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05000259/LER-1980-031, Updated LER 80-031/03X-1:on 820415,during 4 Kv Shutdown Bus 2 Transfer,Fault on Normal Feeder Bus from TS1B to 480-volt SD Bd 1B Caused Loss of Power to Board.Caused by Fault Condition at Busway Joint Above Board1 June 1982Updated LER 80-031/03X-1:on 820415,during 4 Kv Shutdown Bus 2 Transfer,Fault on Normal Feeder Bus from TS1B to 480-volt SD Bd 1B Caused Loss of Power to Board.Caused by Fault Condition at Busway Joint Above Board
05000259/LER-1982-018, Updated LER 82-018/03X-1:on 820317,inspector Observed Bolts Missing from Reactor Core Isolation Cooling Turbine Exhuast Rupture Diaphragm Assembly.Outer Rupture Diaphragm Missing. Caused by Failure to Install Outer Rupture Disc1 June 1982Updated LER 82-018/03X-1:on 820317,inspector Observed Bolts Missing from Reactor Core Isolation Cooling Turbine Exhuast Rupture Diaphragm Assembly.Outer Rupture Diaphragm Missing. Caused by Failure to Install Outer Rupture Disc
05000259/LER-1982-023, Followup LER 82-023/03X-2:on 820327,recirculation Pump 1A Tripped Due to Spurious Generator Starter Relay Operation. Caused by Hi-temp Relay Trip.Relay Reset in 20 Minutes & Pump Returned to Svc.No Recurrence Control Planned13 October 1982Followup LER 82-023/03X-2:on 820327,recirculation Pump 1A Tripped Due to Spurious Generator Starter Relay Operation. Caused by Hi-temp Relay Trip.Relay Reset in 20 Minutes & Pump Returned to Svc.No Recurrence Control Planned
05000259/LER-1982-039, Reissued LER 82-039/03L-0:on 820609,fuse Blew Resulting in Inboard Primary Containment Isolation.Caused by Shorted Coil for Relay 16A-K66B,GE Type CR120A.Fuse & Relay Coil Replaced & Hydrogen Analyzers Returned to Normal6 July 1982Reissued LER 82-039/03L-0:on 820609,fuse Blew Resulting in Inboard Primary Containment Isolation.Caused by Shorted Coil for Relay 16A-K66B,GE Type CR120A.Fuse & Relay Coil Replaced & Hydrogen Analyzers Returned to Normal
05000259/LER-1982-064, Updated LER 82-064/03X-1:on 820823 & Jan 1984,Station II Cable Tray Fixed Spray Sys Did Not Meet Tech Spec Requirements.Caused by Restriction in Supply Line Strainer Due to Buildup of Silt & Clam Shells20 April 1984Updated LER 82-064/03X-1:on 820823 & Jan 1984,Station II Cable Tray Fixed Spray Sys Did Not Meet Tech Spec Requirements.Caused by Restriction in Supply Line Strainer Due to Buildup of Silt & Clam ShellsFire Watch
05000259/LER-1982-089, Updated LER 82-089/03T-1:on 821103,primary Containment Purge Sys Failed to Achieve Required Flow Rate.Caused by Sand Dust Clogging HEPA Filters.New Filters Installed8 April 1983Updated LER 82-089/03T-1:on 821103,primary Containment Purge Sys Failed to Achieve Required Flow Rate.Caused by Sand Dust Clogging HEPA Filters.New Filters Installed
05000259/LER-1983-018, Updated LER 83-018/031-2:on 830325,while Performing SI 4.2.A-13,standby Gas Train B Found Inoperable.Caused by Erratic Mcdonnel & Miller Flow Switch.Switch Replaced & SI 4.7.B-1 & SI 4.7.A-13 Completed27 July 1984Updated LER 83-018/031-2:on 830325,while Performing SI 4.2.A-13,standby Gas Train B Found Inoperable.Caused by Erratic Mcdonnel & Miller Flow Switch.Switch Replaced & SI 4.7.B-1 & SI 4.7.A-13 Completed
05000259/LER-1983-029, Updated LER 83-029/03L-1:on 830604,during Standby Gas Treatment Sys Operability Test,Train B Discovered Inoperable.Caused by Erratic Mcdonnel & Miller Model AF-1 Flow Switches.Damper Adjusted.W/Undated Ltr27 February 1984Updated LER 83-029/03L-1:on 830604,during Standby Gas Treatment Sys Operability Test,Train B Discovered Inoperable.Caused by Erratic Mcdonnel & Miller Model AF-1 Flow Switches.Damper Adjusted.W/Undated Ltr
05000259/LER-1983-066, Updated LER 83-066/03X-1:on 831112,interlock That Prevents Bridge Travel Over Core W/One Rod Withdrawn & Fuel Grapple Extended Failed to Operate,Resulting in Loss of Rod Block Function.Caused by Improper adjustment.W/840309 Ltr9 March 1984Updated LER 83-066/03X-1:on 831112,interlock That Prevents Bridge Travel Over Core W/One Rod Withdrawn & Fuel Grapple Extended Failed to Operate,Resulting in Loss of Rod Block Function.Caused by Improper adjustment.W/840309 Ltr
