be made in 60 days. The resident inspector has been notified.Safe Shutdown
Unanalyzed Condition
Temporary Modification
Fire Protection Program
ENS 473122 October 2011 01:06:00PerryNRC Region 3GE-6This event is being reported in accordance with 10CFR50.72(b)(2)(i). On October 2, 2011, at approximately 0100 hours (EDT), the Perry Nuclear Power Plant commenced a controlled plant shutdown. The shutdown was due to the anticipated investigation and expected repair time of the Unit 1 startup transformer exceeding the Technical Specification (TS) Required Action completion time. On September 29, 2011, at 0529 hours (EDT) the Unit 1 startup transformer failed due to an internal fault, which required entry into TS 3.8.1 Action A.2 for one required offsite circuit inoperable. The determination has been made that the required action, which is to restore the required offsite circuit to OPERABLE status, cannot be met by the required completion time and a plant shutdown is being initiated. The NRC Resident Inspector has been notified. The licensee expects to have the Unit offline between 1300-1400 hours (EDT) and plans to issue a press release.Offsite Circuit
ENS 4736621 October 2011 20:25:00PerryNRC Region 3GE-6This event is being reported in accordance with 10CFR50.72(b)(2)(xi). On October 21, 2011, at approximately 1723 hours EDT, notification of a fuel oil spill was made to the US Environmental Protection Agency (EPA), National Response Center. At the time of the event, the plant was in Mode 1 at 100 percent rated thermal power. The fuel oil spill was caused by a leak in an underground pipe outside the protected area, but inside the owner controlled area. The spill is estimated between 1000 to 1500 gallons and is contained onsite. However, a certified wetlands specialist was contacted and determined the area met the criteria for wetlands designation, which in turn made the event reportable. Clean Harbors Incorporated is assisting with the onsite clean-up and remediation. Additionally, the Ohio EPA: State Emergency Response Commission, Perry Township Fire Department, Lake County Emergency Planning Committee, and the U.S. Coast Guard were notified in accordance with plant procedures. This event is also being reported in accordance with the plant's Operating License, Appendix B, Environmental Protection Plan, which states, in part, that any occurrence of an unusual or important event that indicates or could result in significant environmental impact causally related to plant operation shall be recorded and reported to the NRC within 24 hours followed by a written report. The licensee notified the NRC Resident Inspector.
ENS 475087 December 2011 18:29:00PerryNRC Region 3GE-6

On November 16, 2011, at 2000 hours (EST), control room operators accepted the results of an immediate investigation related to the adequacy of a calculation related to the flooding analysis for service water piping in the control complex. The conclusions of the original analysis assumed operator actions to mitigate the flooding. The existing procedural guidance at that time lacked specificity for the required operator actions. This was identified as a non-conforming condition with respect to a USAR flooding analysis. The immediate investigation determined that significant margin exists for mitigation of the service water leakage crack compared to the 30 minute actions required in the original analysis. A preliminary strategy for flood mitigation was identified in the immediate investigation. Guidance was provided to the operators for a leak mitigation strategy in a night order, and a prompt functionality assessment was requested for the control complex building with respect to the flooding analysis. On November 22, 2011, at 1957 hours (EST), the prompt functionality assessment was accepted by the control room operators. The assessment included compensatory measures that simplified guidance for mitigating the flooding from the service water system. The compensatory measures were implemented. On December 2, 2011, the NRC Component Design Basis Inspection team debriefed that the condition identified should have been called in to the NRC Operations Center within eight hours and that missing the call was a violation of 10 CFR 50.72(b)(3)(ii)(B). On December 7, 2011, at 1320 hours (EST), a call was received from the NRC Region III informing the compliance supervisor that the eight-hour notification should still be made. The NRC Resident Inspector has been notified.

  • * * UPDATE FROM CHARLES ELBERFELD TO JOHN KNOKE AT 1412 EST ON 12/10/11 * * *

The licensee added further clarification to the event reported above as follows: Given that an unanalyzed condition existed until the appropriate measures were implemented, an eight-hour call in accordance with the aforementioned section of 10 CFR 50.72 should have been made. After further consideration, station management decided the eight-hour call was missed and it is being reported as required. The NRC Resident Inspector has been notified." R3DO (Skokowski) notified.

Unanalyzed Condition
Functionality Assessment
ENS 475159 December 2011 22:41:00PerryNRC Region 3GE-6

On December 7, 2011, a 10 CFR 21 report (reference NRC EN No. 47498) was received from a vendor for a defect with NUS Controllers. The defect involves spring clips that form part of the seismic restraints for the controllers. The controllers referenced in the report are installed for the Reactor Core Isolation Cooling (RCIC) system in the control room and remote shutdown panel. Based on initial information provided by the vendor, it was determined that the RCIC system remained operable. On December 9, 2011, additional information provided by the vendor did not support the immediate operability determination and the RCIC system was declared inoperable for Technical Specification (TS) Limiting Condition for Operation (LCO) 3.5.3 Condition A at 1835 hours (EST). At 1932 hours (EST), the High Pressure Core Spray system was verified operable per TS LCO 3.5.3 Required Action A.1. TS LCO 3.5.3 Required Action A2 requires restoration of the RCIC system to operable status within 14 days. Qualified spring clips have been obtained and will be installed on the controllers. This condition is being reported in accordance with 10 CFR 50.72(b)(3)(v)(B) as a condition that at the time of discovery could have prevented the fulfillment of the safety function of a system needed to remove residual heat. The NRC Resident Inspector has been notified.

