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 Entered dateSiteRegionReactor typeEvent description
ENS 3945918 December 2002 15:22:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

An unauthorized entry into the protected area occurred by a contract employee. Immediate compensatory measures were taken upon discovery. The licensee has notified the NRC Resident Inspector. Contact the HOO for additional details.

  • * * UPDATE ON 10/14/03 @ 1650 BY REIMERS TO GOULD * * *

After further review of this event the Licensee has concluded that this event is not reportable and therefore it should be retracted. The NRC Resident Inspector will be informed. Notified Reg 2 RDO(Ogle)

ENS 4018922 September 2003 15:07:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopA licensed employee was determined to be under the influence of alcohol upon entry into the plant access control point. Access to the facility was denied and the employee's access to the facility has been suspended. Contact the Headquarters Operations Officer for additional details. The licensee has notified the NRC Resident Inspector.
ENS 4024313 October 2003 17:53:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopThe control room was notified by Land Utilization at 1700 EDT that they had contacted the Florida Fish and Wildlife for information on where to take the injured crocodile found on the plant access road. The crocodile was taken to the Miami Zoo. The NRC Resident Inspector was notified along with the State
ENS 4059015 March 2004 18:40:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopAt 1330 ET on 3/15/04, it was determined that a contract supervisor had tested positive for drugs on an access reinstatement urinalysis test. Access has been denied. The individual had only been badged for one day. A work review was conducted and no safety-related activities had been performed. Contact HOO for additional details. The licensee has notified the NRC Resident Inspector.
ENS 4075214 May 2004 18:26:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopAt 1728 EDTon 05/14/04, while performing maintenance on Turbine 1st stage steam pressure transmitter (PT-447), feedwater regulating valve (FRV) 4A was observed to close. At 1729, an automatic actuation of RPS occurred on Low Steam Generator level in the 4A Steam Generator. This was followed shortly by a manual reactor trip by the operator. All control rods fully inserted. All 3 turbine driven AFW pumps started as expected and are supply steam generators through both feedwater supply headers. The electric plant remains in a normal lineup. RCPs are in operation transferring decay heat to the steam generators. The MSIVs are open with the steam generators discharging steam to the main condenser using the condenser steam dump valves. All steam generator atmospheric dump valves opened on the reactor trip and closed. The plant is investigating the cause of the FRV closure and intends to stay in Mode 3 until the cause is determined and appropriate repairs are made. There was no impact on the other operating unit. The licensee will notify the NRC Resident Inspector.
ENS 410072 September 2004 11:20:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

Turkey point entered EAL 12A based on a confirmed hurricane warning from the State of Florida State Warning Point. The Licensee will notify the NRC Resident Inspector.

  • * * UPDATE FROM P. REIMERS TO W. GOTT AT 0611 ON 9/5/04 * * *

Hurricane Warning no longer in effect for the local area. Turkey Point no longer meets any Emergency Classification and is therefore deescalating from the Unusual Event. Notified R2DO (Landis), NRREO (Case), IRD (Wessman), DHS (McKentry), FEMA (Kuzia).

ENS 4104516 September 2004 23:30:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopAt 2010, Turkey Point 1/2 (Fossil Plant) hazardous Material Coordinator contacted the Florida Department of Environmental Resources and informed them of an oil spill with attending fire that occurred at Turkey Point Unit 2 (Fossil Plant) on 09/16/04. At 1654, Turkey Point Unit 2 (fossil Plant) developed an oil leak and fire on the third level burner deck. The fire was extinguished by automatic deluge system and fire team members. Less than 50 gallons of oil leaked and was contained on the third level burner deck. Turkey Point Units 3 and 4 were not affected. The licensee will notify the NRC Resident Inspector.
ENS 4105920 September 2004 20:56:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopA contract employee was determined to be under the influence of illegal drugs during a reinstatement urinalysis test. The employee's access to the plant has been terminated. Contact the Headquarters Operations Officer for additional details. The licensee will be notifying the NRC Resident Inspector.
ENS 4106422 September 2004 17:14:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopThe following information was obtained by the licensee via facsimile: Off-site notification to Miami-Dade County Environmental Resource Management was made at 1600 EDT 9/22/2004 for an oil spill and fire at the adjacent fossil Unit 2. The fire was extinguished by fossil plant personnel. The ignition source for the fire is unknown. The oil spill was in the fossil feed pump area. The licensee has notified the NRC Resident Inspector.
ENS 4106824 September 2004 17:23:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

Turkey Point Nuclear entered an Unusual Event due to Category 12 Natural Phenomena sub category A. Confirmed hurricane warning. The licensee notified the NRC Resident Inspector, State and Local authorities.

  • * * UPDATE 0723 EDT ON 9/26/04 FROM KEN HARRISON TO S. SANDIN * * *

The licensee is terminating their Unusual Event as of 0715 EDT after the Hurricane Warning was lifted for Miami-Dade. The licensee informed both state and local agencies and the NRC Resident Inspector. Notified R2 Response Manager (Len Wert), NRR (Stu Richards), IRD (Susan Frant), FEMA (Austin) and DHS (SWO).

