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 Discovered dateReporting criterionTitleDescriptionLER
ENS 3971429 March 2003 11:00:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedDEGRADED CONDITION DUE TO LEAKAGE AT SMALL BORE INCONEL 600 PENETRATION
The following information was received from the licensee via facsimile
"The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73
"On March 29, 2003, at approximately 04:00 Mountain Standard Time (MST) engineering personnel performing preplanned visual examinations of reactor coolant System (RCS) piping in accordance with procedure requirements discovered boric acid residue on three RCS small bore Inconel 600 penetrations. One location was the RCS hot leg in-service thermowell 3JRCBTW0112HB. The visual observation was characterized as a small white trail of boron residue running down the hot leg approximately 2 inches. There were no signs of dripping, spraying, puddles of liquid, or liquid running down the nozzle or hot leg. The residue appeared dry. The other two were on pressurizer heater sleeves (nozzles) A-4 and A-18. The visual observation at these two locations was characterized as a small white buildup of boron residue around the heater sleeve as the sleeve enters the pressurizer bottom head. There does not appear to be residue running down the outside of the sleeves. There were no signs of dripping, spraying, puddles of liquid, or liquid running down the nozzle or (pressurizer). The residue appeared dry
"Technical Specifications (TS) Limiting Condition for Operation (LCO) 3.4.14 permits no reactor coolant system (RCS) pressure boundary leakage and therefore, the discovery of leakage (presumed boric acid residue) from the hot leg thermowell and the pressurizer heater sleeves was a degradation of a principal safety barrier. Therefore, the ENS notification of this event is in accordance with 10CFR50.72(b)(3)(ii). The control room personnel entered LCO 3.4.14 Condition B and are continuing to place the plant in Mode 5. The RCS was being cooled down in preparation for Unit 3's tenth refueling outage. At the time of discovery, the RCS was at approximately 520 degrees F and 2218 psia
"An investigation of this event will be conducted in accordance with the PVNGS (Palo Verde Nuclear Generating Station) corrective action program. The cracking of Alloy 600 components both at Palo Verde and industry-wide has been attributed to axially oriented, primary water stress corrosion cracking (PWSCC). PWSCC is not considered a significant threat to the structural integrity of the RCS boundary, thermowell, or heater sleeves as this type of cracking typically results only in small leaks
"The bases for this conclusion is that if PWSCC occurred at Palo Verde, the cracks would be predominately axial in orientation. As in this case, the cracks would result in visibly detectable leakage that would be apparent during visual examinations, performed as part of walkdown inspections, before significant damage to the reactor coolant boundary occurred
"Palo Verde has a program for replacing the Alloy 600 hot leg thermowells. This thermowell was scheduled for replacement during this refueling outage. The plans to replace the thermowell remain unchanged
"A mechanical nozzle sleeve assembly (MNSA) will be installed on each of the pressurizer heater sleeves
"No ESF actuations occurred and none were required. There were no structures, systems, or components that were inoperable at the time of discovery that contributed to this condition. There were no failures that rendered a train of a safety system inoperable and no failures of components with multiple functions were involved. The event did not result in the release of radioactivity to the environment and did not adversely affect the safe operation of the plant or health and safety of the public.
The licensee has informed the NRC Resident Inspector.
05000530/LER-2003-002
ENS 4034922 November 2003 05:53:0010 CFR 50.72(b)(3)(iv)(A), System ActuationValid Actuation of the "a" Emergency Diesel Generator During TestingThe following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On November 21, 2003, at approximately 22:53 Mountain Standard Time, Palo Verde Nuclear Generating Station Unit 2 experienced a valid actuation (start) of the 'A' Emergency Diesel Generator (EDG). Unit 2 had been performing testing of the capability to parallel the EDG 'A' with the Gas Turbine Generator #1 (alternate AC Power source for station blackout.) The Train 'A' 4.16 Kv bus had been successfully transferred to the EDG and loads carried by the EDG for approximately 5 minutes. When the EDG speed control was taken from 'droop' mode (load sharing) to 'isochronous' mode (fixed frequency,) the EDG output breaker tripped opened, resulting in a valid Loss of Power (LOP) signal based on undervoltage on the Train 'A' bus. The EDG resupplied the bus in the LOP mode. Offsite power remained available to both safety buses throughout the event. The other (Train 'B') safety bus is being supplied by offsite power and its EDG is operable. The offsite electrical grid is stable. Palo Verde Unit 2 is shutdown and defueled in its 11th refueling outage. No other ESF actuations occurred and none were required. There were no structures, systems, or components that were inoperable at the time of discovery that contributed to this condition. There were no failures that rendered a train of a safety system inoperable and no failures of components with multiple functions were involved. The event did not result in the release of radioactivity to the environment and did not adversely affect the safe operation of the plant or health and safety of the public. Troubleshooting will be conducted to determine the cause of the EDG output breaker opening. The licensee has notified the NRC Resident Inspector.05000529/LER-2003-002
ENS 405033 February 2004 22:35:0010 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
Technical Specification Required Shutdown Due to Rcs Pressure Boundary LeakageThe following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On February 3, 2004 at approximately 14:18 MST, Palo Verde Nuclear Generating Station (PVNGS) Unit 1 identified reactor coolant system (RCS) pressure boundary leakage. PVNGS Unit 1 was in Mode 1 (Power Operation) at 99% power with normal RCS temperature and pressure at the time of discovery. A normal reactor shutdown was commenced at 15:35. Technical Specification Limiting Condition for Operation 3.4.14 (RCS Operational Leakage) allows no pressure boundary leakage and requires the plant to be in Mode 3 (Hot Shutdown) within 6 hours and Mode 5 (Cold Shutdown) within 36 hours and TLCO 3.14.103 (Structural Integrity). The leakage was discovered on a High Pressure Safety Injection Drain Valve (SIA-V056) with is connected to the RCS loop 1 hot leg and is non isolable. The location of the leak is at a weld on the valve socket weld and is estimated at 10 drops per second. No automatic or manual reactor protection system or engineered safety features actuations occurred and none were required. There were no other component failures, testing or work in progress that contributed to the leak. The leak is located within the containment building, therefore there is no release of radioactivity to the environment and no impact to the health and safety of the public. There is no elevated RCS activity and heat removal is via normal steaming to the main turbine condenser, The electric grid is stable. The licensee has notified the NRC resident Inspector.05000528/LER-2004-001
ENS 4053320 February 2004 17:33:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification Due to a Press Release Concerning the Unit 2 ShutdownThe following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the Information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. This ENS notification is to inform the agency of the shutdown of Palo Verde Nuclear Generating Station Unit 2, due to increasing primary to secondary leakage, for which a news release has been issued. Unit 2 was shutdown to Mode 3 on February 19, 2004 at 18:28 Mountain Standard Time (MST) following detection of increased primary to secondary leakage at approximately 15:22 MST. The leakage was less than the Technical Specification 3.4.14(d) limit of 150 gallons per day through any one SG. Steam generator #1 was isolated at approximately 18:40 MST. The unit has been cooled down to Mode 5 in preparation of maintenance to repair the steam generator. Current plant conditions are approximately 160 degrees F and 350 psia. The decision to issue a press release was made at approximately 09:00 MST on February 20, 2004. The press release was issued at approximately 10:33 MST. The NRC Resident Inspector has been notified of this ENS call. This is the 1st cycle using these Steam Generators which were replaced in 2003. The licensee indicated that the change in in primary to secondary leakage was a step increase but was unable to accurately quantify the amount since it was less than 20 gallons per day.
ENS 4055629 February 2004 07:00:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedBoric Acid Residue Found on Pressurizer Heater SleeveThe following event description is based on information currently available. If through subsequent reviews of this event, additional Information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On February 29, 2004, at approximately 05:21 Mountain Standard Time (MST) engineering personnel performing preplanned visual examinations of reactor coolant system (RCS) piping in accordance with procedure requirements discovered boric acid residue on the A03 pressurizer heater sleeve. The heater sleeve is an alloy 600 penetration. The visual observation was characterized as a small white buildup of boron residue around the heater sleeve as the sleeve enters the pressurizer bottom head. There does not appear to be residue running down the outside of the sleeve. There were no signs of dripping, spraying, puddles of liquid, or liquid running down the nozzle or pressurizer. The residue appeared dry. Technical Specifications (TS) Limiting Condition for Operation (LCO) 3.4.14 permits no reactor coolant system (RCS) pressure boundary leakage and therefore, the discovery of leakage (presumed boric acid residue) from the pressurizer heater sleeve was a degradation of a principal safety barrier. Therefore, the ENS notification of this event is in accordance with 10CFR50.72(b)(3)(ii). The control room personnel entered LCO 3.4.14 Condition B and are taking action to place the plant In Mode 5 within 36 hours. The Unit had been shutdown and was being maintained in Mode 3 while troubleshooting a turbine-generator excitation problem. At the time of discovery, the RCS was at approximately 565 degrees F and 2245 psia. An investigation of this event will be conducted in accordance with the PVNGS corrective action program. No ESF actuations occurred and none were required. There were no structures, systems, or components that were inoperable at the time of discovery that contributed to this condition. There were no failures that rendered a train of a safety system inoperable and no failures of components with multiple functions were involved. The event did not result in the release of radioactivity to the environment and did not adversely affect the safe operation of the plant or health and safety of the public. The licensee notified the NRC Resident Inspector.05000530/LER-2004-001
ENS 405611 March 2004 23:49:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleasePress Release Regarding Boron Residue

The license provided the following via facsimile:

"This ENS notification is to inform the agency of a news release that was issued 03/01/04 at 1649 Mountain Standard Time (MST) regarding the shutdown of Palo Verde Nuclear Generating Station Unit 3 and discovery of boron residue on a pressurizer heater sleeve which was reported to the Headquarters Operations Center in ENS ID 40556.

The unit has been cooled down to Mode 5 in preparation of maintenance to repair the pressurizer heater sleeve. Current plant conditions are approximately 125 degrees F and 35 psia. The NRC Resident Inspector has been notified of this ENS call.

ENS 4068017 April 2004 14:26:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification - Small Fire at Palo Verde 1: Two Employees Injured, No Plant Equipment Damage

On Saturday, April 17, 2004, at approximately 07:26 (MST), a fire in the Palo Verde Nuclear Generating Station Unit 1 turbine building resulted in two injuries due to burns. Both individuals were transported offsite for treatment. One of the two was airlifted with suspected second degree burns. Neither involved any radioactive contamination. No press release is planned, but media attention has already been observed in response to media monitoring communications on local police/fire scanners. Calls have been received from several TV stations. One local station broadcast the fire and injuries at approximately 09:40 (MST). Palo Verde Unit 1 is shutdown and defueled in its eleventh refueling outage. The fire was associated with pre-heating for welding in the turbine building. It is suspected that solvent vapor in the vicinity of the pre-heating activity may have flashed. The fire was extinguished in less than 15 minutes and no emergency plan classification was declared or required as a result of the fire. The NRC Resident Inspector has been notified of the event and this ENS notification. The fire occurred near the Main Feed Pump Turbine Alpha, which was dismantled at the time. There appears to be no physical damage to any plant equipment, although some nearby cleaning rags were partially burned.