  • * * UPDATE FROM CHARLES ELBERFELD TO JOHN KNOKE AT 1415 EST ON 12/10/11 * * *

As a follow-up to the condition reported above, we have replaced the affected seismic clips on the controllers and the Reactor Core Isolation Cooling system is now operable as of 0734 on December 10, 2011. The NRC Resident Inspector has been notified." R3DO (Skokowski) notified.

  • * * RETRACTION FROM LLOYD ZERR TO CHARLES TEAL ON 2/6/12 AT 1504 EST * * *

The vendor provided a seismic report to the station. This report showed that the seismic clips holding the Reactor Core Isolation Cooling (RCIC) controller meet the Operating Basis Earthquake (OBE) test requirements and design requirements for a Safe Shutdown Earthquake (SSE) for Perry. Based on this review, it was determined that the spring clips would function properly during and OBE and SSE. Because the condition reported in Event Number 47515 would not have prevented the fulfillment of the safety function of a system needed to remove residual heat, the condition is not reportable, and this notification is being retracted. The evaluation for this condition is documented in condition report 2011-06531. The NRC Resident Inspector has been informed." Notified R3DO (Giessner) and Part 21 Group via email.

Time of Discovery
Safe Shutdown Earthquake
Operating Basis Earthquake
Operability Determination
ENS 4754521 December 2011 21:37:00PerryNRC Region 3GE-6

On December 21, 2011, at 1359 hours EST, it was determined that the test instruction for the weekly groundwater level readings contained non-conservative acceptance criteria. The test instruction acceptance criteria for groundwater level exceeds the initial assumptions used in the Updated Safety Analysis Report (USAR) Chapter 15 accident analysis for 'Postulated Radioactive Releases due to Liquid Containing Tank Failures.' The issue was identified during the conduct of a prompt functionality assessment evaluating the plant underdrain system performance and to ensure all USAR described functions were being met. The test instruction acceptance criteria is less than 575 feet. The calculation supporting the Chapter 15 accident analysis assumes an initial groundwater elevation of 568 feet in order to accumulate a sufficient volume of groundwater to dilute the tank inventory prior to exiting the underdrain system. The accumulation volume results in hold up time allowing for mixing and radioactive decay. With the degraded performance of the underdrain system pumps and high precipitation, the groundwater level had risen above 568 feet but was still less than 575 feet. A preliminary engineering evaluation has determined that significant margin exists in the calculation. A calculation revision is being pursued in parallel with this notification. Compensatory actions involving the repair of 1 permanent non-safety pump and installation of temporary pumps were previously initiated and the groundwater levels are decreasing. Restoration of the remaining permanent plant pumps continues. The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 2/15/12 AT 1315 EST FROM LLOYD ZERR TO ERIC SIMPSON * * *

The calculation supporting the USAR Chapter 15 accident analysis was reviewed and subsequently revised. The revised calculation verifies and initial groundwater elevation of 575 feet is consistent with the preliminary assessment that substantial margin existed in the calculation for the underdrain system. Because the condition reported in Event Number 47545 was not an event or condition that results in the nuclear power plant being in an unanalyzed condition that degrades safety, the condition is not reportable, and this notification is retracted. The evaluation for this condition is documented in condition report 2011-07169. The NRC Resident Inspector and R3DO (Passehl) were notified.