ENS 410831 October 2004 16:30:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopThe following was received from the licensee via facsimile: A 56-year old male AREVA contractor died from a heart attack. A report of potential heart attack was made at 1242 (EDT) to the control room. Off-site medical assistance was used and the contractor was transported to South Miami-Homestead Hospital at 1340 (EDT). (The) contractor was pronounced dead at 1415 (EDT). The licensee also reported that the individual was not contaminated and was stricken while working in a contractor trailer located near the facility administration building. The licensee has notified the NRC Resident Inspector and will be notifying the Occupational Safety Health Administration (OSHA).
ENS 411027 October 2004 20:24:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopA single point vulnerability has been identified in the dousing system for the Emergency Containment Filter (ECF) System that could have resulted in dousing all filter units with borated water during an accident. Inadvertent dousing of the filters could adversely impact the methyl-iodide removal efficiency of the ECFs assumed in the plant safety analyses. This condition applies to both Turkey Point units. However, it is reportable under 10 CFR 50.72 only with respect to Unit 4 since Unit 4 is currently in operation while Unit 3 is in a refueling outage. The design deficiency has been evaluated in accordance with NRC Generic Letter 91-18. The ECFs have been determined to be operable but nonconforming and reportable under 10 CFR 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(C)and (D). A design change is being prepared to correct the vulnerability on both units. The licensee has notified the NRC resident inspector.
ENS 4122929 November 2004 01:36:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

Dropped rod E-11 in Shut Down Bank 'B' at 2334 on 11/28/04 while performing Low Power Physics Testing after refueling. Shutdown bank not fully withdrawn with dropped rod placed Unit 3 in Tech Spec Action Statement 3.0.3. RX trip breakers were opened at 0009 (11/29/04). Unit 3 entered 3-EOP-E.O, Reactor Trip or Safety Injection, the unit was placed in Mode 3 and transitioned to 3-EOP-ES-0.1, Reactor Trip Response and then into 3-GOP-301. All plant equipment responded as required and the unit remains stable in mode 3 while the Rod Control failure is investigated. The licensee notified the NRC resident inspector.

  • * * UPDATE AT 1838 EST ON 1/11/05 FROM MICHAEL KOHL TO S. SANDIN * * *

The purpose of this update is to clarify that the reactor was not critical at the time of reactor trip. The dropped rod added sufficient negative reactivity to render the reactor subcritical prior to the manual reactor trip. The cause of the dropped rod was an intermittent contact in a pin connector associated with rod E-11. The licensee will inform the NRC Resident Inspector. Notified R2DO (Landis).

ENS 4123230 November 2004 10:22:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

During low power physics testing, Shutdown Bank B, rod E-11 dropped from 227 steps (ARO (all rods out) 230) to 135 steps. Technical Specification 3.0.3 was entered. Unit 3 Reactor was tripped at 0920 and stabilized in mode 3. The licensee will notify the NRC Resident Inspector. See also similar event EN # 41229 11/29/04.

  • * * UPDATE AT 1838 EST ON 1/11/05 FROM MICHAEL KOHL TO S. SANDIN * * *

The purpose of this update is to clarify that the reactor was not critical at the time of reactor trip. The dropped rod added sufficient negative reactivity to render the reactor subcritical prior to the manual reactor trip. The cause of the dropped rod was an intermittent contact in a pin connector associated with rod E-11. The licensee will inform the NRC Resident Inspector. Notified R2DO (Landis).

ENS 4125714 December 2004 12:45:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopU3 manually tripped (Shift Manager decision). Fire in U3 HP turbine near bearing housing (offsite assistance not required). All plant equipment functioned as designed. A fire broke out near the #2 bearing housing on Unit 3 HP turbine and lasted about 9 minutes in length. Exact character of fire was not available at time of reporting. No unusual vibration readings or visual indications were observed prior to fire. Onsite fire brigade personnel responded to the turbine area without assistance of offsite emergency personnel. Five minutes into the event Unit 3 reactor was manually tripped. Nine minutes into the event, shift supervisor declared the fire was out. Fire personnel indicated the fire was "easily" put out. Licensee is evaluating action to be taken. When Unit 3 reactor was manually tripped, all rods inserted fully. No primary or secondary power relief valves actuated. AFW activated as expected. Licensee chose to close the MSIV to slow down the cooldown rate. Presently, decay heat is being removed via the steam dump into the atmosphere. Fire did not affect operational ability of Unit 4 or cause instability on the electrical grid. The licensee has notified the NRC Resident Inspector.
ENS 4129225 December 2004 08:50:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopManual reactor trip at 21.5" Hg and lowering. AFW initiated and operated as designed. On 12/25/04 Unit 4 at Turkey Point experienced a declining vacuum in the main condenser. When the condenser vacuum reached 21.5 Hg, manual trip criteria was reached and the plant was manually shut down. Decay heat is being removed via the Atmospheric Steam Dumps. There is no known primary to secondary tube leakage. The AFW system started as expected. All rods inserted correctly and all systems functioned as designed. The licensee will notify the NRC Resident Inspector.
ENS 4129828 December 2004 23:51:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopUnit 3 unplanned Manual Reactor trip from 70% due to Generator Exciter cooling water leak. Leak caused voltage regulator transfer to manual. Cooling water leak was isolated after the manual reactor trip. Water was noted in the 3B 4kv safety related bus room affecting 3B Residual Heat Removal Pump breaker. This component is considered inoperable pending corrective action. Plant is stable in mode 3. Auxiliary Feed Water actuated automatically, as expected, and operated normally following the reactor trip. All control rods fully inserted. The MSIV's were manually closed to prevent excessive RCS cooldown and decay heat is being removed via the atmospheric steam dumps. Unit 4 was unaffected. The licensee will notify the NRC Resident Inspector.
ENS 4150821 March 2005 12:20:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopOn 3/21/05 at 1045, the Control Room was notified of a fuel oil spill. The event was believed to have occurred on Saturday, 3/19/05 between 1900 and 0300. The amount of fuel oil ( Grade 2 Diesel) that was spilled was approximately 219 gallons and dispersed over a distance of about 1 mile. The cause of the spill was possibly due to a valve left open on the tanker after making a fuel delivery. The long trail of oil was made as the tanker left the site. The spill is contained and being cleaned up at this time. The area will be excavated and transported to Redland Construction. The location of the fuel oil spill occurred outside of the Nuclear Plant protected area at the new fossil plant. Construction site. DERM (Department of Environmental Resources Management) will be notified by Turkey Point Land Utilization representative. The NRC Resident Inspector will be notified.
ENS 4151122 March 2005 04:21:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopThe licensee provided the following information via fax (licensee text in quotes) The 4A SGFP (Steam Generator Feed Pump) tripped, initiating a Turbine Runback. Operators manually inserted a Reactor Trip at 15% Steam Generator level. The reactor tripped and all control rods inserted. Auxiliary Feedwater automatically initiated as expected. All systems operated as expected except the 4A SGFP discharge MOV which has no (position) indication (in the main control room and is being) investigated. Decay heat is being removed by atmospheric steam dumps. The licensee will notify the NRC Resident Inspector.
ENS 4151623 March 2005 22:29:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