05000259/LER-1984-004, Updated LER 84-004-01:on 840106,reactor Mode Switch Moved from Run to Startup,Causing Half Scram.Caused by Personnel Error.Unit Manually Scrammed.Operator & Nuclear Engineer Counseled Re Use of Rod Notch Override11 April 1984Updated LER 84-004-01:on 840106,reactor Mode Switch Moved from Run to Startup,Causing Half Scram.Caused by Personnel Error.Unit Manually Scrammed.Operator & Nuclear Engineer Counseled Re Use of Rod Notch OverrideHalf scram
05000259/LER-1984-007, Followup LER 84-007-01:on 840127,operator Observed Decreasing Pressure on Control Atmospheric Dilution Tanks. Caused by Two Isolation Valves Being in Closed Position. Operating Instructions Revised2 March 1984Followup LER 84-007-01:on 840127,operator Observed Decreasing Pressure on Control Atmospheric Dilution Tanks. Caused by Two Isolation Valves Being in Closed Position. Operating Instructions Revised
05000259/LER-1984-014, Updated LER 84-014-01:on 840222,reactor Scrammed When Turbine High Pressure First Stage Pressure Exceeded 142 Psig W/Turbine Stop Valves Closed.Caused by Procedural Error. Operating Instruction Revised13 March 1984Updated LER 84-014-01:on 840222,reactor Scrammed When Turbine High Pressure First Stage Pressure Exceeded 142 Psig W/Turbine Stop Valves Closed.Caused by Procedural Error. Operating Instruction Revised
05000259/LER-1984-022, Updated LER 84-022-01:on 840212,investigation Determined That Single Failure or LOCA & Loss of Offsite Power Could Cause Equipment Necessary for Electrical Board Room Cooling to Be Lost.Caused by Design Oversight20 July 1984Updated LER 84-022-01:on 840212,investigation Determined That Single Failure or LOCA & Loss of Offsite Power Could Cause Equipment Necessary for Electrical Board Room Cooling to Be Lost.Caused by Design Oversight
05000259/LER-1985-049, Corrected Page 1 to LER 85-049-00:on 850623,during Performance of Work on Diesel Generator Battery Racks, Several Rack Support Studs Found Broken.Caused by Use of Stud Matl Not Suitable for Welding25 October 1985Corrected Page 1 to LER 85-049-00:on 850623,during Performance of Work on Diesel Generator Battery Racks, Several Rack Support Studs Found Broken.Caused by Use of Stud Matl Not Suitable for Welding
05000259/LER-1985-054, Advises That LER 85-054-00 Cancelled10 February 1986Advises That LER 85-054-00 Cancelled
05000260/LER-1981-052, Updated LER 81-052/03X-1:on 811007,containment Atmosphere Hydrogen Analyzer B Sample Return Pump Discovered Cycling. Probably Caused by Randon Failure.Gas Calibr Performed & Analyzer Returned to Svc12 April 1982Updated LER 81-052/03X-1:on 811007,containment Atmosphere Hydrogen Analyzer B Sample Return Pump Discovered Cycling. Probably Caused by Randon Failure.Gas Calibr Performed & Analyzer Returned to Svc
05000260/LER-1982-010, Corrected LER 82-010/03L-0 on 811021,during Full Power,Avg Power Range Monitor Output Signal Calibr Was Not Performed within Required Frequency During 811014-28.Caused by Personnel Error.Personnel Instructed to Be More Careful4 March 1982Corrected LER 82-010/03L-0 on 811021,during Full Power,Avg Power Range Monitor Output Signal Calibr Was Not Performed within Required Frequency During 811014-28.Caused by Personnel Error.Personnel Instructed to Be More Careful
05000260/LER-1982-013, Updated LER 82-013/03X-1:on 820412,pressure Switch 2-PS-68-96 Found to Operate Above Tech Spec Limits.Caused by Drifted Calibr.Barton Model 288 Pressure Switch Recalibr, Functionally Tested & Returned to Svc1 June 1982Updated LER 82-013/03X-1:on 820412,pressure Switch 2-PS-68-96 Found to Operate Above Tech Spec Limits.Caused by Drifted Calibr.Barton Model 288 Pressure Switch Recalibr, Functionally Tested & Returned to Svc
05000260/LER-1982-028, Followup LER 82-028/03X-3:on 810921,turbine Reactor Bldg Doors 237 & 238 Opened Simultaneously,Breaching Secondary Containment.Caused by Failed Folger Adams Interlock Sys Due to Loose Door Latch Screws.Procedures Revised9 March 1984Followup LER 82-028/03X-3:on 810921,turbine Reactor Bldg Doors 237 & 238 Opened Simultaneously,Breaching Secondary Containment.Caused by Failed Folger Adams Interlock Sys Due to Loose Door Latch Screws.Procedures Revised
