05000296/LER-1978-030-03, /03L-0 on 781031:evidence of Grease in 6 Snubbers Located in Core Spray,Main Steam & Residual Heat Removal Sys.Snubbers Replaced.Recurrence Control Action Incl Replacement of Grease Fittings W/Those Incompatible W/Guns

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/03L-0 on 781031:evidence of Grease in 6 Snubbers Located in Core Spray,Main Steam & Residual Heat Removal Sys.Snubbers Replaced.Recurrence Control Action Incl Replacement of Grease Fittings W/Those Incompatible W/Guns
ML18024A561
Person / Time
Site: Browns Ferry 
Issue date: 11/27/1978
From:
TENNESSEE VALLEY AUTHORITY
To:
Shared Package
ML18024A560 List:
References
LER-78-030-03L-01, LER-78-30-3L-1, NUDOCS 7812050201
Download: ML18024A561 (5)


LER-1978-030, /03L-0 on 781031:evidence of Grease in 6 Snubbers Located in Core Spray,Main Steam & Residual Heat Removal Sys.Snubbers Replaced.Recurrence Control Action Incl Replacement of Grease Fittings W/Those Incompatible W/Guns
Event date:
Report date:
2961978030R03 - NRC Website

text

. NUCLEAR REGULATORYCOMMISSION LICENSEE EVENT REPORT

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8 0 60 61 IzOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 Evidence of rease on the oil reservoir alemite fitting of six Bergen Paterson Model

~03 HS SA h draulic snubb ers was dis cover ed durin an ins ec tion.

The snubb ers were in the

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core s ra main steam and residual heat removal s stems.

The grease could have

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eventuall de raded the o eration of the snubbers (T.S. 3.6.H.1).

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hazard to the ublic health or safet

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fittin s not corn atible with rease uns.

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~ i i Form BF-17 BF 15.2 6/09/78

'ER SUPPLEMENTAL INFORMATION BFRO 296 /

7830 Technical Specification Involved 3

6 H 1 Reported Under Technical Specification Date of Occurrence

>0/3~/7g Time of Occurrence pim Unit Identification and Descri tion of Occurrence:

See attached sheet.

Conditions Prior to Occurrence:

Refueling outage in progress.

Action specified in the Technical Specification Surveillance Requirements met due to ino erable e ui ment.

Describe.

None.

Refueling in progress.

A arent Cause of Occurrence:

Maintenance personnel mistakenly infected grease into the hydraulic snubbers during routine lubrication.

Anal sis of Occurrence:

Functional testing of five snubbers with grease in the oil reservoir revealed no noticeable effect on the proper operation of the snubber.

Prolonged operation with grease in the reservoir could result in an inoperable snubber.

Corrective Action; The 6 snubbers were replaced.

The alemite fittings will be replaced during the refueling outages beginning with unit l,.cycle 2.

The hydraulic snubbers in the that entry in the drywell is required.

Failure Data:

None Tennessee Valley Authority - Browns Ferry Nuclear Plant

Identification and Descri tion of Occurrence:

As a result of finding evidence of grease on two hydraulic snubbers by the NRC inspector, an inspection of all the accessible hydraulic snubbers in the three units was conducted.

Four other hydraulic snubbers were found on unit 3 with evidence of grease on the alemite fitting. All the grease appeared fresh with no evidence of dust.

Investigation revealed that about one week earlier, the annual lubrication program had been initiated.

Discussion with personnel responsible for lubrication revealed no one knowingly had lubricated the snubbers although it was evident from the discussion that if they had lubricated the snubber, they would not have wiped off the lubricant.

Review of the lubri-cation schedule revealed that the snubbers were not on the schedule.

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11/27/78

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