Unit 4 reactor was manually tripped from 20 percent power per 4 - GOP - 103 "Power Operation to Hot Standby" (normal shutdown procedure), during a load reduction to take the unit off line. The reason for the load reduction was an oil leak of approximately 100 drops per minute on the "4B" steam generator feed pump. The reactor was tripped when directed by 4 - GOP - 103. All rods fully inserted, no relief valves lifted, and all other systems functioned normally. The licensee notified the NRC Resident Inspector.

  • * * UPDATE FROM V. BARRY TO M. RIPLEY 1125 EST 03/24/05 * * *

The licensee provided the following information via facsimile (licensee text in quotes): Upon review, the manual reactor trip from 20 percent power is not reportable in accordance with 10 CFR 50.72(b)(2)(iv)(13) since it was part of the pre-planned sequence of reactor shutdown steps contained in procedure 4-GOP-103, "Power Operation to Hot Standby." In addition, the reactor shutdown was not required by Technical Specifications. The NRC Resident Inspector will be notified of this retraction.

ENS 4155231 March 2005 13:00:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopTwo contract supervisors had a positive test during a random drug sampling. Both supervisors have had their plant access terminated and were escorted offsite. A review of the work performed by both individuals is in progress. Contact the Headquarters Operations Officer for additional details. The licensee notified the NRC Resident Inspector.
ENS 415778 April 2005 14:30:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopThe licensee provided the following information via facsimile (licensee text in quotes): On March 12, 2005, Turkey Point received two packages from, Nucon International that were inappropriately marked. 49CFR173.422(a) requires that packages containing radioactive material be marked on the outside with the UN number proceeded by the letters 'UN.' The packages had the Radioactive Material marking an the outside of the inner packing. The shipment of the unmarked packages constitute an "Undeclared Hazardous Material" as defined in 49CFR171.8. In accordance with 49CFR171.16(a)4, a 30-day report documenting the event was submitted to DOT on April 8, 2005. The survey of the two packages confirmed there was no spread of contamination. This report is being submitted in. accordance with 10CFR50.72(b)(2)(xi) due to offsite notification to DOT of the above incident. The licensee will notify the NRC Resident Inspector.
ENS 417433 June 2005 01:00:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

Declared Unusual Event due to RCS leakage greater than 10 gallons per minute. VCT level is lowering with constant plant temperature, pressure and pressurizer level. VCT level lowering at approximately 19 gallons per minute with associated rise in RWST level approximately 20 gallons per minute. The licensee will notify the NRC Resident Inspector.

  • * * UPDATE FROM MELIN TO W. GOTT AT 0120 ON 06/03/05 * * *

The licensee briefed NRC Management (McGinty, P. Hiland, R. Haag, J Munday) that the leakage was verified to be CVCS leakage and not RCS leakage. The leakage was stopped at 0055 and the licensee is evaluating termination/retraction criteria. NRC will not enter Monitoring Mode.

  • * * UPDATE FROM G MELIN TO W. GOTT AT 0140 ON 06/03/05 * * *

At 0055, leakage stopped. Leakage verified to be CVCS leakage, not RCS. The leakage is stopped. Validating no other anomalies exist then will evaluate termination and retraction of UE notification.

  • * * UPDATE FROM G MELIN TO P. SNYDER AT 0221 ON 06/03/05 * * *

Notification of termination of Unusual Event at 0221. Plant validation complete. RCS gross leakage is 0.07 gallon per minute and plant parameters are stable. Leakage confirmed to be from CVCS system which has been isolated. The licensee will notify the NRC Resident Inspector. Notified R2DO (R. Haag), NRR EO (P. Hiland), IRD (T. McGinty), R2 (J. Munday), DHS (I. Lee), FEMA (C. Ligget), and DOE (M. Smith)