Unanalyzed Condition
Functionality Assessment
ENS 477101 March 2012 05:51:00PerryNRC Region 3GE-6On March 1,2012, at approximately 0224 (EST), a manual Reactor Protection System (RPS) actuation was initiated due to 3 turbine bypass valves going open as a result of an automatic turbine runback signal. At the time of the event, the plant was in Mode 1 at 100% power. All control rods are inserted into the core and the plant is currently stable in Mode 3 (Hot Shutdown) with reactor pressure at approximately 930 psig. No Emergency Core Cooling Systems were required or utilized to respond to the event and there were no other reportable actuations. Reactor coolant level is being maintained in its normal band by the feedwater system and decay heat is being removed by the condenser. The plant is in a normal electrical line-up with all three Emergency Diesel Generators operable and available if needed. The cause of the automatic turbine runback has not been determined and is being investigated. During the transient, Reactor Water Cleanup System (RWCU) tripped. No automatic isolation signal was received. At the time of the event, restoration of a Stator Water Cooling pressure gauge was being performed (following maintenance). The NRC Resident Inspector has been notified.
ENS 479016 May 2012 20:53:00PerryNRC Region 3GE-6This event is being reported in accordance with 10 CFR 50.72(b)(2)(xi). On May 6, 2012, during daily chlorination activities, it was identified that the National Pollutant Discharge Elimination System (NPDES) permit limit for Total Residual Chlorine was exceeded between approximately 0935 hours (EDT) and 0947 hours (EDT) when the noncompliance was corrected. The maximum measured value was 0.29 mg/L, which exceeded the NPDES Maximum Concentration Limit of 0.2 mg/L. On May 6, 2012, at approximately 1930 hours (EDT), a 'Noncompliance Notification for Exceedance of a Daily Maximum Discharge Limit' was made to the Ohio Environmental Protection Agency. The cause of the NPDES permit noncompliance is under investigation. Chlorination evolutions have been suspended pending investigation results. At the time of the event, the plant was in Mode 1 at 100 percent rated thermal power. This event is also being reported in accordance with the plant's operating license, appendix B, Environmental Protection Plan, which states, in part, that any occurrence of an unusual or important event that indicates or could result in environmental impact causally related to plant operation shall be recorded and reported to the NRC within 24 hours followed by a written report. The licensee notified the NRC Resident Inspector.
ENS 479027 May 2012 16:16:00PerryNRC Region 3GE-6This event is being reported in accordance with 10 CFR 50.72(b)(2)(xi). On May 7, 2012, at approximately 1233 hours (EDT), an inadvertent actuation of the Perry Nuclear Power Plant's alert notification system occurred. Twenty of the seventy-six total sirens sounded for three minutes affecting Ashtabula, Geauga, and Lake Counties. Following the actuation the county agencies received calls from members of the public. A successful quiet test of the sirens had been conducted earlier in the day (at approximately 0830 hours (EDT)). At this time, all sirens are functioning correctly. The siren actuation was not related to any condition or event at the Perry Nuclear Power Plant. The actuation signal originated from the Lake County Emergency Operations Center while thunderstorms were passing through the area. Additional investigation is in progress to determine the cause of the inadvertent actuation. At the time of the event, the plant was in Mode 1 at 100 percent rated thermal power. Lake County officials plant to issue a press release. The NRC Resident Inspector has been notified.Siren
ENS 4791310 May 2012 10:29:00PerryNRC Region 3GE-6

Beginning at approximately 1100 hours EDT on May 10, 2012, plant personnel will be taking the plant integrated computer system (ICS) out-of-service for planned maintenance. During the time ICS is out-of-service, the Safety Parameter Display System (SPDS), the Emergency Response Data System (ERDS), and the automatic mode calculation of the Computer Aided Dose Assessment Program (CADAP) will be unavailable. The computer outage is scheduled for two hours. In the event of an emergency, plant parameter data will be orally transmitted to the facilities through the Status Board Ring Down circuit with back-up by the Private Branch Exchange, Off Premise Exchange, and various redundant intrafacility circuits throughout the emergency facilities. The dose assessment function will be maintained during the out-of-service time period by manual input of data into CADAP and, if required, by manual calculation. The ability to open and maintain an 'open line' using the Emergency Notification System will not be affected and will be the primary means of transferring plant data to the NRC as a contingency until the ERDS can be returned to service. This event is being reported in accordance with 10 CFR 50.72(b)(3)(xiii). A follow-up notification will be made when the maintenance activities are completed and the equipment is restored. The NRC Resident Inspector has been notified.

  • * * UPDATE AT 1245 EDT ON 5/10/12 FROM MORSE TO HUFFMAN * * *

The maintenance activities were completed as scheduled and the integrated computer system and associated systems SPDS, ERDS and CADAP has been returned to service as of 1238 EDT. The licensee will notify the NRC Resident Inspector. R3DO (Giessner) notified.

