ENS 41913
ENS Event | |
---|---|
07:19 Aug 12, 2005 | |
Title | Plant Entered Lco Action Statement 3.8.1 to Be in Mode 5 Due to Unit 1 "B" Diesel Gen. Being Declared Inoperable |
Event Description | On August 12, 2005, at approximately 00:19 hours Mountain Standard Time (MST), Palo Verde Nuclear Generating Station (PVNGS) Unit 1 commenced a reactor shutdown required by Technical Specification 3.8.1.
Limiting Condition for Operability (LCO) 3.8.1 requires two diesel generators (DGs) each capable of supplying one train of the onsite Class 1E AC Electrical Power Distribution System be available. On August 9, 2005, at approximately 04:20 MST, Unit 1 Diesel Generator 'B' failed to maintain the proper steady state output voltage (4080-4300 VAC) during monthly operability surveillance testing per '40ST-9DG02'. Diesel Generator 'B' was declared inoperable and the Unit entered LCO 3.8.1 action 'B'. An engineering action plan was initiated in an attempt to identify the cause of the generator output voltage fluctuation and correct the problem. To date, troubleshooting efforts have unable to isolate the problem. On August 12 at 0420 MST the 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> Completion Time associated with LCO 3.8.1 Action 'B' will expire and at 00:19 MST Unit 1 commenced a reactor shutdown in compliance with LCO 3.8.1 Action 'H'. The event did not result in the release of radioactivity to the environment and did not adversely affect the safe operation of the plant or health and safety of the public. The required offsite power sources are operable and the electrical grid is stable. The NRC Resident Inspector will be notified. |
Where | |
---|---|
Palo Verde Arizona (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown | |
LER: | 05000528/LER-2005-004 |
Time - Person (Reporting Time:+-3.88 h-0.162 days <br />-0.0231 weeks <br />-0.00531 months <br />) | |
Opened: | Brad Eklund 03:26 Aug 12, 2005 |
NRC Officer: | Chauncey Gould |
Last Updated: | Aug 12, 2005 |
41913 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 41913\u003C/a\u003E - \u003Ca href=\"/Palo_Verde\" title=\"Palo Verde\"\u003EPalo Verde\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003EPlant Entered Lco Action Statement 3.8.1 to Be in Mode 5 Due to Unit 1 \"B\" Diesel Gen. Being Declared Inoperable\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 41913 - Palo Verde\n","link":"","lat":33.386894444444444,"lon":-112.86263333333333,"icon":"/w/images/9/93/Arizona_Public_Service_icon.png"}],"imageoverlays":null} | |
Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (94 %) |
After | Power Operation (94 %) |
WEEKMONTHYEARENS 506002014-11-06T18:16:0006 November 2014 18:16:00
[Table view]10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Dropped Control Element Assembly ENS 496012013-12-03T06:24:0003 December 2013 06:24:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Tech Spec Required Shutdown Due to Dropped Control Element Assembly ENS 442742008-06-06T06:56:0006 June 2008 06:56:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Tech Spec Required Shutdown Due to Leak in Safety Injection Tank Vent Line ENS 438042007-11-24T05:26:00024 November 2007 05:26:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Plant Shutdown Due to Inoperable Load Sequencer ENS 437362007-10-22T10:11:00022 October 2007 10:11:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Shutdown Due to Inoperable Steam Driven Auxiliary Feedwater Pump ENS 431732007-02-19T21:57:00019 February 2007 21:57:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unit 2 Performed a Ts Required Shutdown ENS 428472006-09-19T08:05:00019 September 2006 08:05:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Pressurizer Heater Capacity Less than Tech Spec Limit ENS 424872006-04-10T19:33:00010 April 2006 19:33:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unit 2 Entered a Ts Required Shutdown Due to Inoperable Auxiliary Feedwater Pumps ENS 420502005-10-11T23:02:00011 October 2005 23:02:00 10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Tech Spec Required Shutdown of Both Unit 2 and 3 ENS 419392005-08-22T23:05:00022 August 2005 23:05:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Shutdown Due to Core Protection Calculator System (Cpcs) Software Not Consistent with System Design Requirements. ENS 419132005-08-12T07:19:00012 August 2005 07:19:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Plant Entered Lco Action Statement 3.8.1 to Be in Mode 5 Due to Unit 1 "B" Diesel Gen. Being Declared Inoperable ENS 415022005-03-18T22:00:00018 March 2005 22:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Inoperable Diesel Generator ENS 413892005-02-09T08:04:0009 February 2005 08:04:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specifications Required Shutdown Due to Loss of Normal and Alternate Power to Safety Bus ENS 405032004-02-03T22:35:0003 February 2004 22:35:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Technical Specification Required Shutdown Due to Rcs Pressure Boundary Leakage 2014-11-06T18:16:00 | |