  • * * * UPDATE FROM D. DAILEY TO M. RIPLEY 1635 ET 04/18/04 * * * *

1) Both workers received facial burns. One was treated and released at approximately 11:00 MST on Saturday, April 17, 2004. The other was released during the morning of Sunday, April 18, 2004. 2) There was no equipment damage as a result of the fire. The apparent cause of the fire in the "A" main feed pump turbine lower shell was residual isopropyl alcohol in a drain hole. The alcohol is used to clean solvent residue to have the turbine shell oil-free for NDE (non-destructive examination) purposes. The NRC Resident Inspector has been notified of this ENS update. Notified NRC Region 4 Duty Officer (D. Powers)

ENS 407379 May 2004 03:39:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationManual Reactor Trip During Physics Testing Due to Control Element Assembly Slipping 6 Inches.On May 8, 2004, at approximately 20:39 Mountain Standard Time (MST) Palo Verde Unit 1 operations manually tripped the reactor when a Control Element Assembly (CEA) slipped approximately 6 inches (CEA # 89) while conducting physics testing (at 10E-02 percent power) following Unit 1's eleventh refueling outage. Unit 1 was at normal operating temperature and pressure prior to the trip. All CEAs inserted fully into the reactor core (Initial Conditions: Regulating groups 1, 2 & 5 were fully withdrawn, regulating group 3 was fully inserted, regulating group 4 was being inserted when CEA # 89 slipped approximately 6 inches. Shutdown groups were fully withdrawn). This was an uncomplicated reactor trip. No emergency classification was required per the Emergency Plan. No automatic ESF actuations occurred and none were required. Safety related buses remained energized during and following the reactor trip. No LCOs (Limiting Conditions of Operations) have been entered as a result of this event. No major equipment was inoperable prior to the event that contributed to the event. Unit 1 is stable at normal operating temperature and pressure in Mode 3 (Hot Standby). The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The event did not adversely affect the safe operation of the plant or the health and safety of the public. The Senior Resident Inspector was informed of the Unit 1 reactor trip.
ENS 407957 June 2004 21:58:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationReactor Trip Due to Main Turbine Electro-Hydraulic Control System FailureOn June 7, 2004, at approximately 14:58 Mountain Standard Time (MST) while at 99% RTP (rated thermal power), Palo Verde Unit 3 experienced an apparent electro-hydraulic control (EHC) system fault resulting in Combined Intercept Valve (CIV) closure. This plant upset was followed by a Reactor Power Cutback System (RPCS) initiation. Several seconds later the Reactor automatically tripped on Lo DNBR from approximately 65% RTP. Unit 3 was at normal temperature and pressure prior to the trip. All CEAs (control rod assemblies) inserted fully into the reactor core. This was an uncomplicated reactor trip. No emergency classification was required per the Emergency Plan. No automatic ESF actuations occurred and none were required. Safety related buses remained energized during and following the reactor trip. The Emergency Diesel Generators did not start and were not required. The offsite power grid is stable. No significant LCOs have been entered as a result of this event. No major equipment was inoperable prior to the event that contributed to the event. Unit 3 is stabilized at normal temperature and pressure at approximately 565 degrees F and 2250 psia in Mode 3. The reactor coolant system remains in normal forced circulation with heat removal via the steam bypass control system to the condenser and feedwater from the non-essential auxiliary feedwater system. The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The event did not adversely affect the safe operation of the plant or the health and safety of the public. The Senior Resident Inspector was informed of the Unit 3 reactor trip and this notification. The Senior Resident Inspector was on-site at the time of the reactor trip.05000530/LER-2004-002
ENS 4081414 June 2004 14:44:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Alert Declared - Reactor Trip Due to Loss of Off Site Power

On June 14, 2004, at approximately 07:44 Mountain Standard Time (MST) all three units at the Palo Verde Nuclear Generating Station experienced automatic reactor trips coincident with a grid disturbance and loss of offsite power in the Palo Verde Switchyard. Unit 2 declared an ALERT Emergency Plan classification at approximately 07:54 due to a loss of AC power to essential buses reduced to a single power source for greater than 15 minutes such that any additional single failure would result in a station blackout. Subsequently, at 09:51 Unit 2 downgraded the Emergency Plan classification to a NOTIFICATION OF UNUSUAL EVENT when AC power was restored from a single essential bus to both essential buses. Units 1 and 3 declared a NOTIFICATION OF UNUSUAL EVENT at 07:53 MST due to a loss of offsite power to essential buses for greater than 15 minutes. The NOTIFICATION OF UNUSUAL EVENT was terminated for all 3 units at 12:07 MST. Unit 1 and 2 manually initiated a Main Steam Isolation System ESF actuation by procedure. Unit 3 received an automatic Main Steam Isolation System ESF actuation. Due to the loss of offsite power, the Emergency Plan Technical Support Center (TSC) was unavailable. The Unit 2 Satellite TSC was to be staffed by the Emergency Response Organization in response to the loss of assessment capability. Power to the TSC has since been restored. The Emergency Plan ALERT declaration includes staffing of the Joint Emergency New Center to address expected media interest. All three units were at normal operating temperature and pressure prior to the trip. All CEAs inserted fully into the reactor cores. All Emergency Diesel Generators (EDGs) (2 per unit) associated with each of the 3 units started as expected in response to the loss of offsite power to their safety buses. Unit 2's train "A" EDG started, but did not indicate volts or amps and was manually shutdown. The offsite power grid had several perturbations for approximately one hour following the event but has been stable since. LCO 3.8.1, AC Sources - Operating, was entered in each unit as a result of this event. Heat removal is to atmosphere via atmospheric dump valves in natural circulation. Main steam safety valves may have lifted for a brief time. Restoration of forced reactor coolant circulation is pending assurance that the offsite power grid can reliably support the load. No major equipment was inoperable prior to the event that contributed to the event. All 3 units are stable at normal operating temperature and pressure in Mode 3. The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The event did not adversely affect the safe operation of the plant NRC Resident Inspector was notified. FBI Jeff Muller and Mr. Rosales (Mexican National Commission of Nuclear Safety and Safeguards (CNSNS)) were notified.

  • * * Update at 1815 @ 06/14/04 * * *

Notified Reg 4 RDO (Graves), NRR (Bateman), DHS (Lee), FEMA (Canupp), DOE (Sal Moroni), EPA (Stalcup), EPA (Crews), HSS (Davidson), and Mexico (Rosales) NOTE: See events 40815, 40816 and 40818

ENS 4081514 June 2004 14:44:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Unusual Event Declared Due to Reactor Trip Due to Loss of Off Site Power

On June 14, 2004, at approximately 07:44 Mountain Standard Time (MST) all three units at the Palo Verde Nuclear Generating Station experienced automatic reactor trips coincident with a grid disturbance and loss of offsite power in the Palo Verde Switchyard. Unit 1 declared a NOTIFICATION OF UNUSUAL EVENT at 07:53 MST due to a loss of offsite power to essential buses for greater than 15 minutes. The NOTIFICATION OF UNUSUAL EVENT was terminated at 12:07 MST. Unit 1 manually initiated a Main Steam Isolation System ESF actuation by procedure. Due to the loss of offsite power, the Emergency Plan Technical Support Center (TSC) was unavailable. The Unit 2 Satellite TSC was to be staffed by the Emergency Response Organization in response to the loss of assessment capability. Power to the TSC has since been restored. The unit was at normal operating temperature and pressure prior to the trip. All CEAs inserted fully into the reactor cores. All Emergency Diesel Generators (EDGs) (2 per unit) associated with the unit started as expected in response to the loss of offsite power to their safety buses. The offsite power grid had several perturbations for approximately one hour following the event but has been stable since. LCO 3.8.1, AC Sources - Operating, was entered as a result of this event. Heat removal is to atmosphere via atmospheric dump valves in natural circulation. Main steam safety valves may have lifted for a brief time. Restoration of forced reactor coolant circulation is pending assurance that the offsite power grid can reliably support the load. No major equipment was inoperable prior to the event that contributed to the event. The Unit is stable at normal operating temperature and pressure in Mode 3. The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The event did not adversely affect the safe operation of the plant NRC Resident Inspector was notified. FBI Jeff Muller and Mr. Rosales (Mexican National Commission of Nuclear Safety and Safeguards (CNSNS)) were notified.

  • * * Update at 1815 @ 06/14/04 * * *

Notified Reg 4 RDO (Graves), NRR (Bateman), DHS (Lee), FEMA (Canupp), DOE (Sal Moroni), EPA (Stalcup), EPA (Crews), HSS (Davidson), and Mexico (Rosales) Note: see related events # 40814, 40816 and 40818

ENS 4081614 June 2004 14:44:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Unusual Event Due to Reactor Trip Due to Loss of Off Site Power

On June 14, 2004, at approximately 07:44 Mountain Standard Time (MST) all three units at the Palo Verde Nuclear Generating Station experienced automatic reactor trips coincident with a grid disturbance and loss of offsite power in the Palo Verde Switchyard. Unit 3 declared a NOTIFICATION OF UNUSUAL EVENT at 07:53 MST due to a loss of offsite power to essential buses for greater than 15 minutes. The NOTIFICATION OF UNUSUAL EVENT was terminated at 12:07 MST. Unit 3 received an automatic Main Steam Isolation System ESF actuation. Due to the loss of offsite power, the Emergency Plan Technical Support Center (TSC) was unavailable. The Unit 2 Satellite TSC was to be staffed by the Emergency Response Organization in response to the loss of assessment capability. Power to the TSC has since been restored. The unit was at normal operating temperature and pressure prior to the trip. All CEAs inserted fully into the reactor cores. All Emergency Diesel Generators (EDGs) (2 per unit) associated with the unit started as expected in response to the loss of offsite power to their safety buses. The offsite power grid had several perturbations for approximately one hour following the event but has been stable since. LCO 3.8.1, AC Sources - Operating, was entered as a result of this event. Heat removal is to atmosphere via atmospheric dump valves in natural circulation. Main steam safety valves may have lifted for a brief time. Restoration of forced reactor coolant circulation is pending assurance that the offsite power grid can reliably support the load. No major equipment was inoperable prior to the event that contributed to the event. The Unit is stable at normal operating temperature and pressure in Mode 3. The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The event did not adversely affect the safe operation of the plant NRC Resident Inspector was notified. FBI Jeff Muller and Mr. Rosales (Mexican National Commission of Nuclear Safety and Safeguards (CNSNS)) were notified.