ENS 4801311 June 2012 14:41:00PerryNRC Region 3GE-6On June 11, 2012, at 0845 hours, an unexpected Division 3 battery DC system trouble alarm was received in the control room along with indication of lowering battery voltage. As a result of this condition, the plant operators declared the Division 3 DC electrical power subsystem inoperable at 0852 hours and entered the applicable Technical Specifications which require the High Pressure Core Spray System (HPCS) be declared inoperable. HPCS is a single-train safety system and its inoperable status is considered a loss of safety function. The cause of the trouble alarm was failure of the normal battery charger. Following a walkdown inspection of the Division 3 DC electrical bus with no abnormalities noted, the reserve charger was placed in service at 0858 hours to supply the bus. At 1245 hours, the HPCS system was declared operable following restoration of the Division 3 DC electrical power subsystem to operable status. This event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D). The NRC Resident Inspector has been notified.
ENS 480693 July 2012 20:35:00PerryNRC Region 3GE-6This event is being reported in accordance with 10CFR50.72(b)(2)(xi). On July 3, 2012, at approximately 1738 hours, an inadvertent actuation of the Perry Nuclear Power Plant's (PNPP) alert notification system occurred. Seventy-five of seventy-six sirens sounded for three minutes, affecting Ashtabula, Geauga, and Lake Counties. Following the actuation, county agencies received calls from members of the public. PNPP's capability to notify the public in an emergency has been retained. The siren actuation was not related to any condition or event at the PNPP. An investigation is in progress to determine the cause of the inadvertent actuation. At the time of the event, the plant was in Mode 1 at 100 percent rated thermal power. The public was informed of the inadvertent actuation by way of the Emergency Alert System (EAS). The NRC Resident Inspector has been notified. The licensee has notified State and Local agencies.Siren
ENS 4831918 September 2012 12:58:00PerryNRC Region 3GE-6On July 23, 2012, at 2057 hours, the Perry Nuclear Power Plant experienced a loss of the normal power supply to the Reactor Protection System (RPS) A electrical bus. The loss of RPS bus A caused an actuation of several Division 1 containment outboard isolation valves. The actuation signal caused full closure of one or more valves in each of the following Division 1 subsystems: Main Steam line drains, Containment Radiation Monitor, Drywell Radiation Monitor, Reactor Water Cleanup, Fuel Pool Cooling and Cleanup, Liquid Radwaste Sumps, Containment Vessel Chilled Water, Containment Vacuum Relief, Condensate Transfer and Storage, Mixed Bed Demineralizer and Distribution, Containment Personnel Airlocks, Service Air, and Instrument Air. Division 2 components and valves were not affected. This event is considered an invalid system actuation reportable under 10 CFR 50.73(a)(2)(iv)(A). The isolation was not initiated in response to actual plant conditions or parameters, and was not a manual initiation. Therefore, this notification is provided via a 60 day optional phone call in accordance with 10 CFR 50.73(a)(1) instead of submitting a written Licensee Event Report. The event meets reporting criteria specified in 10 CFR 50.73(a)(2)(iv)(B)(2) as a general containment isolation valve signal affecting containment isolation valves in more than one system. All affected systems functioned as expected in response to an outboard isolation signal. The valves were reopened in accordance with plant procedures. The failure mechanism that caused the loss of RPS bus A was a degraded voltage regulator. The voltage regulator was replaced and retested with satisfactory results. The NRC Resident Inspector has been notified.
ENS 4841517 October 2012 07:40:00PerryNRC Region 3GE-6

At approximately 0800 hours EDT on October 17, 2012, computer engineering personnel will be taking the plant integrated computer system (ICS) out-of-service for planned maintenance. During the time ICS is out-of-service, the Safety Parameter Display System (SPDS) and the Emergency Response Data System (ERDS) will be unavailable. The computer outage is scheduled for twelve hours. In the event of an emergency, plant parameter data will be communicated to the facilities through the Status Board Ring Down circuit with back-up by the Private Branch Exchange, Off Premise Exchange, and various redundant intra-facility circuits throughout the emergency facilities. The dose assessment function will be maintained during the out-of-service time period by manual input of data into the Meteorological Information and Dose Assessment System (MIDAS). The ability to open and maintain an 'open line' using the Emergency Notification System will not be affected and will be the primary means of transferring plant data to the NRC as a contingency until the ERDS can be returned to service. This event is being reported in accordance with 10 CFR 50.72(b)(3)(xiii). A follow-up notification will be made when the maintenance activities are complete and the equipment is restored. The (NRC) Resident Inspector has been notified.

  • * * UPDATE FROM THOMAS MORSE TO VINCE KLCO ON 10/17/12 AT 2146 EDT * * *

As of 2140 EDT on 10/17/12, the ERDS system was tested and restored to service. The licensee notified the NRC Resident Inspector. Notified the R3DO (Orth).

ENS 4844928 October 2012 16:27:00PerryNRC Region 3GE-6At approximately 1008 EDT on October 28th, 2012, a failure between the Plant Computer and the MMI (Man Machine Interface) occurred. The cause is due to a failure of the data diode. The Plant Computer is still working however the MMI is not, therefore Safety Parameter Display System (SPDS) outside of the Control Room and the Emergency Response Data System (ERDS) is unavailable. In the event of an emergency, plant parameter data will be communicated to the facilities through the status board ring down circuit with back-up by the Private Branch Exchange (PBX), Off Premise Exchange (OPX), and various redundant intra-facility circuits throughout the emergency facilities. The dose assessment function is maintained during this out of service time period by manual input of data into the Meteorological Information and Dose Assessment System (MIDAS). The ability to open and maintain an 'open line' using the Emergency Notification System is not affected and will be the primary means for transferring plant data to the NRC as a contingency until the ERDS can be returned to service. At 1548 EDT on October 28th, 2012, a re-start of the data diode was successful in restoring the connection between the Plant Computer and the MMI. SPDS and the ERDS are functioning as designed. This event is being reported in accordance with 10 CFR 50.72(b)(3)(xiii). The NRC Resident Inspector has been notified. The licensee has notified the State and local agencies.
ENS 4854228 November 2012 10:50:00PerryNRC Region 3GE-6

Entered an Unusual Event (under Emergency Action Level) MU1, toxic gas, carbon monoxide (CO), detected in the Radwaste Control Room. Levels rose to 34 ppm and the Radwaste Control Room was evacuated prior to reaching the First Energy exposure limit of 35 ppm. The source of the CO has not been determined. There is no radiation release from this event. There were no personnel injuries and offsite assistance was not requested. There was no effect on plant operations. The licensee has notified state and local authorities and the NRC Resident Inspector. Notified DHS SWO, FEMA, DHS NICC and NuclearSSA via email.