05000260/LER-1983-074, Updated LER 83-074/03X-1:on 831105 & 10,turbine Exhaust Inner Rupture Diaphragms Failed During HPCI Initiation. Investigation Underway to Determine Cause of Failures. Diaphragms Replaced & HPCI Returned to Svc5 December 1983Updated LER 83-074/03X-1:on 831105 & 10,turbine Exhaust Inner Rupture Diaphragms Failed During HPCI Initiation. Investigation Underway to Determine Cause of Failures. Diaphragms Replaced & HPCI Returned to Svc
05000260/LER-1986-003, Corrected Page 2 to LER 86-003-00:on 860226,energized Isolation Logic Tripped.Caused by Personnel Error.Temporary Cover for Protection Against Accidental Bumping of Bus Transfer Switch Provided10 April 1986Corrected Page 2 to LER 86-003-00:on 860226,energized Isolation Logic Tripped.Caused by Personnel Error.Temporary Cover for Protection Against Accidental Bumping of Bus Transfer Switch Provided
05000296/LER-1979-005, Updated LER 79-005/01T-2:on 790506,RHR Svc Water Supply to RHR HX 2B Isolated Standby Coolant Supply.Caused by Lack of Administrative Control Over Sys Cross Connect Valves. Controls Improved27 April 1984Updated LER 79-005/01T-2:on 790506,RHR Svc Water Supply to RHR HX 2B Isolated Standby Coolant Supply.Caused by Lack of Administrative Control Over Sys Cross Connect Valves. Controls Improved
05000296/LER-1983-026, Supplemental LER 83-026/03X-4:on 830411,while Attempting to Establish EECW Flow Rate to Emergency Diesel Generator 3 Coolers,Head on HX Found Cracked.Caused by Mfg Defect.Cast Iron Head Replaced25 November 1983Supplemental LER 83-026/03X-4:on 830411,while Attempting to Establish EECW Flow Rate to Emergency Diesel Generator 3 Coolers,Head on HX Found Cracked.Caused by Mfg Defect.Cast Iron Head ReplacedHydrostatic
05000296/LER-1984-004, Followup LER 84-004-01:on 840228,RHR Outboard Loop II Isolation Valve CFV-74-67 Stem Found Broken Upon Disassembly.Caused by Overloading.Valve Stem Replaced W/Stronger & More Durable Matl15 June 1984Followup LER 84-004-01:on 840228,RHR Outboard Loop II Isolation Valve CFV-74-67 Stem Found Broken Upon Disassembly.Caused by Overloading.Valve Stem Replaced W/Stronger & More Durable Matl
IR 05000259/197903229 November 1979RO-50-259/79-32:on 791128,during Insp of Restraints,Typical Hanger Identified as Possibly Unacceptable.Caused by Possible Misapplication of Hanger.Insp & Analyses Will Be Conducted to Determine Effect on Sys
IR 05000260/197901130 May 1979RO 50-260/79-011 on 790526:rod Inadvertently Pulled Three Notches During Attempt to Reach Criticality.Cause Not Established.Operator Interviewed
IR 05000260/198002517 June 1980RO-BFRO-50-260/8025:on 800617,Dresser Industries Safety Valves Identified as Possibly Having Guides W/Cracks. Condition Identified in Similar Valves Loaned to Another Util from Browns Ferry.Cause Unknown
IR 05000296/19780218 November 1978Supplementary Reportable Occurrence Rept#BFRO-50-296/7821 on 780817.Following Reactor Scram,Cooldown Rate Was Exceeded Due to Safety Valves Actuating & Not Completely Closing. Caused by Excessive Pilot Leakage
IR 05000296/19780228 November 1978RO#50-296/7822 on 780822:during Startup at 3% Thermal Pwr, MSRV 1-4 Opened & Did Not Reclose Completely,Resulting in Excessive Vessel Cooldown Rate,Due Apparently to Excessive Pilot & second-stage Leakage in the Valves
IR 05000296/19790182 November 1979RO-50-296/79-18:on 791030,during Logic Testing Per LPCI Mods,Simultaneous Starting of Two RHR Pumps Occurred.Caused by Mismatch Between Current Transformer Ratios on Normal Supply to Shutdown Boards.Transformers Will Be Changed
IR 05000296/197902111 December 1979RO 50-296/79-21:on 791208,w/load Approx 200 Mwe Following Return to Svc After Fuel Outage,Difficulty Occurred in Maintaining drywell-to-torus Pressure Differential.Caused by Leak Around Equipment Hatch Seal.Fasteners RetightenedBackfit
IR 05000296/198002430 June 1980RO-BFRO-50-296/8024:on 800628,during Routine Maint Shutdown, Approx 68 of 185 Control Rods Failed to Fully Insert When Reactor Was Manually Tripped.Unit Is Shut Down Until Cause Determined & Corrective Action Taken
ML16148A3963 December 1980LER 80-009 Has Been CancelledBackfit
ML17276B80231 December 1981BWR Transient Analysis Model Utilizing Retran Program.