  • * * UPDATE ON 6/15/05 @ 1243 FROM JIM SPEICHER TO CHAUNCEY GOULD * * * RETRACTION

Event Notice 41743 reported declaration of an Unusual Event at 00:33 on 6/3/05 for RCS leakage in excess of Technical Specification Limits. The source of leakage was subsequently determined to be from the Chemical and Volume Control System (CVCS) and not from the RCS. The Unusual Event was terminated at 02:00 6/3/05 after the leak was isolated. This event is retracted since the source of the leakage was not from the RCS and upon further review the event did not meet reporting requirements. The NRC Resident Inspector was notified. RDO (Tom Decker), EO (M. Mayfield) and IRD (Peter Wilson) were notified

ENS 4180027 June 2005 04:19:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

UNUSUAL EVENT (EAL #16 - Fire) declared at 0327 on 6/27/05 due to uncontrolled fire in the Unit 4 Main Transformer lasting longer than 10 minutes. Unit 4 experienced an automatic reactor trip from 100% on a turbine trip due to a fire in the Main Transformer. The fire was extinguished after approximately 25 minutes. On-site fire brigade and Miami-Dade fire department responded. The cause of the fire is under investigation. The reactor is stable in Mode 3. No safety systems were affected. All rods fully inserted, no ECCS actuations, no relief valves lifted and no personnel injuries occurred. Offsite power is still available and no emergency diesels auto started, however, there was an auxiliary feedwater actuation. Hazardous Material response is being implemented due to discharge of transformer oil. There may be a possible press release on this event. The NRC Resident Inspector was notified along with State and local agencies.

  • * * UPDATE ON 06/27/05 @ 05:13 BY SPEICHER TO GOULD * * *

The NOUE was terminated at 05:00 due to the fire being extinguished and the emergency no longer existing. The NRC Resident Inspector was notified. Notified RDO 3 (Evans), EDO (Case), IRO (Frant), FEMA (Bagwell), DHS (Reed)

  • * * UPDATE 0915 EDT ON 6/27/05 BY S. SANDIN * * *

Received a call from a member of the Turkey Point Communications Group. The licensee does not plan on issuing a press release at this time. Notified R2DO (Evans).

ENS 418298 July 2005 22:49:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopPTN (Turkey Point) received a notification from System Operations that switchyard voltage limits (based upon System Operations Contingency Analysis) was forecasted to exceed switchyard voltage limits if Unit 3 had tripped. This condition existed from 1434 to 1448 on July 8, 2005. At 1915 on July 8, 2005, PTN determined that both Unit 3 and 4 Startup Transformers were inoperable at 1434 on July 8, 2005, and entered Technical Specification 3.8.1.1 action e. This action was to notify the NRC within 4 hours; and to restore at least one of the inoperable Startup Transformers to OPERABLE status within 24 hours. At 1448 on July 8, 2005, both Startup Transformers were declared OPERABLE and PTN exited Technical Specification 3.8.1.1 action e. The licensee stated that the potential for low grid voltage at the Turkey Point Nuclear Plant was based on offsite conditions and was a postulated condition. Low voltage conditions did not actually occur. The licensee notified the NRC Resident Inspector.
ENS 4194324 August 2005 23:26:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

The licensee declared an Unusual Event in accordance with their emergency procedures due to hurricane force winds expected within 24 hours. The licensee does not have any Limiting Conditions for Operation on safety related equipment. No electrical grid disturbances currently exist and the licensee is currently testing their diesel generators in accordance with their emergency procedures. All emergency diesel generators are operable. The licensee notified state and local government agencies and the NRC Resident Inspector.

* * *  UPDATE FROM D. MORRIS TO W. GOTT AT 0141 EDT ON 08/26/05  * * * 

The licensee terminated the Unusual Event at 0110. Updated National Weather Service data removed the hurricane warning in the area. The licensee notified state and local governments. The licensee notified the NRC Resident Inspector. Notified R2DO (Ayers), NRR EO (Kuo), IRD Manager (Wilson), FEMA (Irwin), and DHS (Biasco).

ENS 4200119 September 2005 11:26:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

Turkey Point nuclear power plant is under a hurricane warning from the National Hurricane Center, starting at 11:00 EDT for Tropical Storm Rita. On-site facilities are not being activated at this time. No off-site assistance is requested. All 4 Emergency Diesel Generators are available and fully operable if needed. The electrical grid is stable. The licensee has notified the State and local agencies. The licensee will notify the NRC Resident Inspector.

  • * * UPDATE FROM D. FUNK TO W GOTT AT 1917 ON 09/19/05 * * *

Tropical storm force winds are expected between 0700 and 2100 on 09/20/05. Maximum expected sustained wind speed is 53 MPH. The licensee notified the NRC Resident Inspector. Notified R2DO (C Ogle) and R2 IRC (J. Hufham)

  • * * UPDATE FROM C. MONTGOMERY TO M. RIPLEY 1410 EDT 09/20/05 * * *

As of 1353 EDT 09/20/05, Turkey Point nuclear power plant is no longer in an Unusual Event due to a hurricane warning from the National Hurricane Center for Hurricane Rita. The licensee notified the NRC Resident Inspector, and State and County officials . Notified R2 DO (Ogle), IRD Mgr (Wilson), NNR EO (Benner), FEMA (Liggett), HERO (Gott), DHS via DOE Nuclear Event Notification Desk (J. Everett)

ENS 4205615 October 2005 08:54:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

Auxiliary Feedwater actuation due to low steam generator level following a manual reactor trip. At 0702 on 10/15/05, a manual reactor trip was initiated due to decreasing level on the 3C steam generator. Auxiliary Feedwater system actuated as expected due to post-trip steam generator level decrease. 3C steam generator level was restored using Auxiliary and Main feed. The cause of the loss of steam generator level control is under investigation. The plant is stable in Mode 3 with the Auxiliary Feedwater system in standby. All control rods fully inserted. The decay heat removal path is normal feedwater through the steam generators and out the atmospheric relief valves. There are no primary to secondary steam generator tube leaks. Safety related electrical busses are powered via normal offsite power. Emergency diesel generators are available if needed. There was no impact on Unit 4. The licensee notified the NRC Resident Inspector.