  • * * UPDATE AT 1504 EST ON 11/28/12 FROM MARIKIO BLOUNT TO HUFFMAN * * *
(At 1452 EST, the licensee) terminated the Unusual Event for MU1, due to toxic gas - carbon monoxide, detected in the Radwaste Control Room.  The source of the carbon monoxide readings was determined to be from a leaking acetylene bottle.  The acetylene bottle has been removed from the building.  Carbon monoxide readings have returned to normal.

The licensee noted that the acetylene is detected as carbon monoxide by the toxic gas monitoring devices. The licensee has notified State and local authorities and the NRC Resident Inspector. Notified R3DO (Stone), NRR (EO) Lubinski) , IRD (Marshall), DHS SWO, FEMA, DHS NICC and NuclearSSA via email.

ENS 4854428 November 2012 19:47:00PerryNRC Region 3GE-6At 1930 (EST) on November 28, 2012, it was determined that a Notification of Unusual Event (NOUE) was not declared for an event that occurred on June 3, 2012, when an equipment failure resulted in a deposit of ion exchange resin onto the floor of the Radioactive Waste building. Subsequent radiological surveys indicated that conditions met the requirements for a NOUE in accordance with the Perry Nuclear Power Plant Emergency Plan. This report is being provided within one hour of the recognition of the undeclared event. As discussed in NUREG 1022, Revision 2, an actual declaration of an Unusual Event is not necessary. The Initiating Conditions for the emergency classification no longer existed at the time of recognition. The NRC Resident Inspector has been notified.
ENS 4861020 December 2012 07:51:00PerryNRC Region 3GE-6

Computer engineering personnel will be taking the plant integrated computer system (ICS) out-of-service for planned maintenance. During the time ICS is out-of-service, the Safety Parameter Display System (SPDS) and the Emergency Response Data System (ERDS) will be unavailable. The computer outage is scheduled for six hours. Contingency plans have been established to transmit plant parameter data and perform the dose assessment function in the event of an emergency while ERDS is unavailable. This event is being reported in accordance with 10 CFR 50.72(b)(3)(xiii). A follow-up notification will be made when the maintenance activities are complete and the equipment is restored. The licensee notified the NRC Resident Inspector.

  • * * UPDATE FROM JIM CASE TO HOWIE CROUCH AT 1309 EST ON 12/20/12 * * *

At 1300 EST, the plant integrated computer system was restored and SPDS and ERDS was returned to service. Notified R3DO (Cameron) and ERDS Group email.

ENS 4868822 January 2013 06:57:00PerryNRC Region 3GE-6On January 22, 2013, at approximately 0332 hours (EDT), an automatic Reactor Protection System (RPS) actuation occurred at the Perry Nuclear Power Plant, Unit 1. At the time of the event, the plant was in Mode 1 at 100% power. All control rods are inserted into the reactor core and the plant is currently stable in Mode 3 (Hot Shutdown) with reactor pressure and level being maintained in the normal shutdown range. The RPS actuation was initiated by a low reactor water level (Level 3 - 178") signal. In response to the RPS actuation and subsequent reactor Level 2 (130") signal, the High Pressure Core Spray (HPCS) system and Reactor Core Isolation Cooling (RCIC) system both actuated and injected to maintain reactor coolant level. The reactor level is currently being maintained in its normal band by the feedwater system and decay heat is being removed by (turbine bypass valves to) the condenser (both HPCS and RCIC have been returned to standby). The plant is in a normal electrical line-up with all three Emergency Diesel Generators operable and available, if needed. The Containment Isolation Valves (responded to the Level 2 and 3) isolation signals as designed. The cause of the RPS actuation is under investigation. The NRC Resident Inspector has been notified.
ENS 4870831 January 2013 09:28:00PerryNRC Region 3GE-6On January 31, 2013, at approximately 0210 hours (EST), the ability to transfer plant parameter data via the Emergency Response Data System (ERDS) was lost. ERDS capability was restored at 0701 hours (EST). The cause is under investigation. In the event of an emergency while ERDS was unavailable, contingency plans were in place to transmit plant parameter data, This event is being reported in accordance with 10 CFR 50.72(b)(3)(xiii), The NRC Resident Inspector has been notified.
ENS 4876919 February 2013 16:39:00PerryNRC Region 3GE-6

On February 19, 2013, at approximately 1303 EST, the control room was notified that a supplemental worker (i.e., a contract individual) had fallen and was injured. The worker was in a contaminated area. Due to the individual's condition, the individual was not surveyed by a Health Physics technician prior to being transported in their anti-contamination clothing. The individual was transported by ambulance accompanied by Health Physics personnel to the local hospital for medical treatment (i.e., TriPoint Medical Center). Subsequently, the worker was declared deceased at the hospital. This notification is being made in accordance with 10 CFR 50.72(b)(3)(xii) and 50.72(b)(2)(xi). Additionally, OSHA was notified pursuant to the requirements of 29 CFR 1904.39. The Lake County Coroner was also notified. Subsequent surveys found no contamination on the worker, hospital, medical personnel, or ambulance. No press release is planned. The NRC Resident Inspector has been notified.