  • * * Update at 1815 @ 06/14/04 * * *

Notified Reg 4 RDO (Graves), NRR (Bateman), DHS (Lee), FEMA (Canupp), DOE (Sal Moroni), EPA (Stalcup), EPA (Crews), HSS (Davidson), and Mexico (Rosales) Note: see related events 40815 , 40814 and 40818

ENS 4087014 July 2004 08:35:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationAutomatic Reactor Trip Following a Main Generator TripThe following information was received from the licensee via facsimile: The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On July 14, 2004, at approximately 01:35 Mountain Standard Time (MST) Palo Verde Unit 2 experienced a Main Generator Trip immediately followed by an automatic Reactor Trip. The reactor was at approximately 100% power and normal operating temperature and pressure prior to the event. The cause of the Main Generator Trip was most likely the result of electrical storm conditions present at the site at the time of the trip. Unit 2 was at normal operating temperature and pressure prior to the trip. All CEAs inserted fully into the reactor core. Heat removal was maintained to the condenser via the steam bypass control system. This was an uncomplicated reactor trip, No emergency classification was required per the Emergency Plan. No automatic ESF actuations occurred and none were required. Safety related buses remained energized during and following the reactor trip. The Emergency Diesel Generators did not start and were not required. The offsite power grid is stable. No LCOs have been entered as a result of this event. No major equipment was inoperable prior to the event that contributed to the event. Unit 2 Is stable at normal operating temperature and pressure in Mode 3. The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The event did not adversely affect the safe operation of the plant or the health and safety of the public. The (NRC) Senior Resident Inspector was informed of the Unit 2 reactor trip. No primary or secondary power-operated or manual relief valves lifted as a result of the plant transient. Units 1 and 3 were unaffected by the trip on Unit 2. Offsite power was maintained to Unit 2 safety busses throughout the event.05000529/LER-2004-002
ENS 4087414 July 2004 23:30:00Other Unspec ReqmntAll Three Units Exceeded the Maximum Power Level Specified in Their Operating LicensePalo Verde Nuclear Generating Station Units 1, 2, and 3 determined that the Maximum Power Level specified in Operating License Condition 2.C(1) was exceeded in the past due to a nonconservative feedwater flow input in the secondary calorimetric calculation since installation of ultrasonic feedwater flow measurement (UFM) instrumentation in Units 1 and 3 in 1999 and 2000 in Unit 2. On 06/09/2004, the vendor (Caldon) notified Palo Verde via a letter that there may be an error of up to one to one and one-half percent in the flow measurement. As a compensatory measure, all three units reduced power and removed the UFM from service. Feedwater flow venturis are used for measurement with the UFM out of service. Engineering evaluation concluded on 07/14/2004 the maximum Palo Verde specific calorimetric error was approximately 38.76 Mw in Units 1 and 3 and 39.90 MW in Unit 2 or approximately 1 %. The error resulted in core power levels above the Operating License limit of 3876 MW thermal in Units 1 and 3 and the Operating License limit of 3990 MW thermal In Unit 2 while the UFM was in service. This report is being made because a review of historical operating data revealed that the Maximum Power Level was exceeded. The Palo Verde safety analyses bound a power level of 102%. Power level did not exceed the safety analysis. No ESF actuations occurred and none were required as a result of the miscalibration. There were no other structures, systems, or components that were inoperable at the time of discovery that contributed to this condition. There were no failures that rendered a train of a safety system inoperable and no failures of components with multiple functions were Involved. The event did not result in the release of radioactivity to the environment and did not adversely affect the safe operation of the plant or health and safety of the public. The NRC Resident Inspector was notified.
ENS 4091331 July 2004 01:45:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
Air Void in Post-Loca Recirculation Piping SystemOn July 30, 2004, at approximately 18:45 Mountain Standard Time (MST), Palo Verde Nuclear Generating Station Units 1, 2, and 3 were operating at approximately 100% power at normal operating temperature and pressure when it was discovered that a void in the post-LOCA (Loss Of Coolant Accident) recirculation piping from the containment sump may have prevented fulfillment of the safety function to remove residual heat and mitigate the consequences of a Loss of Coolant Accident. The volume of the ECCS (Emergency Core Cooling System) piping sections between the closed containment sump isolation butterfly MOVs (SIAUV0673/0674 and SIBUV0675/0676) and the associated train sump recirculation check valves (SIAV205 and SIBV206) are void of water and occupied with air (Approx. 120 cubic feet). The concern is that during a Recirculation Actuation Signal (RAS) the trapped volume of air between the isolation valves and the downstream check valve cold potentially enter the operating SI pumps (HPSI and CS), which could potentially cause cavitations and/or air binding of the pumps or possibly a water hammer event. RAS does not occur for approximately 20 minutes, or longer following a LOCA. In accordance with Generic Letter 91-18, substitution of manual action for automatic action to open the inner containment sump isolation valves following a LOCA, but prior to the RAS setpoint will allow the void to clear, with the exception of a small section between the outer containment isolation valve and the check valve. Engineering had provided reasonable assurance that the recirculation check valve void will not result in an unacceptable void fraction forming in the HPSI/Containment Spray pump suction piping and pump. The Control Room Operators have been briefed on the need to perform the manual Operator action to open the inboard ECCS Sump isolation valves (SIAUV673 and SIBUV675) upon receipt of a Containment Spray Actuation System (CSAS) actuation. Each Shift Crew will be briefed accordingly until the EOPs are revised to incorporate this action (will take about 24 hours to be incorporated). Engineering continues to evaluate this condition. There were no RPS/ESF actuations, and none were required. There were no structures, systems or components that were inoperable at the start of (the) event that contributed to the event. This condition did not result in any challenges to the fission product barrier or result in any releases of radioactive materials. There were no adverse safety consequences or implications as a result of this event. This condition did not adversely affect the safe operation of the plant or health and safety of the public. The NRC Resident Inspector was notified of this event by the licensee.05000528/LER-2004-009
ENS 4122424 November 2004 19:20:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentEccs Loops Declared Inoperable in Support of Log Term Accident Mitigation

The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On November 24, 2004, at approximately 12:20 Mountain Standard Time (MST), Palo Verde Nuclear Generating Station Unit 3 was operating at 0% power at approximately normal operating temperature and pressure when 3 of the 4 ECCS injection check valves were identified to be in a degraded condition. While performing normal torque verifications on the bonnet bolts for these check valves, it was identified that the graphoil seals were degraded in that the seal material had extruded past the retaining ring. Although there was no evidence of actual leakage associated with these valves, the long term integrity of the valves during post accident operation could not be assured. As a result, the Operators conservatively declared both trains of ECCS inoperable per LCO 3.5.3 and 3 of 4 Safety Injection Tanks inoperable per LCO 3.5.1, requiring entry into LCO 3.0.3. Operations also declared both RCS loops inoperable per LCO 3.4.5. A cooldown and depressurization of the RCS is in progress to Mode 5. Unit 3 was preparing for Mode 2 entry following a refueling outage when the degraded check valve seals were identified. Engineering continues to evaluate this condition. There were no RPS/ESF actuations, and none were required. There were no structures, systems or components that were inoperable at the start of event that contributed to the event. This condition did not result in any challenges to the fission product barrier or result in any releases of radioactive materials. There were no adverse safety consequences or implications as a result of this event. This condition did not adversely affect the safe operation of the plant or health and safety of the public. The NRC Resident Inspector has been notified of this condition and this ENS notification.

  • * * RETRACTION FROM DAN MARKS TO BILL HUFFMAN AT 14:52 EST ON 12/14/04 * * *

Engineering has determined that these RCS PIV's (Pressure Isolation Valves) were always capable of performing their safety function. The extrusion of the graphite seal material for the check valves did not affect the capability of the RCS PIV check valves safety function and did not present a danger to the pressure boundary of the RCS. It was estimated that no more than about 5% of the graphite material was extruded. The loss of this small amount of packing material, did not challenge the integrity of the seal. This is based on industry experience and the results of Palo Verde tests. Also, the functionality of the SI check valves disc was not compromised since the internal disc to seat clearances achieved were within the range desired. Nevertheless, the seals for valves SIEV227, 237 & 247 were replaced while in Mode 5 to add additional margin to the joint design. LCO 3.0.3 and the other impacted LCO entries (3.4.5, 3.5.1, 3.5.3) were conservative and were not required. Therefore, this 10CFR50.72(b)(3)(v)(D) notification, ENS ID # 41224 of 11/24/2004, 20:01 ET, is retracted and no followup LER will be submitted for this event. The NRC Resident Inspector has been notified of the retraction and this notification. R4DO (Pick) notified.