* * * UPDATE AT 1147 ON 10/19/05  FROM E. TREMBLAY TO P. SNYDER * * *

Updated to include notification under 10 CFR 50.72 (b)(2) for manual reactor trip. The licensee notified the NRC Resident Inspector. R2DO (Ernstes) notified.

ENS 4206722 October 2005 23:24:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopDeclaration of an Unusual Event due to Turkey Point Nuclear Site in a confirmed hurricane warning due to the projected path of Hurricane Wilma. The licensee indicated all 4 EDG's were available if required, and all safety systems were also available if required. The licensee will notify the NRC Resident Inspector. UPDATE FROM NRC (WILSON) TO NRC (KNOKE) AT 17:00 ON 10/23/05 The NRC entered into Monitoring Mode due to hurricane force winds expected to be at the site within 12 hours.
ENS 4207425 October 2005 02:16:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopAt 2300 on October 24, 2005, both unit 3 and unit 4 start up transformers were declared inoperable and Tech Spec 3.8.1.1.e action statements were entered. With both units being energized from their respective start-up transformers, the high voltage limit is 241.5kV in accordance with 0-ONOP-004.6, Degraded Switchyard Voltage. System Operations reported switchyard voltage at 243.5 kV and 242.5 kV for unit 3 and unit 4 respectfully. System Operations was requested to lower switchyard voltage to within limits. At 0015 on October 25, 2005, switchyard voltage being lowered to within the switchyard limits and both start-up transformers were declared operable. The high switchyard voltage is due to hurricane Wilma's impact on the Florida service area that has (led) to low system load with cooler weather conditions. The NRC Resident Inspector has been notified.
ENS 4207525 October 2005 13:01:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopAt 1000 EDT on October 25, 2005, it was discovered that no good data is being transmitted via the FTS-2001 communications link. The communications link itself is functioning properly; however, the front end processor and the spare train for Unit 4 are not on-line. The estimated time of repair for restoration of data flow is approximately 1700 EDT on 10/25/05. The licensee notified the NRC Resident Inspector.
ENS 4207825 October 2005 22:05:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

Small Class B fire on the Unit 3 High Pressure Turbine. Fire is currently out, presented no challenges, and lasted 13 minutes The fire occurred underneath the high pressure turbine bearing and was caused by oil soaked insulation. The fire was extinguished by the site's fire brigade and resulted in no injuries to plant personnel. Plant safety and emergency systems were not affected by the fire and all plant systems functioned as required. Currently, the fire brigade is being debriefed and it is anticipated that the site will terminate the Unusual Event shortly. The licensee notified the State, local authorities and the NRC Resident Inspector.

  • * * UPDATE AT 23:54 EDT ON 10/25/2005 FROM MICHAEL COEN TO RIPLEY * * *

Small class B fire on the Unit 3 High Pressure Turbine. Fire is currently out, presented no challenge, and lasted 13 minutes. Terminated Unusual Event at 2330. The plant is in mode three both before and after the event. The plant startup schedule has not been determined. The licensee will notify the NRC Resident Inspector. Notified the IRD Manager (Blount), FEMA (Chris Leggett), R2DO (Ernstes), and NRR EO (Hannon).

ENS 4210431 October 2005 23:02:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

Unusual event category 10A on Unit 4. Loss of offsite power to Unit 4 due to loss of Unit 4 Startup Transformer. Auto AFW actuation. Auto starting and loading of both Unit 4 Emergency Diesel Generators. The licensee stated that the plant is stable in Mode 3 at approximately 700 psi and 380 deg F. The plant was experiencing electrical grid instabilities at the time of the trip of the Startup Transformer. The exact cause of the transformer trip is being investigated. The grid instabilities were associated with the plant's Northwest Bus, therefore, Unit 3 is not affected and continues to operate at approximately 60% power. The licensee notified the State of Florida and will notify the NRC Resident Inspector

      • UPDATE FROM D. FUNK TO J. KNOKE AT 02:15 ON 11/02/05 ***

The licensee terminated from their Unusual Event (EAL 10A) at 0200 EST on 11/02/05. Unit 4 A & B 4 KV busses are now powered from off-site power using Unit 4 startup transformer." The power / mode for Unit 4 is now 0% power / Mode 5. The licensee will notify the NRC Resident Inspector and has notified State, local and other government agencies. Notified R2DO (Ayres), NRR EO (Case), IRD-MOC (Wilson), DHS (J. Frost) and FEMA (S. Kimbrell).

ENS 4213711 November 2005 16:50:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopDuring a reactor startup, while withdrawing the second shutdown bank, a failure of the 2BD rod control power cabinet occurred. Shutdown Bank B group 2 rods failed to withdraw. After gathering data and indications for troubleshooting, a manual reactor trip was initiated. All rods fully inserted. The Unit was and remains in mode 3. There were no other required or actual ESF actuations. The licensee will notify the NRC Resident Inspector.
ENS 4214817 November 2005 08:55:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopEmergency Response Data System (ERDS) was unavailable from 00:47 until 01:51 due to an Emergency Response Data Acquisition and Display System (ERDADS) failure. The problem has been corrected and ERDADS is currently able to supply data to ERDS. The licensee will notify the NRC Resident Inspector.
ENS 421898 December 2005 13:41:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

There will be a "loss of U3 ERDADS data retrieval capability to Emergency Response Data System (ERDS) link due to a planned software modification to the U3 ERDADS computer. The expected duration of the loss of capability is 3 hours. The licensee notified the NRC Resident Inspector.

