ENS 41951
ENS Event | |
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01:24 Aug 27, 2005 | |
Title | Rps Actuation - Reactor Scram on High Steam Generator Level |
Event Description | The following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73.
On August 26, 2005, at approximately 18:24 Mountain Standard Time (MST) Palo Verde Unit 1 experienced an automatic reactor scram on high steam generator #1 level. All rods inserted, as required. Unit 1 was at normal operating temperature and pressure prior to the trip. The main turbine was not yet synchronized to the grid; turbine chest warming was in progress. The main turbine automatically tripped in response to the reactor trip. A reactor startup had been completed and operators were transferring feedwater from a motor driven auxiliary feedwater pump to the steam driven 'A' main feedwater pump at approximately 1.2% reactor power. Steam generator #1 level decreased from a normal level of approximately 40% narrow range (approx. 77% wide range) to approximately 12% narrow range (approx. 66% wide range). An operator took manual control of feedwater to increase level. Upon returning feedwater control to automatic after level was restored, steam generator #1 level continued to increase, resulting in a reactor trip on high steam generator level at approximately the Technical Specification reactor trip and Main Steam Isolation Signal (MSIS) setpoint of 91.5%. The MSIS (ESF actuation) functioned as required. No other ESF actuations occurred or were required. No emergency classification was required per the Emergency Plan. Safety related buses remained energized during and following the reactor trip. The Emergency Diesel Generators did not start and were not required. The offsite power grid is stable. No LCOs have been entered as a result of this event. No major equipment was inoperable prior to the event that contributed to the event. The maximum power level during the feedwater transient was approximately 8.5%. Unit 1 is stable at normal operating temperature and pressure in Mode 3. The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The maximum RCS pressure was approximately 2251 psia (normal 2250). The maximum steam generator pressure was approximately 1188 psia (normal 1165). The event did not adversely affect the safe operation of the plant or the health and safety of the public. The licensee notified the NRC Resident Inspector. |
Where | |
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Palo Verde Arizona (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
Time - Person (Reporting Time:+-1.08 h-0.045 days <br />-0.00643 weeks <br />-0.00148 months <br />) | |
Opened: | Brian Ferguson 00:19 Aug 27, 2005 |
NRC Officer: | John Knoke |
Last Updated: | Aug 27, 2005 |
41951 - NRC Website
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WEEKMONTHYEARENS 565512023-06-02T11:05:0002 June 2023 11:05:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 564592023-04-09T04:44:0009 April 2023 04:44:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of Reactor Coolant Pumps ENS 556262021-12-06T19:03:0006 December 2021 19:03:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Unit 3 Automatic Trip ENS 552652021-05-19T10:15:00019 May 2021 10:15:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to High Pressurizer Pressure ENS 551142021-02-26T17:33:00026 February 2021 17:33:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Trip Due to Loss of Two Reactor Coolant Pumps ENS 545602020-03-04T03:50:0004 March 2020 03:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Trip Due to Low Steam Generator Level ENS 542242019-08-16T15:21:00016 August 2019 15:21:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip ENS 534772018-06-27T07:00:00027 June 2018 07:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Low Steam Generator Water Level ENS 534242018-05-23T18:28:00023 May 2018 18:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip on Low Departure from Nucleate Boiling Ratio ENS 532152018-02-16T04:53:00016 February 2018 04:53:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness Automatic Reactor Trip Due to Low Departure from Nucleate Boiling Signal ENS 522262016-09-08T04:31:0008 September 2016 04:31:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Stuck Open Pressurizer Main Spray Valve ENS 496002013-12-03T00:58:0003 December 2013 00:58:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Following the Loss of the 1A Reactor Coolant Pump ENS 478372012-04-15T19:20:00015 April 2012 19:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Control Rod Deviation During Startup ENS 474722011-11-23T02:25:00023 November 2011 02:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Control Element Deviation ENS 471332011-08-06T18:19:0006 August 2011 18:19:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Dropped Control Element Assembly ENS 465562011-01-20T01:41:00020 January 2011 01:41:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Main Feedwater Pump Trip ENS 457482010-03-07T18:24:0007 March 2010 18:24:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Notification of Unusual Event Due to Electrical Fault Causing Damage to Equipment ENS 455372009-12-03T11:30:0003 December 2009 11:30:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip After Loss of Instrument Air to Containment ENS 449702009-04-04T06:54:0004 April 2009 06:54:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram Due to High Vibrations in the Turbine ENS 445252008-09-28T04:51:00028 September 2008 04:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Unit 3 Reactor Manually Tripped Following Automatic Turbine Trip on High Vibration ENS 444962008-09-16T21:00:00016 September 2008 21:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip During Troubleshooting of Control Rod Drive Mechanism Motor Generators ENS 442462008-05-29T04:34:00029 May 2008 04:34:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Improper Movement of Cea'S ENS 436972007-10-06T17:59:0006 October 2007 17:59:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Condenser Tube Rupture ENS 429252006-10-21T22:48:00021 October 2006 22:48:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Control Element Assembly Position Transmitter Output Deviations ENS 429202006-10-19T18:47:00019 October 2006 18:47:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Following the Trip of Secondary Condensate Pumps ENS 427302006-07-26T14:35:00026 July 2006 14:35:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Variable Overpower Reactor Trip Following Turbine Control Valve Maintenance ENS 426812006-07-02T02:28:0002 July 2006 02:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Following Large Leak in Condensate System ENS 423872006-03-05T14:10:0005 March 2006 14:10:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Low Departure from Nucleate Boiling Ratio. ENS 419512005-08-27T01:24:00027 August 2005 01:24:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Rps Actuation - Reactor Scram on High Steam Generator Level ENS 408702004-07-14T08:35:00014 July 2004 08:35:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Following a Main Generator Trip ENS 408162004-06-14T14:44:00014 June 2004 14:44:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Due to Reactor Trip Due to Loss of Off Site Power ENS 408152004-06-14T14:44:00014 June 2004 14:44:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Reactor Trip Due to Loss of Off Site Power ENS 408142004-06-14T14:44:00014 June 2004 14:44:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Alert Declared - Reactor Trip Due to Loss of Off Site Power ENS 407952004-06-07T21:58:0007 June 2004 21:58:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Trip Due to Main Turbine Electro-Hydraulic Control System Failure ENS 407372004-05-09T03:39:0009 May 2004 03:39:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip During Physics Testing Due to Control Element Assembly Slipping 6 Inches. 2023-06-02T11:05:00 | |