* * * UPDATE ON 3/21/13 AT 2032 EDT FROM LLOYD ZERR TO PETE SNYDER * * *

The Lake County Coroner has determined that the individual died of natural causes. The NRC Resident Inspector has been notified. Notified R3DO (Passehl).

Fatality
ENS 488947 April 2013 17:47:00PerryNRC Region 3GE-6During an extent of condition review of past radiological events, it was identified that an event on November 17, 2010 met the E-Plan entry criteria for GU1, 'Unexpected Increase In Plant Radiation Levels'. Due to an equipment deficiency, dose rates in one section of the Radwaste building rose from 0.08 mrem/hr to 80 mrem/hr. This satisfied the E-Plan criteria of a 1000 times change over normal radiation levels. This was initially identified in (Perry) Condition Report 2010-85937. The licensee notified the NRC Resident Inspector and will notify State and local authorities.
ENS 4893717 April 2013 05:20:00PerryNRC Region 3GE-6

The Perry Nuclear Power Plant is reporting an event or condition pursuant to 10 CFR 50.72(b)(3)(v)(D). On April 16, 2013, at 2323 EDT, it was identified that Emergency Service Water (ESW) pump 'A' was inoperable due to an inability to maintain minimum flow requirements. As a result, ESW 'A' and the supported Division 1 Emergency Diesel Generator (EDG) were declared inoperable. Coincident with this discovery, a test of the Division 2 emergency systems was in progress with the associated ESW 'B' pump and Division 2 EDG inoperable. Division 2 EDG was available to support the Shutdown Defense In-Depth Strategy. Division 3 EDG was operable and could supply High Pressure Core Spray system injection, if needed. Both EDGs were inoperable simultaneously and Technical Specification 3.8.2 'AC Sources-Shutdown' was entered and required actions taken. These actions included immediately suspending core alterations and immediately initiating actions to restore the required EDG. The test of Division 2 emergency systems was suspended and ESW 'B' and the Division 2 EDG were restored to operable status at 0135 EDT on April 17, 2013. The failure of ESW 'A' minimum flow is currently under investigation. The Resident Inspector has been notified.

  • * * RETRACTION FROM JOHN PELCIC TO CHARLES TEAL ON 4/20/13 AT 1355 EDT * * *

Engineering personnel performed an immediate investigation of the ESW 'A' minimum flow condition. The investigation results showed that the ESW 'A' pump flow exceeded the minimum flow requirement to protect the ESW 'A' system. Therefore, continued operation of ESW 'A' was acceptable and the minimum flow condition originally reported did not cause the Division 1 Emergency Diesel Generator to be inoperable. The condition would not have prevented the fulfillment of a safety function to mitigate the consequences of an accident. Reporting is not required under 10 CFR 50.72(b)(3)(v)(D) and this notification is retracted. The NRC Resident Inspector has been notified. Notified R3DO (Orth).

ENS 4912116 June 2013 02:42:00PerryNRC Region 3GE-6This event is being reported in accordance with 10 CFR 50.72(b)(2)(i) and 50.72(b)(3)(ii)(A). On June 16, 2013 at 0200 EDT, the Perry Nuclear Power Plant commenced a controlled plant shutdown. The shutdown was due to a small leak through the base of a vent line on the 'B' Reactor Recirculation Flow Control Valve. On June 15, 2013 at 2250 EDT, the leak was identified and was subsequently determined to require a plant shutdown in accordance with Technical Specification 3.4.5, Action (C) which requires the plant to be in Mode 3 within 12 hours. The NRC Resident Inspector has been notified." The licensee will also be notifying state and local authorities. The licensee had come down in power to make a drywell entry and investigate drywell leakage indications. Steam was observed to be coming from a vent line that comes off the top of the recirc flow control valve. The licensee was unable to characterize the leak rate other than a small leak. The licensee stated that the steam appeared be coming from a weld location where the vent line comes out of the flow control valve which would classify it as pressure boundary leakage.Pressure Boundary Leakage
ENS 4944617 October 2013 16:25:00PerryNRC Region 3GE-6A review of industry operating experience regarding the impact of unfused Direct Current (DC) ammeter circuits in the control room has determined the described condition to be applicable to the Perry Nuclear Power Plant resulting in a potentially unanalyzed condition with respect to 10 CFR 50 Appendix R analysis requirements. The original plant wiring design and associated analysis for the Class 1 E batteries control room ampere indications do not include overcurrent protection features to limit the fault current. In the postulated event, a fire in the control room could cause one of the ammeter wires to hot short to the ground plane. Simultaneously, it is postulated that the fire causes another DC wire from the opposite polarity on the same battery to also hot short to the ground plane. This could cause a ground loop through the unprotected ammeter wiring. This event could result in excessive current flow (i.e., heating) in the ammeter wiring to the point of causing a secondary fire in the raceway system. The secondary fire could adversely affect safe shutdown equipment and potentially cause the loss of the ability to conduct a safe shutdown as required by 10 CFR 50 Appendix R. This condition is being reported in accordance with 10 CFR 50.72(b)(3)(ii)(B). Interim compensatory measures (i.e., fire watches) have been implemented for affected areas of the plant. The licensee has notified the NRC Resident Inspector. See the following related Event Numbers: 49411, 49419, 49422, and 49444.Hot Short
Safe Shutdown
Unanalyzed Condition
ENS 4974621 January 2014 02:19:00PerryNRC Region 3GE-6This notification is being made pursuant to (10 CFR) 50.72(b)(2)(xi), notification of other government agency. Notification to other government agency, State of Ohio, was made at 0140 (EST) on 1/21/14. At 1310 on 1/20/2014, a leak was identified on a feed water Venturi. In response to the water leak, samples were taken to check for the spread of tritium. A positive result for tritium was identified in the under drain system in the Auxiliary Building which requires communications as part of the NEI ground water protection initiative. The positive sample results were obtained at 2330 on 1/20/14. Actions are in progress stop the leak (perform leak injection). The EPA limit for groundwater is 20,000 pCi/l. The samples taken by the licensee indicated 46,000 pCi/l. The licensee has notified the NRC Resident Inspector and will notify local counties.
ENS 498047 February 2014 08:19:00PerryNRC Region 3GE-6