ENS 4126817 December 2004 17:53:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notifications Made Due to Spill of Approximately 1400 Pounds of Sulfuric AcidOn 12/17/2004 at approximately 10:53 MST, Palo Verde Nuclear Generating Station (PVNGS) notified the Department of Transportation/US. Coast Guard National Response Center of a sulfuric acid spill to the ground at the Water Reclamation Facility. The source of cooling water for PVNGS is treated sewage effluent. The effluent is conveyed to the site through approximately 35 miles of pipeline, and treated in the onsite water reclamation facility to meet plant water quality requirements. The acid spill has no impact to the radiological health and safety of the workers or the public. The spill is estimated at 1400 pounds. The reportable quantity is 1000 pounds. The sulfuric acid is classified as a CERCLA Hazardous Substance and EPCRA Extremely Hazardous Substance. The release has been isolated and the apparent cause is a leak in an underground section of pipe. There were no injuries and no known or anticipated acute or chronic health risks. The National Response Center report number is 744571. The Arizona Department of Environmental Quality was also informed at 10:51 MST. There was no impact to the three generating units from the spill at the Water Reclamation Facility which is located at a separate part of the Owner Controller Area. All 3 PVNGS Units are operating at approximately 100% in Mode 1. The NRC Resident has been notified of the event and this notification.
ENS 4130431 December 2004 17:42:0010 CFR 50.72(b)(3)(iv)(A), System ActuationPlant Had Auto Start and Loading of Two Emergency Diesel GereratorsOn December 31, 2004, at approximately 10:42 Mountain Standard Time (MST) a valid actuation of the Palo Verde Nuclear Generating Station Unit 2 Train A Emergency Diesel Generator (EDG) and Unit 3 Train B EDG occurred as a result of undervoltage on their respective safety buses. Both EDGs started and loaded as designed. The loss of power to the two safety buses was the result of the deenergization of Startup Transformer X01 when Westwing transmission line #2, one of seven 525 kV transmission lines at the Palo Verde switchyard, relayed off. Prior to the event, maintenance and testing were in progress on Westwing Line #1. The apparent cause of the event was inadvertent operation of an adjacent Line #2 protective relay while testing Line #1. Both Units 2 and 3 entered Technical Specification LCO 3.8.1 Condition A for one (of two) required offsite circuits inoperable. Normal offsite power was restored to each safety bus in Units 2 and 3 (at 11:45 MST), the LCO exited and the Unit 3 EDG returned to standby. During shutdown of the Unit 2 A EDG following successful loading of the Safety bus, the EDG was declared inoperable due to a Jacket Water leak and LCO 3.8.1 Condition B was entered. No Emergency Plan declaration was made and none was required. Both units were at approximately 100% power, at normal operating temperature and pressure prior to and following the EDG actuations. No other ESF actuations occurred and none were required. No major equipment was inoperable prior to the event that contributed to the event. The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The event did not adversely affect the safe operation of the plant or the health and safety of the public. The NRC Resident Inspector has been notified of the ESF actuation and this ENS notification.05000529/LER-2004-003
ENS 413797 February 2005 05:19:0010 CFR 50.72(b)(3)(iv)(A), System ActuationEmergency Diesel Start Due to Bus DeenergizationThe following information was provided by the licensee via facsimile: The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On February 6, 2005, at approximately 22:19 Mountain Standard Time (MST) a valid actuation of the Palo Verde Nuclear Generating Station Unit 1 Train `B' Emergency Diesel Generator (EDG) occurred as a result of undervoltage on its respective safety bus (PBB-S04). EDG 'B' started and loaded as designed to energize PBB-S04. The loss of power to the safety bus was the result of a fault associated with 13.8KV breaker NAN-SO6J which caused breakers NAN-SO6H (normal power supply), NAN-S06K (alternate power supply), and NAN-SO6J (EOF & TSC Bldg power supply) to all trip open on Overcurrent. This action resulted in the deenergization of NAN-S06, NAN-S04, and PBB-S04. The PVNGS Fire Department and Auxiliary Operators responded to a report of smoke and upon arrival found no fire. The Fire Department verified the fire was completely extinguished and there were no extensions (secondary fires). Unit 1 entered Technical Specification LCO 3.8.1, Condition 'A', for one (of two) required offsite circuits inoperable. Various other Technical Specifications LCO's were momentarily entered and exited for PBB-S04 being deenergized for approximately 7 seconds. No Emergency Plan declaration was made and none was required. Unit 1 was at approximately 100% power, at normal operating temperature and pressure prior to and following the EDG actuation. No other ESF actuations occurred and none were required. No major equipment was inoperable prior to the event that contributed to the event. The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The event did not adversely affect the safe operation of the plant or the health and safety of the public. The NRC Resident Inspector has been notified of the ESF actuation and this ENS notification. The B EDG is providing power to PBB-S04. Due to loss of power to the TSC, the TSC Diesel started and is providing power to the TSC. The Backup EOF located in Buckeye, AZ will be used in the case of an emergency event. There were no reported injuries. There was damage to the NAN-S06J breaker and it has been isolated. The event has been entered into the site's corrective action program for determining the cause of the breaker trip and damage. This event has no effect on the operation of the other site units.05000528/LER-2005-001
ENS 413899 February 2005 08:04:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownTechnical Specifications Required Shutdown Due to Loss of Normal and Alternate Power to Safety BusThe following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On February 9, 2005, at approximately 01:04 MST, Palo Verde Nuclear Generating Station (PVNGS) Unit 1 commenced a reactor shutdown required by Technical Specification 3.8.1. Limiting Condition for Operability (LCO) 3.8.1 requires two independent AC sources be available. On February 6, 2005, at approximately 22:19 Mountain Standard Time (MST) a valid actuation of the Palo Verde Nuclear Generating Station Unit 1 Train 'B' Emergency Diesel Generator (EDG) occurred as a result of under-voltage on its respective safety bus (PBB-S04). EDG 'B' started and loaded as designed to energize PBB-S04. (Reference EN #41379 reported on 02/06/2005). The loss of power to the safety bus was the result of a fault associated with 13.8KV breaker NAN-SO6J which caused breakers NAN-S06H (normal power supply), NAN-S06K (alternate power supply), and NAN-S06J (EOF & TSC Bldg power supply) to all trip open on over-current. This action resulted in the de-energization of NAN-SO6, NAN-S04, and PBB-S04. PVNGS will be unable to make repairs and restore the required second independent AC power source with the allowed 72 hour required action time frame. The event did not result in the release of radioactivity to the environment and did not adversely affect the safe operation of the plant or health and safety of the public. The NRC Resident Inspector has been notified.05000528/LER-2005-001
ENS 4145128 February 2005 21:57:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessMajor Loss of Siren Coverage within the Emergency Planning ZoneThe following information was provided by the licensee via facsimile (licensee text in quotes): The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On February 28, 2005 at approximately 14:57 Mountain Standard Time, the Palo Verde Emergency Preparedness Program Manager was notified of vandalism to a single siren (#42) that resulted in the siren being inoperable. Based on evidence from previous testing, the vandalism has been established to have occurred sometime between 15:00, Friday, 02/25/2005 and 03:00, Saturday, 02/26/2005. The affected siren is estimated to impact approximately 116 members of the population (7.3%) in the emergency planning zone (EPZ) within 5 miles. Palo Verde's reporting criterion is a loss of capability to inform greater than 5% of the population within 5 miles (or 10% within 5 to 10 miles) for greater than 1 hour. This call is being placed due to the relatively large segment of the population affected, and the uncertainty of the length of time that will be needed to restore the siren to operable condition. The Palo Verde Emergency Plan (section 6.6.2.1) has a contingency for dispatching Maricopa County Sheriff's Office (MCSO) vehicles with loud speakers to alert persons within the affected area(s) when sirens are inoperable. There are no events in progress that require siren operation. The NRC Resident Inspector has been notified of the siren failure and this ENS call.
ENS 414667 March 2005 15:10:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessTwo Emergency Sirens InoperableThe following information was received from the licensee via facsimile (licensee text in quotes): The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On March 7, 2005 at approximately 08:10 Mountain Standard Time, the Palo Verde Emergency Preparedness Program Manager was notified of vandalism to two sirens, #18 and #23, that resulted in the sirens being inoperable. The affected sirens are estimated to impact approximately 465 (total) members of population (approximately 29%) in the emergency planning zone (EPZ) within 5 miles. Palo Verde's reporting criterion is a loss of capability to inform greater than 5% of the population within 5 miles (or 10% within 5 to 10 miles) for greater than 1 hour. This call is being placed due to the relatively large segment of the population affected, and the uncertainty of the length of time that will be needed to restore the siren to operable condition. The Palo Verde Emergency Plan (section 6.6.2.1) has a contingency for dispatching Maricopa County Sheriff's Office (MCSO) vehicles with loud speakers to alert persons within the affected area(s) when sirens are inoperable. There are no events in progress that require siren operation. The NRC Resident Inspector has been notified of the siren failure and this ENS call. The vandals cut the battery cables and removed the batteries. The theft has been reported to the MCSO.
ENS 4148613 March 2005 01:45:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Operability of One Emergency Evacuation SirenThe following was provided by the licensee: The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On March 12, 2005 at approximately 18:45 Mountain Standard Time, the Palo Verde Emergency Preparedness Program Manager was notified of an inoperable single siren #36. Palo Verde has had 4 other sirens vandalized by breaking locks and stealing the internal battery since approximately February 25, 2005. The specific cause of this siren being inoperable has not been determined. Based on evidence from previous testing, this loss of siren #36 has been established to have occurred sometime between 22:00, Friday, 03/11/2005 and 03:00, Saturday, 03/12/2005. The affected siren is estimated to impact approximately 82 members of population (5.1 %) in the emergency planning zone (EPZ) within 5 miles. Palo Verde's reporting criterion is a loss of capability to inform greater than 5% of the population within 5 miles (or 10% within 5 to 10 miles) for greater than 1 hour. This call is being placed due to the relatively large segment of the population affected and the uncertainty of the length of time that will be needed to restore the siren to operable condition. The Palo Verde Emergency Plan (section 6.6.2.1) has a contingency for dispatching Maricopa County Sheriff's Office (MCSO) vehicles with loud speakers to alert persons within the affected area(s) when sirens are inoperable. Palo Verde has also been informed that Siren #42, previously inoperable due to the same vandalism and reported in EN #41451 on February 28, 2005, has been returned to service. There are no events in progress that require siren operation. There was not anything unusual or not understood concerning this event and all systems functioned as required. The NRC Resident Inspector has been notified of the siren failure and this ENS call. The licensee will inspect the siren on Sunday or Monday to determine if vandalism is involved.
ENS 4149716 March 2005 01:51:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notifications Due to Caustic SpillThe following information was provided by the licensee via facsimile (licensee text in quotes): The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On March 15, 2005 at approximately 18:51 Mountain Standard Time (MST), the Palo Verde Nuclear Generating Station informed another government agency, the EPA/DOT National Response Center, of a caustic spill, related to the protection of the environment. Notification was also made to the Arizona Department of Environmental Quality and the Arizona Department of Public Safety (State Police). No news release is planned or expected. A commercial tanker truck was transferring caustic sodium hydroxide at Unit 1 when a drip was observed from the transfer hose at approximately 16:54 MST. The spill was limited to approximately one quart outside of the spill containment berm. The evolution was terminated and the tanker truck was driven out of the Protected Area. A drip trail was later discovered at approximately 18:00 along the path of the truck out of the Protected Area, including a puddle of approximately 3 gallons in the sally port (access point). The truck was returning to Phoenix, AZ. The spill quantity on-site is not estimated to have approached a reportable quantity (1,000 pounds), but due to the evidence that the truck was leaking while in transit to Phoenix, the Palo Verde Hazardous Materials Emergency Coordinator conservatively elected to make the government notifications. Additionally, Palo Verde notified the trucking company which ultimately located the truck upon its return to the company yard. No leak existed at that time, suggesting the leakage was limited to the caustic that remained in the truck's discharge pipe after the transfer was stopped. There was no impact to control room habitability and no safety systems, including essential ventilation, were actuated or required. The spill did not hamper site personnel in the performance of duties necessary for the safe operation of the nuclear power plant. The NRC Resident inspector was notified of the chemical spill and this ENS notification.
ENS 4150218 March 2005 22:00:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownTechnical Specification Required Shutdown Due to Inoperable Diesel GeneratorThe following information was obtained from the licensee via facsimile (licensee text in quotes): The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On March 18, 2005, at approximately 15:00 hours Mountain Standard Time (MST), Palo Verde Nuclear Generating Station (PVNGS) Unit 1 commenced a reactor shutdown required by Technical Specification 3.8.1. Limiting Condition for Operability (LCO) 3.8.1 requires two diesel generators (DGs) each capable of supplying one train of the onsite Class 1E AC Electrical Power Distribution System be available. On March 17, 2005, at approximately 04:11 MST, Unit 1 Diesel Generator "A" failed to start during its post maintenance retest. The diesel generator (DG) tripped on incomplete sequence. Prior to tripping, the DG reached approximately 100 rpm for fifteen seconds. It has been determined that the cause of the DG failure was due to a governor failure. The failed governor has been replaced. At 17:50 on March 17, 2005, DG "B" was tested satisfactorily to confirm there is not a common cause failure. Unit 1 is being shutdown because the retest of DG "A" requires the Unit to be in Mode 5. The LCO 3.8.1 would expire at 04:00 MST, March 19, 2005 requiring initiation of Shut Down required by Technical Specifications if no action was taken. The event did not result in the release of radioactivity to the environment and did not adversely affect the safe operation of the plant or health and safety of the public. The NRC Resident Inspector has been notified. At the time of the notification, power was 70% and was being reduced in preparation for reactor shutdown to Mode 3.05000528/LER-2005-006
ENS 4162923 April 2005 07:00:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedDiscovered Two Axial Indications on Inside Diameter of Reactor Vessel Head Penetration