* * * UPDATE FROM M.A. NEWTON TO P. SNYDER AT 2022 ON 12/8/05 * * * 

Unit 3 ERDADS data retrieval capability to ERDS link due a planned software modification to Unit 3 ERDADS computer has been restored. The total duration for this loss of capability was 6 hours." The system was returned to service at 2004. The licensee will notify the NRC Resident Inspector.

ENS 423998 March 2006 22:38:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

While restoring power to the 3C 480V Load Center following planned maintenance, the 3A safety related 4KV Bus was deenergized by the 3A Sequencer. This resulted in a valid actuation of the emergency diesel generator. The plant was in Mode 5, depressurized, with reactor coolant system level at approximately the vessel flange level. This resulted in a temporary loss of residual heat removal flow which was restored within approximately seven (7) minutes. Reactor coolant system temperature increased from 113 degrees F to 140 degrees F. Reactor coolant system level and temperature were stabilized at pre-event values. At this time the licensee is preparing to restore off-site power to the 3A Bus and put the emergency diesel generator in standby. The licensee is also investigating the cause of the power loss to the 3A safety related 4KV Bus. The licensee will notify the NRC Resident Inspector.

  • * * UPDATE FROM G. RICHARDSON TO M. RIPLEY 2248 EST 03/09/06 * * *

In response to questions regarding the cause of the loss of the 3A 4KV bus, the following information is provided: The 3C 480 volt Load Center was de-energized for maintenance and was being restored at the time of the event. One of the maintenance activities associated with the 3C Load Center involved replacement of the 480V feeder breaker for the load center. A rotating cam inside the auxiliary switch for the replacement breaker was misaligned. The misaligned cam caused the switch contacts to operate in reverse, such that normally open contacts would be normally closed and vice versa. One of the auxiliary contacts on the 3C Load Center 480V feeder breaker provides input to the A-train Emergency Diesel Generator (EDG) Load Sequencer. With this contact operation reversed (closed vs. open with the breaker open), the Load Sequencer sensed undervoltage on the 3C Load Center, when the 4kV feeder breaker for the load center was closed. The contact being open would normally block the undervoltage signal, until the 480V feeder breaker was closed and the bus was energized. Once the A-train Load Sequencer sensed the undervoltage condition, the 3A 4kV bus was stripped and then re-energized from the 3A EDG. The licensee notified the NRC Resident Inspector. Notified R2DO (Fredrickson)

ENS 424009 March 2006 09:20:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

While the Unit 3 Startup Transformer was inoperable for planned maintenance, it was discovered that both the 3A and 3B Emergency Diesel Generators were inoperable. The Emergency Diesel Generators were inoperable due to a configuration that resulted in the Emergency Diesel Generators being in the Droop mode versus the Isochronous mode. This configuration was improperly established when offsite power was supplied to Unit 3 via the Main and Auxiliary Transformers (Backfeed). Upon discovery, jumpers were installed to place both (Unit 3) Emergency Diesel Generators in the proper Isochronous mode correcting this condition at 0615 on March 9, 2006. Unit 4 was identified to be in a condition where one of its required Startup Transformers (from Unit 3) and one of its required Emergency Diesel Generators (from Unit 3) were out of service. Both (Unit 3) Emergency Diesel Generators were restored to an operable condition approximately twenty (20) minutes after discovery. Technical Specification 3.8.1.1 Action c entered due to inoperable Unit 3 Startup Transformer and one inoperable Unit 3 EDG and requires a 4 hour notification report to the NRC. The licensee notified the NRC Resident Inspector.

  • * * * UPDATE AT 1301 EST ON 3/9/06 FROM M. MURPHY TO P. SNYDER * * * *

As reported in Event Notification # 42400, with Unit 4 at 100% power in Mode 1, and the Unit 3 Startup Transformer out of service for planned maintenance, both the 3A and 3B Emergency Diesel Generators were declared inoperable due to a configuration that placed both Emergency Diesel Generators in the droop mode versus the normal isochronous mode. This placed Unit 4 in a Technical Specification Action Statement for one of its required Startup Transformers and one of its required Emergency Diesel Generators being inoperable. This EN# 42400 supplement documents that, although the 3A and 3B Emergency Diesel Generators were declared inoperable, the droop mode condition is bounded within previous analyses that demonstrate that the Emergency Diesel Generators and required electrical loads would operate to satisfactorily perform their safety function at the resulting reduced electrical frequency. Refer (to) Turkey Point LER 2004-001-01, dated 10/18/04. The licensee notified the NRC Resident Inspector. Notified R2DO (Fredrickson).