This event is being reported in accordance with 10CFR 50.72(b)(2)(i), 'Initiation of a Shutdown Required by Technical Specifications.' At 2043 hours (EST) on February 06, 2014, the Perry Nuclear Power Plant entered Technical Specification 3.6.1.3 Primary Containment Isolation Valves (PCIVs), action C.1, due to leakage identified during local leak rate testing of the containment penetration for the Containment and Drywell Purge system. Leakage was identified on the outboard containment isolation valve resulting in the plant exceeding the limit for secondary containment bypass leakage. The Containment and Drywell Purge system penetration is normally isolated and remains isolated in accordance with Technical Specifications. Action C.1 requires restoration of the leakage rate within four hours. At 0043 hours on February 7, 2014, the plant entered Technical Specification 3.6.1.3, 'Primary Containment Isolation Valves (PCIVs)', action E as the leakage rate was not restored. Action E requires the plant be in Mode 3 in 12 hours and Mode 4 in 36 hours. At 0600 hours on February 07, 2014, the Perry Nuclear Power Plant initiated a shutdown in accordance with Technical Specification 3.6.1.3, action E. Repairs to restore the penetration leakage to within allowable limits are in progress. The NRC Resident Inspector has been notified.

  • * * UPDATE PROVIDED BY DAVE ODONNELL TO JEFF ROTTON AT 1220 EST ON 02/07/2014 * * *

At 0943 hours (EST) the reactor shutdown to comply with Technical Specification 3.6.1.3 action E was terminated (with the reactor at 42% power). A blind flange was installed downstream of the outboard containment isolation valve. Local leak rate testing of the containment penetration for the Containment and Drywell Purge system verified that leakage was within the limits for secondary containment bypass leakage. The NRC Resident Inspector has been notified. The licensee has commenced increasing reactor power. Notified R3DO (Orlikowski)

Local Leak Rate Testing
ENS 499872 April 2014 14:42:00PerryNRC Region 3GE-6

Release of toxic or flammable gas affecting the Protected Area boundary deemed detrimental to the safe operation of the plant. Emergency Action Level entered: MU-1. The leak is Trichloroethylene (TCE) gas used in the Off-Gas building. The Off-Gas building ground and basement levels were evacuated due to the leak. There is no safe-shutdown equipment located in the Off-Gas building. The licensee is working to isolate the leak. The licensee informed the NRC Resident Inspector. The licensee notified the State of Ohio and the local counties. Notified DHS SWO, FEMA Ops Center, NICC Watch Officer, DOE Ops Center, USDA Ops Center, HHS Ops Center, and Nuclear SSA via email.

  • * * UPDATE AT 1630 EDT ON 4/2/14 FROM DON ROGERS TO S. SANDIN * * *

The licensee notified the following outside agencies: U.S. EPA National Response Center, Ohio EPA, Perry Township Fire Department, Lake County Emergency Planning Committee, and the U.S. Coast Guard. Notified R3DO (Passehl).

  • * * UPDATE FROM MICHAEL ADLER TO DANIEL MILLS AT 0115 EDT ON 04/05/2014 * * *

Unusual Event has been terminated on 4/5/2014 at 0059 EDT. The trichloroethylene leak has been stopped. Access has been restored to all normally accessible areas. Unit 1 remains in Mode 1 at 100% power. The licensee notified the NRC Resident Inspector and the Local and State emergency agencies. Notified the IRD MOC (Gott), R3DO (Passehl), and NRR EO (McGinty). Notified DHS SWO, DOE Ops Center, FEMA Ops Center, HHS Ops Center, NICC Watch Officer, USDA OPS Center, EPA EOC, FDA EOC, and Nuclear SSA via email.