The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up will be made via the ENS or under the reporting requirements of 10CFR50.73. On April 23, 2005, at approximately 11:35 Mountain Standard Time (MST) engineering personnel performing preplanned in-service examinations of reactor vessel head vent penetration in accordance with procedure requirements discovered two axial indications in the Palo Verde Nuclear Generating Station Unit 2 reactor vessel head vent penetration. The indications are located on the inner diameter surface of the pipe adjacent to the J-weld to the head and are part of the RCS pressure boundary. The indications are characterized as axial, estimated less than 0.080 inch deep, approximately 0.1 inch long, and oriented at approximately 90 degrees from each other. The indications are not through-wall. There is no evidence of RCS pressure boundary leakage. Technical Specifications (TS) Limiting Condition for Operation (LCO) 3.4.14 permits no reactor coolant system (RCS) pressure boundary leakage and there is no evidence of pressure boundary leakage. Nevertheless, the indications are being conservatively identified as abnormal degradation of the reactor coolant system pressure boundary and will necessitate taking corrective action to restore the barrier's capability. Therefore, the ENS notification of this event is in accordance with 10CFR50.72(b)(3)(ii)(A). The Unit had been shutdown for its 12th refueling outage and was being maintained de-fueled for maintenance. No ESF actuations occurred and none were required. There were no structures, systems, or components that were inoperable at the time of discovery that contributed to this condition. There were no failures that rendered a train of a safety system inoperable and no failures of components with multiple functions were involved. The event did not result in the release of radioactivity to the environment and did not adversely affect the safe operation of the plant or health and safety of the public.

An investigation of this event will be conducted in accordance with PVNGS corrective action program.

The NRC Resident Inspector was notified of this event by the licensee.

05000529/LER-2005-001
ENS 4178317 June 2005 18:00:0010 CFR 21.21
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
Potential Degraded Condition Due to Pressurizer Heater Element Non-Conformance

The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On June 15, 2005, Palo Verde Nuclear Generating Station was informed by Framatome that Thermocoax pressurizer heater elements provided for, and installed in Unit 3, were in non-conformance with specifications. Specifically, the active heating portion of the element was approximately 8 inches lower than design. The result of this error is that the active (heating) portion of the element extended into the nozzle area of the pressurizer heater sleeve and the heating effect on the pressurizer sleeve exceeded design, and possibly code-allowable temperature. Unit 3 operators entered Technical Requirements Manual LCO 3.4.103, Structural Integrity, Condition A for a ASME Code Class 1 component not conforming with requirements. The pressurizer can not be isolated and RCS temperature was already more than 50 degrees F above the minimum temperature required by NDT consideration when the condition was discovered. TLCO 3.0.100.3 is not applicable in Mode 5 and Technical Specification 3.4.9, Pressurizer, is not applicable in Mode 5. The RCS is in Mode 5 at approximately 190 degrees F and 350 psia. Engineering personnel are evaluating the code acceptability and potential for significant degradation resulting from the temperatures experienced by the pressurizer heater sleeves. On June 17, 2005, at approximately 11:00 AM MST, Palo Verde was informed that based on x-ray results of a PVNGS failed Thermocoax heater that revealed the active portion of the heater is longer than previously assumed, the metal temperatures exceeded ASME code allowable values. Stress levels are still under evaluation. This report is conservatively being placed per 10CFR50.72(b)(3)(ii)(A) based on the potential that the RCS pressure boundary may be seriously degraded, and 10CFR21(d)(3)(i) based on a defect in the pressurizer heater, a basic component, that may affect its safety function necessary to assure the integrity of the reactor coolant pressure boundary. An investigation of this condition will be conducted in accordance with the PVNGS corrective action program. The Thermocoax heater elements were installed in November 2004, when all heaters in the Unit 3 pressurizer were replaced. Due to the increased failure rate all Thermocoax heater elements have been replaced in the last 30 days with General Electric style pressurizer heater elements that were used previously. The heaters, which were also provided to SONGS 2&3 and Waterford 3, had a design variance (480 VAC single phase instead of 480 VAC 3-phase) which made them unique to Palo Verde. The impact of this variance is currently being evaluated. The licensee notified the NRC Resident Inspector.

* * * UPDATE ON 8/1/05 AT 1143 EDT FROM R. BUZZARD TO P. SNYDER * * *

The licensee is retracting this event based on the following: This is a retraction of ENS 41783, placed with the Headquarter Operations Center on 06/17/2005 at 1839 EDT. On June 15, 2005, Palo Verde Nuclear Generating Station was informed by Framatome that the Thermocoax pressurizer heaters provided for, and installed in Unit 3, were in non-conformance with the applicable design specification. Specifically, the heating section of the heater was manufactured approximately 8 inches longer than cited in the specification. The result of this error was that the heating section extended into the pressurizer lower head. Engineering analysis concluded that the pressurizer lower head exceeded design and ASME Code allowable temperatures. This condition was reported on June 17, 2005 (ENS 41783). Further Engineering analysis concluded that the RCS pressure boundary (pressurizer lower head) was not significantly degraded. APS has requested NRC approval for a relief request (reference letter to the NRC dated June 19, 2005). The proposed alternative discussed in this relief request provided an acceptable level of quality and safety since no significant creep effects were introduced into the Unit 3 pressurizer lower head as a result of the design non-conformance. Therefore, APS has requested that the proposed alternative be authorized pursuant to 10 CFR 50.55a(a)(3)(i). The NRC provided verbal approval for Unit 3 to continue operation. Based on the above information the "Degraded Operation" ENS notification made on June 17, is being retracted. The heater supplier, FRAMATOME ANP, INC, reported the defect in accordance with10CFR Part 21 on July 22, 2005 (ENS 41864). The licensee has retracted both the 10CFR Part 50.72(b)(3)(ii)(A) degraded condition notification and their 10 CFR Part 21 notification. Retraction of the 10 CFR Part 21 notification is based on the fact that the vendor reported the same condition. The licensee notified the NRC Resident Inspector of the retraction. Notified R4DO (D. Powers).

ENS 4178923 June 2005 15:23:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionUnit 2 Aux Feedwater Train Separation Not Maintained During OperationThe following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On 6/23/05 at approximately 08:23 MST, it was identified that the door between the 'A' and 'B' Train Aux Feedwater Pump rooms was open and unattended. The door was immediately closed and secured. This door is required to be maintained secured in the closed position (except for personnel ingress/egress) during Modes 1 through 4 to provide a barrier for protection from fire or internal flooding. Station procedures require compensatory measures to be established when this door is maintained open in Modes 1-4. The compensatory measures include stationing an individual with the responsibility to close the door in the event of internal flooding. Since this compensatory measure was not established, this condition is considered to be reportable as an unanalyzed condition per the criteria of 10CFR50.72(b)(3)(ii)(B). Investigation is in progress to determine the duration and reason that this door was inappropriately open. The licensee notified the NRC Resident Inspector.05000529/LER-2005-003
ENS 4180429 April 2005 07:43:0010 CFR 50.73(a)(1), Submit an LERInvalid System ActuationThis report is being made under 50.73 (a)(2)(iv)(A). On April 29, 2005, at approximately 0043 Mountain Standard Time, Palo Verde Nuclear Generating Station Unit 2 experienced an invalid 1/2 leg Engineered Safety Feature Actuation Signal (ESFAS) actuation (B train) when operations personnel prematurely implemented a tag out causing loss of vital power to the 'B' train ESFAS cabinet. The following alarms were received; Recirculation Actuation Signal B, Auxiliary Feedwater Actuation Signal-1B, Containment Spray Actuation Signal B, Main Steam Isolation Signal B, Containment Isolation Actuation Signal B, Safety Injection Actuation Signal B, Auxiliary Feedwater Actuation Signal-2B (all Leg 1-3), and Emergency Diesel Generator (EDG) Start Signal B. At the time of the event Unit 2 was in the 'B' train work window for refueling outage 2R12 and not all 'B' train equipment actuated - EDG B, Low Pressure Safety Injection B, Containment Spray B, and the B train Recirculation Actuation Signal sump valves were tagged out of service for maintenance. During the performance of the 'Inadvertent Plant Protection System - ESFAS Actuations' procedure, Operations personnel determined that all 'B' ESFAS equipment operated as expected considering the 'B' train equipment that was tagged out for maintenance. The licensee notified the NRC Resident Inspector.
ENS 4181029 June 2005 11:43:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness
Evacuation Siren InoperableThe following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On June 29, 2005 at approximately 08:55 Mountain Standard Time (MST), the Palo Verde Emergency Preparedness Program Manager was notified of an inoperable single siren #36. An alarm indicates that the inoperability started at 04:43 AM MST. The siren was vandalized by destroying the battery case and stealing the internal battery. The affected siren is estimated to impact approximately 215 members of population (10.1 %) in the emergency planning zone (EPZ) within 5 miles. Palo Verde's reporting criterion is a loss of capability to inform greater than 5% of the population within 5 miles (or 10% within 5 to 10 miles) for greater than 1 hour. This call is being placed due to the relatively large segment of the population affected and the uncertainty of the length of time that will be needed to restore the siren to operable condition. The Palo Verde Emergency Plan (section 6.6.2.1) has a contingency for dispatching Maricopa County Sheriffs Office (MCSO) vehicles with loud speakers to alert persons within the affected area(s) when sirens are inoperable. The County was informed at 09:25 AM MST to implement the MCSO notification if a need arises. There are no events in progress that require siren operation. The NRC Resident Inspector has been notified of the siren failure and this ENS call.
ENS 4187426 July 2005 23:35:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessInoperable Single Emergency SirenOn July 26, 2005 at approximately 09:07 Mountain Standard Time (MST), the Palo Verde Emergency Preparedness Department was notified of an inoperable single siren (#42). While reviewing the siren monitoring computer log, an Information Services Technician received a no response signal on siren #42. Upon investigation, siren #42 was found inoperable. The siren was vandalized by destroying the battery case and stealing the internal battery. The affected siren is estimated to impact approximately 144 members of population (6.8%) in the emergency planning zone (EPZ) within 5 miles. Palo Verde's reporting criterion is a loss of capability to inform greater than 5% of the population within 5 miles (or 10% within 5 to 10 miles) for greater than 1 hour. This call is being placed due to the relatively large segment of the population affected and the uncertainty of the length of time that will be needed to restore the siren to operable condition. The Palo Verde Emergency Plan (section 6.6.2.1) has a contingency for dispatching Maricopa County Sheriff's Office (MCSO) vehicles with loud speakers to alert persons within the affected area(s) when sirens are inoperable. The County was informed at 09:38 MST to implement the MCSO notification if a need arises. There are no events in progress that require siren operation. The NRC Resident Inspector has been notified of the siren failure and this ENS call.
ENS 4191211 August 2005 15:45:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness
One Emergency Preparedness Siren Out of Service

On August 11, 2005 at approximately 08:45 Mountain Standard Time (MST), the Palo Verde Emergency Preparedness Department identified an inoperable single siren (#15). While reviewing the siren monitoring computer log, an Information Services Technician received a 'no response' signal on siren #15. Upon investigation, siren #15 was found inoperable. The siren was vandalized by destroying the siren controller case and stealing the internal battery. The affected siren is estimated to impact approximately 496 members of population in the emergency planning zone (EPZ) beyond 5 miles but within 10 miles. Palo Verde's reporting criterion is a loss of capability to inform greater than 10% of the population beyond 5 miles but within 10 miles. This call is being placed due to the relatively large segment of the population affected and the uncertainty of the length of time that will be needed to restore the siren to operable condition. The Palo Verde Emergency Plan (section 6.6.2.1) has a contingency for dispatching Maricopa County Sheriff's Office (MCSO) vehicles with loud speakers to alert persons within the affected area(s) when sirens are inoperable.