ENS 426173 June 2006 16:45:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopAt 1545, Turkey Point Unit 2, a Fossil Plant, reported a leaking fuel coil heater gasket which leaked approximately 500 gallons of #6 Fuel Oil. This leak occurred at 1100 this morning. Most of this fuel oil was captured in a berm. However, approximately 200 gallons of the oil drained into the cooling canals. Miami-Dade DERM (Department of Environmental Resources Management) was notified at approximately 1430 and the State Warning Point was notified at approximately 1500. The licensee stated that the leak posed no threat to the operation or safety of Units 3 and 4. The licensee notified the NRC Resident Inspector.
ENS 4276614 August 2006 00:30:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopThere has been a fuel oil spill at the Turkey Point - Fossil plant of approximately 200 gal at 21:30 on 8/13/06. Turkey Point Nuclear control room was contacted at 00:02 on 8/14/06. The Control Room was notified that the spill had been contained and clean-up was in progress. DERM (Department of Environmental Resource Management) had been contacted at 23:05, and a vacuum truck from SWS Environmental had been dispatched to the site to assist in clean-up. The spill was contained on-site, with no chance of release off-site. The NRC Resident Inspector will be notified of this notification by the licensee.
ENS 4279523 August 2006 11:23:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopOn 08/23/06 at 0940, Turkey Point Nuclear Station was informed of a possible news release concerning the activities of a non-supervisor initial operator student. The initiating activities in question occurred prior to the employment of the individual at Florida Power and Light and have resulted in the recent off site arrest of the student on felony charges. Plant access was suspended immediately upon supervisor notification pending further investigation. Florida Power and Light and Turkey Point were not mentioned in the initial news release. The licensee notified the NRC Resident Inspector.
ENS 432896 April 2007 19:01:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopThis is a non-emergent event. At 1600 EDT, Unit 5 (conventional Co-Generation plant) reported to Florida state agencies a spill of their Closed Cooling Water due to a failure of a system valve. The magnitude of the spill was approximately 2500 gal of cooling water which contained Molybdates. The water was contained in the site's normal drain system. Agencies notified: Florida State Warning Point Florida Department of Environmental Protection - District Florida Department oh Environmental Protection - District Citing Office The actual event occurred at 0822. Turkey Point Control Room was informed of the notification at 1610. The licensee will notify the NRC Resident Inspector.
ENS 434086 June 2007 09:32:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

At 0746, on 6/6/2007, a Unit 3 shutdown was initiated in accordance with station procedures. Unit 3 entered Technical Specification (TS) 3.0.3 at 0745 on 6/6/2007. TS 3.0.3 was entered when the Analog Rod Position Indicator (ARPI) for control rod F-4 was declared inoperable. Control rod F-4 is located in control bank C. The ARPI for control rod M6, which is also in control bank C, has been previously declared inoperable. With two ARPIs in control bank C inoperable, TS Limiting Condition for Operation 3.1.3.2, Action a, cannot be met thus necessitating entry into TS 3.0.3. ARPI repairs will be performed as required. The licensee notified the NRC Resident Inspector.

* * * UPDATE FROM E. NEVILLE TO P. SNYDER AT 1400 ON 6/6/07 * * * 

Turkey Point Unit 3 entered Mode 3 at 1152 on 6/6/07 after manually tripping from approximately 25% power. At 1152 Turkey Point exited TS 3.0.3 since the condition for which it was entered no longer applied. The site borated to compensate for the control rods for which position indication was lost. All control rods fully inserted on the trip. The plant is currently steaming to atmospheric relief valves. No primary to secondary tube leaks exist. The licensee will notify the NRC Resident Inspector. Notified R2DO (Fredrickson).

ENS 436145 September 2007 12:46:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

The Plant Process Computer System (Emergency Response and Data Acquisition System, 'ERDADS') will be taken out of service for an approximate 4 week period (on Unit 3) to implement a planned modification. The current ERDADS is being replaced on Unit 3 and a computer outage is required for the installation of the new ERDADS. During this time period ERDS and SPDS functions will not be available for Unit 3. Unit 4 will function normally after a modification (expected duration 6 hours) to the existing computer operating system software is implemented. Also, Unit 3 Regulatory Guide 1.97 category 2D containment temperature and power system indicators for motor control centers, batteries, and inverters will not be available in the Control Room, although other instrumentation is available to monitor these parameters. This is an 8-hour reportable event per 10 CFR 50.72(b)(3)(xiii) Major Loss of Assessment Capability. The operation of plant systems will not be affected due to this planned action. ERDS and SPDS parameters will be monitored by control board indications. Compensatory actions have been developed. Follow up notification to NRC will be given once Unit 4 ERDS and SPDS are returned to service. The licensee notified the NRC Resident Inspector.

  • * * UPDATE PROVIDED BY JIM SPEICHER TO JEFF ROTTON AT 1031 EDT ON 09/10/07 * * *

The Plant Process Computer System (Emergency Response and Data Acquisition System, 'ERDADS') was taken out of service on both Unit 3 and Unit 4 in order to implement a planned modification on Unit 3. The current ERDADS system is being replaced on Unit 3 during the current Unit 3 refueling outage. In order to perform this replacement, ERDS and SPDS functions had to be temporarily removed from Unit 4. ERDADS and SPDS functions have been returned to service on Unit 4 and have been verified to operate correctly. The ERDS link for Unit 4 was satisfactorily tested on 9/7/07. The ERDADS replacement on Unit 3 will continue with an estimated completion on September 24, 2007. The licensee notified the NRC Resident Inspector. Notified R2DO (S. Shaeffer)

  • * * UPDATE FROM NIELSEN TO HUFFMAN AT 1642 EDT ON 10/10/07 * * *

The Plant Process Computer System (Emergency Response and Data Acquisition System. 'ERDADS') was taken out of service in order to implement a planned modification on Unit 3. Replacement of the ERDADS system on Unit 3 is complete. The ERDS link for Unit 3 was satisfactorily tested on 10/10/07. The licensee notified the NRC Resident Inspector. Notified R2DO (Desai).

