Similar Documents at Salem |
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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0261998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 1.With 990115 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr ML18106A9831998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 2.With 981214 Ltr ML18106A9801998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Salem,Unit 1.With 981214 Ltr ML18106A9641998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 2. with 981112 Ltr ML18106A9631998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Salem,Unit 1. with 981112 Ltr ML18106A9151998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 2.With 981012 Ltr ML18106A9131998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Salem,Unit 1.With 981012 Ltr ML18106A8751998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Generating Station,Unit 2.With 980915 Ltr ML18106A8741998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Salem Unit 1.With 980915 Ltr ML18106A8161998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 1. W/980817 Ltr ML18106A8151998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Salem,Unit 2. W/980817 Ltr ML18106A7151998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 2. W/980715 Ltr ML18106A7141998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Salem,Unit 1. W/980715 Ltr ML18106A6541998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 1. W/980615 Ltr ML18106A6531998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Salem Unit 2. W/980615 Ltr ML18106A6121998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Generating Station,Unit 1.W/980515 Ltr ML18106A6111998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Salem Unit 2. W/980515 Ltr ML18106A5561998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem,Unit 1. W/980415 Ltr ML18106A4591998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Salem Unit 2. W/980415 Ltr ML18106A3771998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 1.W/980316 Ltr ML18106A3761998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Salem Generating Station,Unit 2.W/980316 Ltr ML18106A3281998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 2. W/980217 Ltr ML18106A3271998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Salem,Unit 1. W/980217 Ltr ML18106A2721997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem,Unit 2. W/980115 Ltr ML18106A2711997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Salem Generating Station,Unit 1.W/980115 Ltr ML18106A2081997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 1. W/971212 Ltr ML18106A2071997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Salem,Unit 2. W/971212 Ltr ML18102B6811997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 2.W/ 971117 Ltr ML18102B6801997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Salem,Unit 1.W/ 971117 Ltr ML18102B6271997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Salem,Unit 2. W/971015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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- Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Attn.: Document Control Desk MONTHLY OPERATING REPORT SALEMNO. 1 DOCKET NO: 50-272 February 15, 1996 In compliance with Section 6.9.1.6, Reporting Requirements for the Salem Technical Specifications, the original copy of the monthly operating report for the month of January is being sent to you. RH:vls Enclosures C Mr. Thomas T. Martin Sincerely yours, General Manager -Salem Operations Regional Administrator USNRC, Region I 631 Park Avenue King of Prussia, PA 19046 .-.._on._
n _A_ of __ _ _______ _ 9602220050 960131 PDR ADOCK 05000272 R PDR The power is in your hands. 95-2168 REV. 6/94
- OPERATING DATA REPORT Docket No: 50-272 Date: 02/10/96 Completed by: Robert Phillips Telephone:
339-2735 Operating Status 1. unit Name Salem No. 1 Notes 2. Reporting Period January 1996 3. Licensed Thermal Power (MWt) 3411 4. Nameplate Rating (Gross MWe) 1170 5. Design Electrical Rating (Net MWe) 1115 6. Maximum Dependable Capacity(Gross MWe) 1149 7. Maximum Dependable Capacity (Net MWe) 1106 8. If Changes Occur in Capacity Ratings (items 3 through 7) since Last Report, Give Reason NA 9. Power Level to Which Restricted, if any (Net MWe) NIA 10. Reasons for Restrictions, if any
- 12. Hours in Reporting Period 12. No. of Hrs. Rx. was Critical 13. Reactor Reserve Shutdown Hrs. 14. Hours Generator On-Line 15. Unit Reserve Shutdown Hours 16. Gross Thermal Energy Generated (MWH) 17. Gross Elec. Energy Generated (MWH) 18. Net Elec. Energy Gen. (MWH) 19. Unit Service Factor 20. Unit Availability Factor 21. Unit Capacity Factor (using MDC Net) 22. Unit Capacity Factor (using DER Net) 23. Unit Forced outage Rate This Month 744 0 0 0 0 0 0 -2461 0 0 0 0 0 Year to Date 744 0 0 0 0 0 0 -2461 0 0 0 0 0 Cumulative 162961 104380.5 0 100388.3 0 318062229.2 105301000 100202452
- 61. 6 61. 6 55.6 55.1 22.9 24. Shutdowns scheduled over next 6 months (type, date and duration of each) We are presently in a scheduled extension of refueling outage. 25. If shutdown at end of Report Period, Estimated Date of Startup: Under review. 8-1-7.R2 AVEi9E DAILY UNIT POWER LEVEL
- Docket No.: 50-272 Unit Name: Salem #1 Date: 02/10/96 Completed by: Robert Phillips Telephone:
339-2735 Month January 1996 Day Average Daily Power Level Day Average Daily Power Level (MWe-NET) (MWe-NET) 1 0 17 0 2 0 18 0 3 0 19 0 4 0 20 0 5 0 21 0 6 0 22 0 7 0 23 0 8 0 24 0 9 0 25 0 10 0 26 0 11 0 27 0 12 0 28 0 13 0 29 0 14 0 30 0 15 0 31 0 16 0 P. 8.1-7 Rl NO. DATE 3824 01-01-96 s 1 2 F: Forced S: Scheduled DURATION TYPE 1 (HOURS) REASON 2 744 c Reason A-Equipment Failure (explain)
B-Maintenance or Test C-Refueling D-Requlatory Restriction 4 UNIT SHUTDOWN AND POWER REDUCTIONS REPORT MONTH January 1996 METHOD OF SHUTTING DOWN REACTOR LICENSE EVENT REPORT # ----------
zz 3 Method: 1-Manual 2-Manual Scram SYSTEM CODE 4 E-Operator Training & License Examination F-Administrative 3-Automatic Scram 4-Continuation of Previous Outage 5-Load Reduction 9-0ther G-Operational Error (Explain)
H-Other (Explain)
COMPONENT CODE 5 zzzz DOCKET NO. UNIT NAME DATE COMPLETED BY TELEPHONE 50-272 Salem #1 02/10/96 Robert Phillips 609-339-2735.