The County was informed at 09:05 MST to implement the MCSO notification if a need arises. There are no events in progress that require siren operation. The licensee notified the NRC Resident Inspector.

ENS 4191312 August 2005 07:19:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownPlant Entered Lco Action Statement 3.8.1 to Be in Mode 5 Due to Unit 1 "B" Diesel Gen. Being Declared InoperableOn August 12, 2005, at approximately 00:19 hours Mountain Standard Time (MST), Palo Verde Nuclear Generating Station (PVNGS) Unit 1 commenced a reactor shutdown required by Technical Specification 3.8.1. Limiting Condition for Operability (LCO) 3.8.1 requires two diesel generators (DGs) each capable of supplying one train of the onsite Class 1E AC Electrical Power Distribution System be available. On August 9, 2005, at approximately 04:20 MST, Unit 1 Diesel Generator 'B' failed to maintain the proper steady state output voltage (4080-4300 VAC) during monthly operability surveillance testing per '40ST-9DG02'. Diesel Generator 'B' was declared inoperable and the Unit entered LCO 3.8.1 action 'B'. An engineering action plan was initiated in an attempt to identify the cause of the generator output voltage fluctuation and correct the problem. To date, troubleshooting efforts have unable to isolate the problem. On August 12 at 0420 MST the 72 hour Completion Time associated with LCO 3.8.1 Action 'B' will expire and at 00:19 MST Unit 1 commenced a reactor shutdown in compliance with LCO 3.8.1 Action 'H'. The event did not result in the release of radioactivity to the environment and did not adversely affect the safe operation of the plant or health and safety of the public. The required offsite power sources are operable and the electrical grid is stable. The NRC Resident Inspector will be notified.05000528/LER-2005-004
ENS 4193922 August 2005 23:05:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownTechnical Specification Shutdown Due to Core Protection Calculator System (Cpcs) Software Not Consistent with System Design Requirements.The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On August 22, 2005, at approximately 1605 hours Mountain Standard Time (MST), Palo Verde Nuclear Generating Station (PVNGS) Unit 2 commenced a reactor shutdown required by Technical Specification 3.0.3. Westinghouse notified Palo Verde that the current version of the Common Q based Core Protection Calculator System (CPCS) software is not consistent with the system design requirements and Technical Specification Bases regarding the system response to analog input module errors. In that a failed sensor input or failure of the two analog input modules in a given CPCS channel (four total channels) would not result in a CPCS channel trip. At Palo Verde, the CPCS provides the reactor trip functions for Low Departure from Nucleate Boiling Ratio (DNBR) and High Local Power Density (LPD). A failed input sensor would be the most likely cause for both of the redundant input modules to indicate errors simultaneously because the two redundant input modules within a safety channel are connected to a single sensor. A similar scenario would occur if both analog input modules simultaneously failed. In both cases the result would be a failure of the channel without initiating a trip signal. Operations evaluated the non-conforming condition and declared all four channels of the CPCS inoperable. Limiting Condition for Operability (LCO) 3.3.1 only addresses up to two automatic RPS trip channels inoperable, therefore Operations entered LCO 3.0.3 at approximately 13:26 MST. The event did not result in the release of radioactivity to the environment and did not adversely affect the safe operation of the plant or health and safety of the public. The required offsite power sources are operable and the electrical grid is stable. The Common Q based CPCS is installed at the following nuclear power plant site in the United States: Palo Verde Unit 2. At this time, this condition is not transportable to Palo Verde Units 1 and 3. All Emergency Core Cooling systems and their Emergency Diesel Generators are fully operable if needed. The NRC Resident Inspector was notified of this event by the licensee.05000529/LER-2005-004
ENS 4194123 August 2005 20:49:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness
Two Emergency Sirens Inoperable

The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On August 23, 2005 at approximately 13:49 Mountain Standard Time (MST), the Palo Verde Emergency Preparedness Department identified a siren (#42) inoperable due to a failed battery charger. At approximately 14:00 a faxed notice was found indicating siren #15 had failed its response check. The fax was sent approximately at 07:00 but was not noticed till later since out of service siren notifications are generally made via phone or e-mail. Upon investigation, siren #15 was found inoperable due to a circuit board failure. Siren #15 is estimated to impact approximately 144 members of population in the emergency planning zone (EPZ) within 5 miles, and siren #42 is estimated to impact 496 members of the population in the EPZ, beyond 5 miles but within 10 miles. Palo Verde's reporting criterion is a loss of capability to inform greater than 5% of the population within 5 miles and 10% of the population beyond 5 miles but within 10 miles. This call is being placed due to the relatively large segment of the population affected and the uncertainty of the length of time that will be needed to restore the siren to operable condition. The Palo Verde Emergency Plan (section 6.6.2.1) has a contingency for dispatching Maricopa County Sheriff's Office (MCSO) vehicles with loud speakers to alert persons within the affected area(s) when sirens are inoperable. There are no events in progress that require siren operation.

The NRC Resident Inspector has been notified of the siren failure and this ENS call.