ML18024A44929 September 1978LER#78-024/03L-0 on 780911:during Refueling While Performing Surveillance Instru SI-42B-31 2 Broken Wire Was Found on Signal Lead for RCIC Turbine High Steam Flow Switch PDIS-71- 1B Which Provides RCIC Isolation.Loose Connection Repaired
ML18024A45729 September 1978LER#78-025/01T-0 on 780917:during refueling,4 Mstv'S Exceeded Leakage Limits.Defective Valves Will Be Repaired & Retested
ML18024A49013 October 1978LER 78-016/01T-0:on 780930,cracking Discovered in 1-inch Instrument Line & 3/4-inch Bonnet Vent Line on FCV-68-1. Cause Undetermined
ML18024A49417 October 1978LER 78-026/03L-0:on 780924,during Refueling Outage,Smoke Detector XS-39-93KB Alarmed W/O Cause & Could Not Be Cleared.Caused by Normal Aging
ML18024A49825 October 1978LER 78-017/03L-0:on 781004,drywell Oxygen Concentration Was Not Reduced to 4% within 24 H Period After Placing Reactor in Run Mode.Caused by Personnel Safety Considerations During Repair of Inner Drywell Air Lock Repairs
ML18024A5182 November 1978Monthly Oper Rept for Oct 1978Packing leak
Scram Discharge Volume
ML18024A5218 November 1978Supplementary Reportable Occurence Rept BFRO-50-296/7822: on 780822,during Startup at 3 Percent Thermal Pwr,Msrv 1-4 Opened & Did Not Completely Close Resulting in Excessive Cooldown Rate.Caused by Excessive Pilot Leakage
ML18024A5238 November 1978Supplementary Reportable Occurrence Rept#BFRO-50-296/7821 on 780817.Following Reactor Scram,Cooldown Rate Was Exceeded Due to Safety Valves Actuating & Not Completely Closing. Caused by Excessive Pilot Leakage
ML18024A5278 November 1978LER#78-027/03L-0 on 781012:during Refueling Outage,Panel 3-25-327 Was Inoperable,Placing 2 Smoke Detector Zones Out of Svc.Caused by a Contact on Power Transfer Relay Which Failed to Close After Short Power Interruption
ML18024A5346 November 1978LER#78-028/03L-0 on 781014:during Refuel outage,1 Smoke Detector XS-39-108ZE in Mech Equip Room on Elevation 617 Caused False Alarm That Would Not Clear.Caused by Normal Natural Aging of Detector
ML18024A5388 November 1978RO#50-296/7822 on 780822:during Startup at 3% Thermal Pwr, MSRV 1-4 Opened & Did Not Reclose Completely,Resulting in Excessive Vessel Cooldown Rate,Due Apparently to Excessive Pilot & second-stage Leakage in the Valves
ML18024A56127 November 1978LER#78-030/03L-0 on 781031:evidence of Grease in 6 Snubbers Located in Core Spray,Main Steam & Residual Heat Removal Sys.Snubbers Replaced.Recurrence Control Action Incl Replacement of Grease Fittings W/Those Incompatible W/Guns
ML18024A5744 December 1978LER#78-018/03L-0 on 781103:reactor Pressure Switch PS-6B-96, Switch 1 Failed to Operate During Surveillance Testing. Switch Exercised & Adjusted
ML18024A5756 December 1978RO-50-296/782:Bendix Connectors Used Inside Primary Containment Which Failed post-aging Environ Test Were Modified by Potting Plug & Receptacle Portion of Connectors & Passed 10 Year Qualifying Tests
ML18024A5797 December 1978LER#78-020/03L-0 on 781110:during Normal Pwr Oper,Reactor & Turbine Bldg & Refueling Zone Ventilation Exhaust Monitor, RM-90-250 Became Inoperable.Instr & Its Sensing Line Dried Out & Returned to Svc
ML18024A58811 December 1978LER#78-031/01T-0 on 781128:during CRD Scram Timing & Associated LPRM Connect on Verification Noted That All LPRMs Had Been Connected in Reverse Order.Caused by Lack of Explanation in Documents Describing Connection Procedure