ENS 4362710 September 2007 14:51:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopOn September 7, 2007, a small amount of water was discovered in the environmental qualification boundary of the 3B RCS Tcold thermowell (TE-3-420) during inspection of the thermowell. Subsequent mass spectroscopy analysis conducted at 1228, on September 8, 2007, indicated small levels of lithium, boron, strontium, and bromine indicating that the source of the water intrusion into the thermowell was likely reactor coolant system (RCS) fluid. Turkey Point Unit 3 Technical Specification (TS) Limiting Condition for Operation (LCO) 3.4.6.2.a permits no reactor coolant system pressure boundary leakage. As a result of the chemical analysis and indication of fluid in the thermowell, this condition is being reported to the NRC pursuant to the requirements of 10 CFR 50.72(b)(3)(ii)(A) as a degraded condition. An investigation of the source of the water intrusion into the thermowell is ongoing. Leakage into the TE-3-420 was previously noted during the last refueling outage for Unit 3 in March 2006 and a Short Notice Outage (SNO) conducted in June 2007. Previous inspections and sampling did not indicate the presence of boron or activity levels that were consistent with RCS water. At the time of discovery, Turkey Point Unit 3 was in Operational Mode 6 (Refueling). Turkey Point Unit 3 is presently defueled. This is a late prompt notification. The NRC Resident inspector will be notified.
ENS 4364114 September 2007 02:18:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopDuring an investigation in response to a low megger reading, a small amount of water was discovered in the environmental qualification boundary of the 22B RCS Thot thermowell (TE-3-422B2). Analysis of the water on 9/13/07 at 2304 showed Cesium 137 and 134, and Magnesium 54 indicating that the source of water intrusion into the thermowell was likely reactor coolant system (RCS) fluid. We are continuing the investigation for potential causes of water intrusion other than the Reactor Coolant System. This report is being made based on the previous indication of RCS leakage into 23A, RCS Tcold thermowell (TE-3-420) (see EN #43627 from 09/10/07) and similar discovery in our preliminary investigation. PTN Unit 3 Technical Specifications (TS) Limiting Condition for Operation (LCO) 3.4.6.2.a permits no reactor coolant pressure boundary leakage in Modes 1-4. This report to the NRC is pursuant to the requirements of 10 CFR 50.72 (b)(3)(ii)(A) as a degraded condition. Turkey Point Unit 3 is presently defueled. The licensee will notify the NRC Resident Inspector.
ENS 4370510 October 2007 05:35:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

The Emergency Response and Data Acquisition System (ERDADS) was out of service at 0000 EST on 10/10/2007. This resulted in a loss of the ERDS link of plant data to the NRC. This is an 8-hour reportable event pursuant to 10CFR50.72(b)(3)(xiii) Major Loss of Assessment Capability. The cause of the loss appears to be a computer malfunction, there is no evidence of tampering. Follow-up notification to the NRC will be given once Unit 4 ERDS is returned to service. As of 0515 ERDADS was available in the licensee control room, but the ERDS link was not available with the NRC. The licensee notified the NRC Resident Inspector.

  • * * UPDATE FROM NIELSEN TO HUFFMAN AT 1341 EDT ON 10/12/07 * * *

Repairs are complete and the Unit 4 ERDADS system was tested Sat. at 1216 EDT on 10/12/07. The ERDS link of plant data to the NRC has been restored on Unit 4. The licensee notified the NRC Resident Inspector. R2DO (Desai) notified.

ENS 4371611 October 2007 21:37:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopA non-licensed employee supervisor had a confirmed positive for illegal drugs during a random fitness-for-duty test. The employee's access to the plant has been terminated. Contact the Headquarters Operations Officer for additional details.
ENS 4379821 November 2007 09:15:00Turkey PointNRC Region 2Westinghouse PWR 3-Loop

At 0330 on 11/21/07, Unit 4 ERDADS computer system failed and subsequently would not display any data. The plant's other Computer display system continues to show data. However, it has been determined the Emergency Response Data System (ERDS) link from Unit 4 is inoperable. Troubleshooting is in progress and a follow up notification will be made when the Unit 4 Emergency Response Data System is operable. The Unit 3 Emergency Response Data System remains operable. The licensee notified the NRC Resident Inspector.

  • * * UPDATE AT 1145 ON 12/7/2007 FROM EDWARD NIELSEN TO JEFF ROTTON * * *

Repairs are complete and the Unit 4 ERDS link was available at 2321 on 12/1/2007. Subsequent testing and evaluation is complete and the ERDS link has been declared operable at 0800 on 12/7/2007. The licensee notified the NRC Resident Inspector. Notified the R2DO (Musser).

ENS 4380321 November 2007 19:00:00Turkey PointNRC Region 2Westinghouse PWR 3-LoopAt approximately 1115 on 11/21/07 it was discovered that the Unit 3 ERDADS long term historian data stream was not updating. This impacted the ability of the ERDS link to transmit valid data. The modem was functional, but did not appear to be receiving data from the ERDADS computers. The long term historian appears to have gone offline at 1441 on 11/12/07. The probable cause of the malfunction appears to be a post installation modification to the system. The ERDS link was restored at 1130 11/21/07 and testing has confirmed it operable. No evidence of tampering has been discovered and this failure affects Unit 3 only. The NRC Resident Inspector will be notified.