ENS 4195127 August 2005 01:24:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationRps Actuation - Reactor Scram on High Steam Generator LevelThe following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On August 26, 2005, at approximately 18:24 Mountain Standard Time (MST) Palo Verde Unit 1 experienced an automatic reactor scram on high steam generator #1 level. All rods inserted, as required. Unit 1 was at normal operating temperature and pressure prior to the trip. The main turbine was not yet synchronized to the grid; turbine chest warming was in progress. The main turbine automatically tripped in response to the reactor trip. A reactor startup had been completed and operators were transferring feedwater from a motor driven auxiliary feedwater pump to the steam driven 'A' main feedwater pump at approximately 1.2% reactor power. Steam generator #1 level decreased from a normal level of approximately 40% narrow range (approx. 77% wide range) to approximately 12% narrow range (approx. 66% wide range). An operator took manual control of feedwater to increase level. Upon returning feedwater control to automatic after level was restored, steam generator #1 level continued to increase, resulting in a reactor trip on high steam generator level at approximately the Technical Specification reactor trip and Main Steam Isolation Signal (MSIS) setpoint of 91.5%. The MSIS (ESF actuation) functioned as required. No other ESF actuations occurred or were required. No emergency classification was required per the Emergency Plan. Safety related buses remained energized during and following the reactor trip. The Emergency Diesel Generators did not start and were not required. The offsite power grid is stable. No LCOs have been entered as a result of this event. No major equipment was inoperable prior to the event that contributed to the event. The maximum power level during the feedwater transient was approximately 8.5%. Unit 1 is stable at normal operating temperature and pressure in Mode 3. The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The maximum RCS pressure was approximately 2251 psia (normal 2250). The maximum steam generator pressure was approximately 1188 psia (normal 1165). The event did not adversely affect the safe operation of the plant or the health and safety of the public. The licensee notified the NRC Resident Inspector.
ENS 4196029 August 2005 17:30:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOff Site Notifications Due to Loss of Inoperable Emergency Evacuation SirenOn August 29, 2005 at approximately 10:30 Mountain Standard Time (MST), the Palo Verde Emergency Preparedness Department identified an inoperable single siren (#18). The siren was vandalized by stealing the internal battery. The affected siren is estimated to impact approximately 131 members of population in the emergency planning zone (EPZ) within 5 miles. This call is being placed due to the relatively large segment of the population affected and the uncertainty of the length of time that will be needed to restore the siren to operable condition. The Palo Verde Emergency Plan (section 6.6.2.1) has a contingency for dispatching Maricopa County Sheriff's Office (MCSO) vehicles with loud speakers to alert persons within the affected area's) when sirens are inoperable. Maricopa County and State agencies have been informed to implement the MCSO notification if a need arises. There are no events in progress that require siren operation. The NRC Resident Inspector has been notified
ENS 4199615 September 2005 18:40:00Information OnlyEmergency Preparedness Siren ModificationsThis is an information only notification. Commencing approximately 1 PM Mountain Standard Time, September 15, 2005, the Palo Verde Nuclear Generating Station will be performing modifications to Emergency Preparedness sirens within the 5-mile radius of the emergency planning zone (EPZ) to implement corrective action to prevent recurrence of damage due to vandalism that has occurred and been reported in previous ENS notifications (Recent Event Notifications: 41960, 41912, 41874, 41810, 41486, 41466, 41451). Palo Verde's reporting criterion includes a loss of capability to inform greater than 5% of the population (more than 106 people) within 5 miles. Six of the 12 sirens within the 5-mile radius meet this criterion. Only one of these 6 sirens will be out of service at a time for modification. The Palo Verde Emergency Plan (section 6.6.2.1) has a contingency for dispatching Maricopa County Sheriff's Office (MCSO) vehicles with loud speakers to alert persons within the affected area(s) when sirens are inoperable. The MCSO has been informed of the status of siren modification for each of the 6 sirens so that the contingency can be promptly implemented if an event requiring siren activation were to exist, thus no loss of capability to inform the population will occur. The licensee notified the NRC Resident Inspector.
ENS 4205011 October 2005 23:02:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Tech Spec Required Shutdown of Both Unit 2 and 3The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On October 11, 2005 Palo Verde Nuclear Generating Station (PVNGS) Units 2 and 3 at approximately 1602 and 1655 Mountain Standard Time (MST), respectively commenced reactor shutdowns required by Technical Specification 3.0.3. Engineering personnel were unable to demonstrate that the original design of the Emergency Core Cooling System (ECCS) could perform its safety function for its mission time under certain postulated accident scenarios. Specifically, the Refueling Water Tank (RWT) is designed with baffles to prevent a vortex from developing and air binding the Safety Injection pumps during a Loss of Coolant Accident (LOCA). On a LOCA, the High Pressure Safety Injection pumps take a suction from the RWT and inject borated water into the Reactor Coolant System (RCS). At 7.4 percent RWT level, the source of borated water by design automatically shifts from the RWT to the containment sump. However, for small break LOCA there may be insufficient containment pressure to ensure inventory is not continuing to be drawn from the RWT. This may allow the baffles in the bottom of the RWT to uncover. With the RWT baffles uncovered, a vortex may develop, leading to potential air binding of the Safety Injection pumps before the operator manually isolates the RWT. At approximately 1333 Mountain Standard Time, based on the inability to demonstrate that the ECCS can perform its safety function under certain accident scenarios, Palo Verde Units 2 and 3 entered Technical Specification 3.0.3. Engineering continues to evaluate this condition. There were no RPS/ESF actuations, and none were required. There were no structures, systems or components that were inoperable at the start of event that contributed to the event. This condition did not result in any challenges to the fission product barrier or result in any releases of radioactive materials. There were no adverse safety consequences or implications as a result of this event. This condition did not adversely affect the safe operation of the plant or health and safety of the public. The NRC Resident Inspector has been notified of this condition and this ENS notification.05000529/LER-2005-005
ENS 4210131 October 2005 19:02:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseMedia InterestThe following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On October 31, 2005, at approximately 12:02 PM Mountain Standard Time (MST) the Palo Verde Nuclear Generating Station was informed of a request to conduct a media interview with a clearinghouse that provides newsworthy input to local media regarding an emergency preparedness exercise to commence tomorrow. No press release is planned by Palo Verde, but the interview is indication of media interest. The State of Arizona and Maricopa County will be performing an ingestion pathway emergency preparedness exercise on November 1, 2005 through November 3, 2005. The exercise will be evaluated by the Federal Emergency Management Agency (FEMA). Although this exercise will involve significant participation by State and County agencies, Palo Verde participation is expected to be limited to a small control cell of personnel to simulate communication with the State and County. There has been some media interest. There have been no official press releases posted by Maricopa County or the State of Arizona, although the Governor's calendar for November 1, 2005 indicates that the Honorable Janet Napolitano will participate. Resident NRC inspectors are not expected to participate in this exercise, but Palo Verde understands that two NRC Region IV personnel (Messrs. T. Andrews and W. Maier) are expected to support FEMA evaluation of the exercise. Palo Verde Unit 1 is in a refueling outage with all fuel assemblies offloaded to the spent fuel pool. Units 2 and 3 are operating in Mode 1 at approximately 100% power, at normal operating temperature and pressure. The licensee notified the NRC Resident Inspector.
ENS 423812 March 2006 21:30:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite NotificationThe following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS. This is a report of a situation, related to the protection of the environment, for which a notification to another government agency has been or will be made, as described in 10CFR50.72(b)(2)(xi). Specifically, the Palo Verde Nuclear Generating Station (PVNGS) notified the Arizona Department of Environmental Quality (ADEQ) of the possibility of a discharge of non-hazardous material that has the potential to cause groundwater limits to be exceeded At Palo Verde Unit 3, water was observed in a concrete pipe vault that was abutted against soil. The source of the water appeared to becoming from seals around the pipes and originating from the ground behind the pipe chase. The area behind the pipe chase contains a series of pipes buried in a layer of compacted soil. In order to characterize the water and identify its source, a pothole, approximately 13 feet deep and reinforced with a perforated drain pipe was dug in the radiological controlled area yard so that a sample of the water could be obtained. Initial results from the unit laboratory indicated the presence of tritium. A confirmatory sample was collected and analyzed by the State certified laboratory at Palo Verde that confirmed the presence of tritium at a concentration of approximately 7.14 x 10 -5 microCurie per milliliter. The Aquifer Protection Permit Aquifer Quality Limit for tritium is 2.00 x 10 -5 microCurie per milliliter. At this time we are working to identify the source. We currently have no evidence that the water has contaminated any aquifer but are continuing with our investigation. Palo Verde's ground-water monitoring program - in place since the unit operations began - has validated that no tritium has been present in any wells or aquifers in any quarterly samples. PVNGS has just finished collecting its quarterly monitoring samples. Analyzed samples have no indication of tritium. The remaining samples will be completed next week. No Technical Specification effluent limits have been exceeded. No Offsite Dose Calculation Manual (ODCM) effluent limits have been exceeded. No federal effluent limits have been exceeded. Palo Verde has not identified any health or safety risk to the public or onsite personnel. No source of leakage or release path has been identified, therefore no release rate or total quantity released has been quantified. Unit 3 is operating at approximately 100% rated thermal power at normal operating temperature and pressure. This information is also being reported to the Arizona Radiation Regulatory Agency. The licensee notified the NRC Resident Inspector.
ENS 423875 March 2006 14:10:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationAutomatic Reactor Trip Due to Low Departure from Nucleate Boiling Ratio.The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10 CFR 50.73. On March 5, 2006 at approximately 0710 MST Palo Verde Unit 3 experienced a reactor trip (RPS actuation) from 100% rated thermal power due to low departure from nucleate boiling (ratio) (DNBR) trips on all four channels of the core protection calculators (CPCs). The unit was at normal temperature and pressure prior to the trip. Prior to the reactor trip, at approximately 0704 MST, a CEAC (Control Element Assembly Calculator) #1 sensor fail alarm was received. While investigating the alarm, at 0710 MST, a control element assembly (CEA) deviation alarm for CEAC #1, all four CPC channel sensor fail alarms, and a CEA withdrawal prohibit alarm were received. The reactor tripped six seconds later. A CEA calculator (CEAC) fail alarm was received on CEAC #1. The apparent cause is presently suspected to be a failure of CEAC #1. An investigation has commenced to determine the root cause of the reactor trip. All of the control rods fully inserted into the core. Four of eight steam bypass control valves quick opened, per design, directing steam flow to the condenser. No main steam or primary relief valves lifted and none were required. There was no loss of heat removal capability or loss of safety functions associated with the event. Electrical buses transferred to offsite power as designed. The Shift Manager determined this event was an uncomplicated reactor trip. No significant LCOs have been entered as a result of this event. No major equipment was inoperable prior to the event nor contributed to the event. Unit 3 is stable at normal operating temperature and pressure in Mode 3. No ESF actuations occurred and none were required. The event did not result in any challenges to the fission product barrier or resulted in any releases of radioactive materials. There were no adverse safety consequences or implications as a result of this event. The event did not adversely affect the safe operation of the plant or health and safety of the public. The licensee notified the NRC Resident Inspector.05000530/LER-2006-002
ENS 424683 April 2006 03:54:0010 CFR 50.72(b)(3)(iv)(A), System ActuationEmergency Diesel Trip During TestingThe following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On April 2, 2006 at approximately 20:54 Mountain Standard Time, Palo Verde Nuclear Generating Station Unit 3 experienced a valid Loss of Power (LOP) actuation on the Train 'B' 4.16 kV safety bus. The event occurred due to personnel error during performance of surveillance test 73ST-9DG02 (Class 1 E Diesel Generator and Integrated Safeguards Test Train B). EDG 'B' had been started In Emergency Mode per the surveillance test by opening the normal supply breaker to the associated 4.16 kV bus and initiating simulated Safety Injection Actuation System (SIAS) and Containment Isolation Actuation System (CIAS) signals. A subsequent portion of the surveillance test was in progress which demonstrates that the EDG 'test mode' trips are bypassed with the EDG operating in Emergency Mode. The step being performed was intended to simulate an Overcurrent (test mode) trip by installing a jumper at the Overcurrent relay. However the jumper was inadvertently installed at the Differential Current relay, which generated an 'Emergency Mode' trip of EDG 'B'. This resulted in the deenergization of the 4.16 kV bus. The operations staff entered Abnormal Operating Procedure (AOP) 40AO-9ZZ12 (Degraded Electrical) and reset EDG 'B'. Upon reset at approximately 21:26 MST, EDG 'B' automatically started in response to a valid Loss of Power (LOP) signal from the deenergized 4.16 kV bus. The EDG 'B' output breaker automatically closed to restore power to the Train 'B' 4.16 kV and equipment sequenced onto the 4.16 kV bus. Due to the loss of power on the Train 'B' 4.16 kV bus, the Train 'B' Control Room Essential Filtration System (CREFS) and Control Room Emergency Air Temperature Control System (CREATCS) were rendered inoperable and LCOs 3.7.11 Condition 'A' and 3.7.12 Condition 'A' were entered. Operability of Train 'B' CREFS and CREATCS was restored when the Train 'B' 4.16 kV bus was reenergized and these LCO Conditions were exited. Offsite power remained available to the Train 'A' 4.16 kV bus and EDG 'A' remained operable throughout the event. Shutdown Cooling was unaffected since it was being provided by the Train 'A' safety train, which was supplied by offsite power. The offsite electrical grid is stable. Palo Verde Unit 3 Is shutdown and in Mode 5 for its 12th refueling outage. No other ESF actuations occurred and none were required. There were no structures, systems, or components that were inoperable at the time of discovery that contributed to this condition. The event did not result in the release of radioactivity to the environment and did not adversely affect the safe operation of the plant or health and safety of the public. The NRC Resident Inspector has been notified of the ESF actuation and this ENS notification. The site performed a work stand down to discuss this event and prevent recurrence.
ENS 4248710 April 2006 19:33:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownUnit 2 Entered a Ts Required Shutdown Due to Inoperable Auxiliary Feedwater PumpsThe following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On April 10. 2006, at approximately 12:33 hours Mountain Standard Time (MST), Palo Verde Nuclear Generating Station (PVNGS) Unit 2 commenced a reactor shutdown required by Technical Specification (TS) 3.7.5 Condition C. Limiting Condition for Operability (LCO) 3.7.5 requires three AFW trains to be Operable. Condition A of this LCO provides allowance for one steam supply to the turbine driven AFW to be inoperable for a 7 day period. If the inoperable SGAUV138A valve is not restored to an operable condition within 7 days, Unit 2 will be required to shutdown to Mode 3 in 6 hours and to Mode 4 in 12 hours, starting at 10:41 MST on April 10, 2006. The event did not result in the release of radioactivity to the environment and did not adversely affect the safe operation of the plant or health and safety of the public. The NRC Resident Inspector has been notified and is present in the control room.
ENS 425596 May 2006 23:35:0010 CFR 50.72(b)(3)(iv)(A), System ActuationValid Actuation of Emergency Diesel Generator Due to Low Voltage ConditionThe following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On May 6, 2006, at approximately 16:35 US Mountain Standard Time (MST) a valid actuation of the Palo Verde Nuclear Generating Station Unit 3 Train 'A' Emergency Diesel Generator (EDG) occurred as a result of an undervoltage condition on its respective safety bus (PBA-S03). EDG 'A' started and loaded as designed to energize PBA-S03. The loss of power to the safety bus occurred during Gas Turbine Generator testing. GTG number 1 was supplying safety bus PBA-S03 at a low voltage when supply breaker PBA-S03L opened unexpectedly. This resulted in the deenergization of the safety bus PBA-S03. The emergency diesel generator started and all required related safety equipment started as expected. No Emergency Plan declaration was made and none was required. Unit 3 was in mode 5 at 50 psia and140 degrees F. Shutdown Cooling Train B was OPERABLE and in service. No other ESF actuations occurred and none were required. The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The event did not adversely affect the safe operation of the plant or the health and safety of the public. The NRC Resident Inspector has been notified of the ESF actuation and this ENS notification.05000530/LER-2006-004
ENS 4260930 May 2006 15:13:0010 CFR 50.72(b)(3)(iv)(A), System ActuationLoss of Power to Train "a" 4 Kv Safety BusThe following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10 CFR50.73. On May 30, 2006, at approximately 08:13 Mountain Standard Time, Palo Verde Nuclear Generating Station, Unit 1 experienced a Loss Of Power (LOP) to Train 'A' (PBAS03) 4 KV safety bus. At the time of the LOP the 'A' Emergency Diesel Generator (EDG) had just been manually removed from the PBAS03 bus following a maintenance surveillance run and was still operating in a post run cool down mode. The PBAS03 bus was still powered from the off site power source and was at rated voltage. An invalid Load Shed signal was received from the Train 'A' Load Sequencer, which opened the normal off site supply breaker to PBAS03 bus, and stripped all of the Ioads off the bus. Next, a valid LOP signal developed, since the PBAS03 bus was de-energized. The EDG 'A' received a valid emergency run mode signal and returned to rated frequency and voltage; however its output breaker did not reclose on bus PBAS03. This reclosure was blocked by the Train 'A' Load Sequencer which had 'stalled' and was not able to provide the permissive for the DG output breaker to close. The failure of the load sequencer is currently under investigation by the PVNGS engineering department. Offsite power was available to both safety buses throughout the event; however the invalid Load Shed signal blocked immediate restoration of off site power to the Train 'A' bus. The other (Train 'B') safety bus is being supplied by offsite power; however Train 'B' EDG is not available due to planned outage related maintenance. The offsite electrical grid is stable. Efforts are currently in progress to restore the Train 'B' DG for a redundant power source. In addition, efforts are in progress to clear the Load Shed signal off the Train 'A' bus to allow restoration of power from the off site power source. Palo Verde Unit 1 is shutdown and Defueled in a mid-cycle repair outage. The entire core is off loaded to the Spent Fuel Pool and is currently being maintained with inventory and cooling by the Train 'B' components powered from off site power. No other ESF actuations occurred and none were required. The event did not result in the release of radioactivity to the environment and did not adversely affect the safe operation of the plant or health and safety of the public. At 13:04 MST the 'B' EDG was restored and operable. The licensee also indicated that Train 'A' offsite power is expected to be restored within about 1 hour, or 16:20 EDT. The licensee notified the NRC Resident Inspector.05000528/LER-2006-003
ENS 4265118 June 2006 21:55:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
Loss of Onsite Emergency Safety Function - "B" Edg Failed to Start During Test Run

