ML18347A847

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License Event Report 1980-024-00 Re Containment High Radiation Monitor
ML18347A847
Person / Time
Site: Palisades Entergy icon.png
Issue date: 08/12/1980
From: Huston R
Consumers Power Co
To: James Keppler
NRC/RGN-III
References
LER 1980-024-00
Download: ML18347A847 (2)


Text

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                               ~IDJ mm~ tID rrH17 General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201 * (517) 788-0550 August 12, 1980 Mr   James G Keppler Office of Inspection and Enforcement Region III U S"- Nuclear Regulatory Commission 799 Roosevelt Road Glen: Ellyn,. IL 60137
          ~OCKET      50-255 - LICENSE DPR            PALISADES PLANT - LICENSEE EVENT REPORT 80-024 - CONTAINMENT HIGH RADIATION MONITOR On tl:i.e reverse side is Licensee EYent Report 80-024 which is reportable under Technical Specification 6.9.2.A.2.
         ~~

Senior Licensing Engineer CC Director, Office of Nuclear Reactor Regulation Director, Office of Inspection and Enforcement NRC R~sident Inspector - Palisades

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PALISADES ,PLANT NRC FORM366 U.S. NUCLEAR REGULATORY.COMMISSION 17-771 LICENSEE EVENT REPORT CONTROL BLOCK: I. 1 10 e* (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) fil!JIMITIPIAILI ll@IOI Ol-IOI OfOIO IO.b ICYIOl@l4lll lllll IG)I I.I@ 7 8 9 LICENSEE CODE 141 ,5 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 CON'T ITIIJ =~~~~~- L&..l©I 01 5 I 010 Io I 215 I 5 GI o I 713.I1-18 Io K!)J 01*s I ii 2 I 81 ol@ 7 8 . 60 61 DOCKET NUMBER 68 69 EVENT DATE . 741 75 REPORT DATE 80 EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES @ . .. . .. []JI) I With D/G 1-1 inoperable to perform a modification and charging pump P-55A (!!!] I inoperable for repairs, P-55B became ino~erable. Condition not permitted (]]TI I oy LCO of TS 3. 7. D/G 1-1 was restored to . operable status in approx. [III) 1 hour. *thereby restoring plant to a condition*perm.itted by*technical

 @TI]              specifications.                            Occurrence reportable per TS 6._9.2.A.2.

filI] [[[[] 7 B 9 BO SYSTEM CAUSE CAUSE

  • COMP. VALVE CODE CODE SUBCODE COMPONENT CODE . SUBCODE SUBCODE IE I El@ l!..J@ @_j@) I GI EIN I E!R 9 10 11 . 12 13 .

fA !@) l!J@ 18 19

                                                                                                                                                            --~@

20 SEQUENTIAL OCCURRENCE *REPORT REViSION

              @. .NUMBER LER/RQ LVENT EAR                                   . REPORT NO.                                   CODE                 TYPE                              NO.

18 I 0 I y. REPORT 21 22 l=1

                                                            . 23 Io 241 I 214       26 I      1.....-'I_

27 10 11 28 29 I ~ 30 l=J 31

                                                                                                                                                                                 ~

32 ACTION FUTURE EFFECT SHUTDOWN ~ ATTACHMENT NPRD-4 PRIME COMP. COMPONENT.

            *TAKEN         ACTION             ON PLANT             METHOD                     HOURS    22         SUBMITTED       FORM liUB.         SUPPLIER                 MANUFACTURER Lil@W@                             ~@                  ~@)           Io I a I o I              I     l!J@            1.!U@Y 1.!J@ . I A I                            115 @. I@)

33 . 34 35 . 36 37 410 . 41 42 43 . ""' . . 47 CAUSE DESCRIPTION ANO CORREC"rlVE ACTIONS @ .* -. * -- . . IJJ!] I In+/-tial condition of having diesel generator 1-1 and P-55A inoperable.at COii 1 Sal!l.e ti-me was permitted by TS 3. 7. Failure of' P-55B was caused by pump (IIlJ J packing failure. Pump was repacked and restored to service *. o::rn lilIJ 7 8 9 BO FACILITY IJi)\ ~00~ ~ STATUS  % POWER OTHER STATUS ~ DISCOVERY DISCOVERY DESCRIPTION ~ ITTil LI I 019 I 0 l@)I NA . ~~l,___Op.._e_r_a_t_o_r__ Ob__ se_rv__a_t_i_*o_n__* ____________. 8 9 10 12 13 "" 45 "6 80 ACTIVITY CONTENT

  • t::;;...

. RELE.ASED OF RELEASE AMOUNT OF ACTIVITY . LOCATION OF RELEASE@ ITEl 1 8

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9 .

                                ~'11 10 NA                           I                      NA 80
                 . PERSONNEL EXPOSURES                                   ~

II1I1 I 0 I 010 lEJ~__N_A__ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ ____,

              *** NUMBER            t::;,. TYPE/.:;\ DESCRIPT!QN 7        8    9                   11        12          13                                                                                                                                    BO PERSONNEL INJURIES                     c.\

DESCRIPTION~ ITTIJ IOI NUMBER 010 l@)"""""______N_A___________________________________________ 7 8 9 . 11 . 12 80 LOSS 01' OR DAMAGE TO FACILITY t.iJ\ TYPE DESCRIPTION ~ [!TI] Lzj@ .- NA 7 8 9 10 80 PUBLICITY C\ NRC USE ONLY ISSUEDt,;:;\ DESCRIPTION~ 112 I o81 91 N l~.1..0_ _ . --*--*-N_A _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ ___, II IrIIIIIIIII 68 69 . 80}}