ENS 5021319 June 2014 17:06:00PerryNRC Region 3GE-6A review of industry operating experience regarding the impact of unfused Direct Current (DC) circuits has determined the described condition to be applicable to the Perry Nuclear Power Plant (PNPP) resulting in an unanalyzed condition with respect to fire safe shutdown requirements. In the postulated event, a fire induced hot short could adversely impact safe shutdown equipment. The potential exists for a secondary fire to occur due to unfused DC control circuits associated with the Turbine Emergency Bearing Oil Pump, Reactor Feed Pump Turbine 'A' Emergency Lube Oil Pump, Turbine Emergency Seal Oil Pump, and Reactor Feed Pump Turbine 'B' Emergency Lube Oil Pump. These circuits are routed from the respective equipment to other plant areas including the Unit 1 Control Room, Division 1 Cable Spreading, and Division 1 Cable Chase. Without overcurrent protection for these circuits, the potential exists that an initial fire event affecting these circuits could cause short circuits without protection that would cause excessive current through the circuit beyond the capacity rating of the conductors. This could lead to a secondary fire in another plant area where these circuits are routed challenging the ability to achieve and maintain safe shutdown. This condition is being reported in accordance with 10 CFR 50.72(b)(3)(ii)(B). Interim compensatory measures (i.e., fire watches) have been implemented for affected areas of the plant. The licensee has notified the NRC Resident Inspector.Hot Short
Safe Shutdown
Unanalyzed Condition
ENS 5045012 September 2014 10:12:00PerryNRC Region 3GE-6

At 1313 (EDT) on 7/26/14, the plant experienced an electrical transient on bus EK-1-B1 (safety-related 120 volt AC distribution panel) that resulted in partial Balance of Plant Division 2 isolation signals and alarms received in the Control Room. The following component actuations occurred: valve 1P50F140 closed, resulting in a trip of Containment Vessel Chilled Water C; valve 1G41F140 closed, isolating the Fuel Pool Cooling and Clean-up return from the containment building upper pools; valve 1B33F019 closed, isolating Reactor Water sampling; valve 1D17F071B closed, isolating the Drywell Atmosphere Radiation Monitor; valve 1D17F081B closed, isolating the Containment Atmosphere Radiation Monitor; valves 1G61-F030, 1G61-F150, 1G61-F075, and 1G61-F165 closed, isolating the Containment and Drywell Floor and Equipment drain sumps; valve 1G50-F272 closed isolating the Reactor Water Cleanup Backwash Receiving Tank: 1M25F020B, Control Room HVAC Inboard supply damper, closed and Division 2 indicated an auto initiation (M25-S12, Auto Initiate Active amber light was on). This event is considered an invalid system actuation reportable under 10 CFR 50.73(a)(2)(iv)(A).

The isolation was not initiated in response to actual plant conditions or parameters, and was not a manual initiation. Therefore, this notification is provided via a 60 day optional phone call in accordance with 10 CFR 50.73(a)(1) instead of submitting a written Licensee Event Report. The event meets reporting criteria specified in 10 CFR 50.73(a)(2)(iv)(B)(2) as a general containment isolation valve signal affecting containment isolation valves in more than one system. All affected systems functioned as expected in response to the electrical transient on bus EK-1-B1 that resulted in the partial Balance of Plant Division 2 isolation signals. The valves were reopened in accordance with plant procedures. The failure mechanism that caused the electrical transient was a failed capacitor in regulating transformer EFB1B2. The capacitor was replaced and tested with satisfactory results. The NRC Resident Inspector has been notified.

ENS 5055120 October 2014 03:55:00PerryNRC Region 3GE-6

The Perry Power Plant experienced a reactor scram during a shift of non-essential vital power supply to the alternate source. Feedwater was lost resulting in receiving a valid level 3 and level 2 signal. High Pressure Core Spray and Reactor Core Isolation Cooling started and injected. Reactor level and pressure have been stabilized to required bands. The motor feed pump has been started and is controlling level. High Pressure Core Spray and Reactor Core Isolation Cooling have been returned to standby. During the scram, all rods fully inserted into the core. Decay heat is being removed via the steam dumps to the condenser. The electrical grid is stable and supplying plant loads. An emergency diesel generator started, as designed, as a result of the level 2 signal but did not load. No safety valves lifted as a result of the transient. The cause of the loss of feedwater is under investigation. The licensee will be notifying the State of Ohio and Perry Township and has notified the NRC Resident Inspector.

  • * * UPDATE FROM DOUG SHORTER TO HOWIE CROUCH AT 0933 EDT ON 10/20/14 * * *

The plant is currently in Mode 3, stable with cooldown and depressurization to Mode 4 in progress. Level control is being provided by the motor feedwater pump. Troubleshooting of the cause of the scram and loss of feed water is on-going. The initial notification identified 10CFR50.72(b)(3)(iv)(A), 'Specified System Actuation', as a reporting criteria. The specific system that actuated was not provided. As a result of receiving a reactor vessel water level 2 signal a containment/BOP isolation signal was received. All systems isolated as required and the plant is restoring isolated systems in accordance with procedure. The licensee will be notifying the State of Ohio and Perry Township and has notified the NRC Resident Inspector. Notified R3DO (Pelke).

Reactor Vessel Water Level