The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On June 18, 2006, at approximately 1455 Mountain Standard Time (MST), Palo Verde Nuclear Generating Station Unit 1 was operating at 0% power in Mode 6 with the 'A' Emergency Diesel Generator (EDG) inoperable for troubleshooting of the train 'A' load sequencer, The 'B' EDG failed to start during a test run resulting in a loss of the onsite emergency power safety function required by General Design Criterion (GDC) 17. The offsite power source safety function remains available to the plant. The unit entered Technical Specification 3.8.2, AC Sources - Shutdown Condition B for one required DG inoperable. There was no movement of irradiated fuel assemblies, therefore the unit remained in compliance with the Required Actions. The offsite electrical grid is stable. At 1810 MST the 'A' EDG was declared operable, exiting Technical Specification 3.8.2. With the 'A' EDG operable, the safety function for the onsite emergency power was also restored. There were no structures, systems or components that were inoperable at the start of event that contributed to the event. This condition did not result in any challenges to the fission product barrier or result in any releases of radioactive materials. There were no adverse safety consequences or implications as a result of this event. This condition did not adversely affect the safe operation of the plant or health and safety of the public. The NRC Resident Inspector has been notified of this condition and this ENS notification.

  • * * RETRACTION RECEIVED VIA E-MAIL FROM DAN HAUTALA TO JOE O'HARA AT 1702 ON 7/5/06 * * *
Further evaluation has determined that this event is not reportable.  In the 'test' mode, an 'Incomplete Sequence' trip is enabled and functions on an engine start to trip the engine if starting air is not terminated within 15 seconds.  Due to a delay in opening the engine fuel racks by the test mode pneumatic control valve loop, the 'Incomplete Sequence' trip actuated.  During an emergency start, the electrically operated emergency fuel solenoids control the operation of the engine fuel racks and the 'Incomplete Sequence' trip function is bypassed.  Engineering evaluation found none of the equipment required to operate the 'B' EDG in the emergency mode degraded or malfunctioning.  The 'B' EDG was still capable of performing its design function and was 'OPERABLE'.  Additionally, it was determined that the 'A' EDG was fully functional and in a standby condition, capable of performing its design function at the time the 'B' EDG test run trip occurred.

Therefore, this condition is not reportable per 10CFR50.72(2)(b)(v)(B) or (2)(b)(v)(D)." The licensee notified the NRC Resident Inspector. R4DO(Pick) has been notified.

ENS 426812 July 2006 02:28:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationManual Reactor Trip Following Large Leak in Condensate System

On July 1, 2006, at approximately 19:28 MST Palo Verde Unit 3 experienced a manual reactor trip from approximately 100% rated thermal power due to a large leak in the condensate system. The sight glass for the 'A' condensate demin vessel blew out of the vessel creating an approximate 6 inch diameter hole. Several thousand gallons of condensate were discharged to the Turbine Building and the environment. Radiation Protection has sampled the condensate water and have verified no activity is present. Unit 3 was at normal operating temperature and pressure prior to the trip. The 'A' Main feedwater pump tripped on low suction pressure and a Reactor Power Cutback Signal was received. Condenser hotwell levels continued to decrease. When the main control board annunciator for the 'B' Main Feedwater Pump Trip Circuit Energized was received the reactor was manually tripped. All CEAs fully inserted into the reactor core. The event was diagnosed as an uncomplicated reactor trip. No ESF actuations occurred and none were required. Safety related buses remained energized during and following the reactor trip. The offsite power grid is stable. No significant LCOs have been entered as a result of this event. There was no loss of normal heat removal capabilities, or loss of any safety functions associated with this event. No major equipment was inoperable prior to the event that contributed to the event. No primary or secondary safety valves lifted during the event. The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The event did not adversely affect the safe operation of the plant or the health and safety of the public. Unit 3 is stable at normal operating temperature and pressure in Mode 3. There is no estimated time and date for the Unit 3 restart at the time this call is being made. AFW is being used to feed the steam generators and is discharging steam to the main condenser. The licensee stated that the leak has been secured and that there is no significant standing water in the turbine building lower levels. All the water has drained into sumps or out doors. There does not appear to be any electrical or personnel safety hazards as a result of the water leak. The licensee notified the NRC Resident Inspector.

      • UPDATE FROM RAY BUZZARD TO JOHN KNOKE AT 17:28 ON 07/03/06 ***

The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. This notification is a follow-up to the manually initiated reactor trip event reported on July 1, 2006 (ENS 42681). The notification indicated that the reactor was manually tripped from approximately 100% rated thermal power due to a large leak in the condensate system. Prior to the transient the unit was operating at approximately 100 % rated thermal power, however, the manual trip was actually initiated from approximately 55% rated thermal power following a reactor power cutback caused by the loss of the A train main feedwater pump on low suction pressure. In addition, the ENS report stated that Radiation Protection had sampled the condensate water and verified no activity is present. The condensate actually was found to contain tritium at a concentration of 1.22E-5 uCi/ml. The water from the spill flowed to the onsite storm drains, was captured behind dams, and transferred to the onsite retention basins. Samples of resin from the spill were also collected, analyzed by gamma spectroscopy, and found to not contain licensed radioactive material. The licensee notified the NRC Resident Inspector. Notified R4DO (Shannon)

ENS 4270112 July 2006 14:30:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessOne Siren in Ep Zone Is Out of ServiceThe following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73. On July 12, 2006 at approximately 07:30 Mountain Standard Time (MST), the Palo Verde Emergency Preparedness Department reported siren (#23) out of service. Siren #23 is estimated to impact approximately 119 members of population in the emergency planning zone (EPZ) within 5 miles. Palo Verde's reporting criterion is a loss of capability to inform greater than 5% of the population within 5 miles. This call is being placed due to the relatively large segment of the population affected. During an event, the Palo Verde Emergency Plan has a contingency for dispatching Maricopa County Sheriff's Office (MCSO) vehicles with loud speakers to alert persons within the affected area(s) when sirens are inoperable. There are no events in progress that require siren operation. The NRC Resident Inspector has been notified of the siren 23 being out of service and this ENS call. The total population within the 5 mile EPZ is 2120.
ENS 4273026 July 2006 14:35:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationVariable Overpower Reactor Trip Following Turbine Control Valve MaintenanceOn July 26, 2006, at approximately 07:34 Mountain Standard Time (MST) Palo Verde Unit 2 experienced an automatic reactor scram on Variable Overpower. Unit 2 was operating at 90% power at normal operating temperature and pressure prior to the event. A main turbine control valve (CV02) was being returned to service following maintenance. CV02 initially started to open which caused reactor power to decrease to approximately 89%. During the evolution, six steam bypass control valve opened (three valves opened 100 percent, one opened 60 percent, and two opened 5 percent). Reactor power rapidly increased to 98% which resulted in an auxiliary Variable Power Trip (VOPT). The VOPT trip set point is 8 percent. The main turbine automatically tripped in response to the reactor trip. All rods inserted, as required. No ESF actuations occurred and none were required. No emergency classification was required per the Emergency Plan. Safety related buses remained energized during and following the reactor trip. The Emergency Diesel Generators did not start and were not required. The offsite power grid is stable. No LCOs have been entered as a result of this event. No major equipment was inoperable prior to the event that contributed to the event. The maximum power level during the transient was approximately 98%. Unit 2 is stable at normal operating temperature and pressure in Mode 3. The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The maximum RCS pressure was approximately 2260 psia (normal 2240). The maximum steam generator pressure was approximately 1090 psia (normal 1055). The event did not adversely affect the safe operation of the plant or the health and safety of the public. The licensee notified the NRC Resident Inspector.05000529/LER-2006-003