CAUSE AND CORRECTIVE ACTION TO PREVENT RECURRENCE Schedule Extension of Refueling
- 4 Exhibit G -Instructions for Preparation of Data Entry Sheets for Licensee Event Report CLER) File (NUREG-0161) 5 Exhibit 1 -Same Source *
- 10CFR50.59 EVALUATIONS MONTH: JANUARY 1996 DOCKET NO: UNIT NAME: 50-272 SALEM 1 02/10/96 DATE: COMPLETED BY: TELEPHONE:
R. HELLER 609-33 9-5162 The following items were evaluated in accordance with the provisions of the Code of Federal Regulations 10CFR50.59.
The Station Operations Review Committee has reviewed and concurs with these evaluations.
- 1. Design Change Packages (DCP) lEC-3301, Pkg. 1 lEC-3307, Pkg. 2 lEC-3322, Pkg. 3 "Steam Generator Blowdown Upgrade" Rev. 1 -This DCP replaces Steam Generator Blowdown system valves to improve performance and reliability.
It replaces GB185, GB923 & GB924 in the Turbine Building and GB9 & GB189 valves in the Mechanical Penetration Area. In addition it installs a bypass valve around GB9 valves and replaces the carbon steel piping downstream of GB923 valves with stainless steel. This revision will replace some of the encapsulations near the GB9 valves and revise the safety evaluation to include information regarding the encapsulations.
This revision also incorporates the Independent Design Verification, which was not complete at Rev. 0. Some pipe supports are being modified to facilitate installation.
There is no reduction in the margin of safety as defined in the basis for any Technical Specification. (SORC 95-104) "Gaseous Waste Disposal System Piping Reclassification and Modification to Sample Chamber RA-4331" Rev. 0 -This design change package removes the abandoned lRl 4 radiation detector now existing in Sample Chamber RA-4331 and weld a permanent plate in place of the existing fitted shield cap on the chamber. The detector is currently in place only to serve as a piping pressure boundary in order to protect and seal the integrity of the Gaseous Waste Disposal System. There is no reduction in the margin of safety as defined in the basis for any Technical Specification. (SORC 95-142) "Service Water Pipe Replacement:
Auxiliary Building Nuclear Header 11" Rev. 0 -This DCP replaces service water piping in the Unit 1 Auxiliary Building.
The scope of the change involves _I
- 10CFR50.59 EVALUATIONS MONTH: JANUARY 1996 DOCKET NO: UNIT NAME: 50-272 SALEM 1 02/10/96 R.HELLER 609-339-.5162 lEC-3323, Pkg. 1 DATE: COMPLETED BY: TELEPHONE:
replacement of 24", 20", 8" and 4" supply and return piping and associated branch connections supporting the No. 11 Component Cooling Heat Exchanger (CCHX) to/from Service Water Nuclear Header No. 11. The pipe is currently coal tar epoxy lined or cement lined carbon steel. Replacement piping will be 6% molybdenum austenitic stainless steel. This is part of the Service Water Upgrade Program is identified in the UFSAR. This change of material is already defined in the UFSAR. This DCP also incorporates a P&ID location change of temperature.
tap, 1TT14726, and root valve, 11SW123. These changes only reflect the as-built condition and are not implemented per this DCP. There is no reduction in the margin of safety as defined in the basis for any Technical Specification. (SORC 95-128) "Piping Replacement for Service Water Intake Bay # 1 (Blind Flange Installation)
Rev. 2 -This design change package replaces service water piping in the Unit 1 Intake Bay #1. This revision to the package installs a 30"blind flange to the turbine header discharge piping upstream of 11 SW20 at the service water header in Intake Bay # 1. This is being made as an interim solution due to excessive valve seat leakage through turbine header cross tie isolation valve 13 SW20. Installation of this blind flange will allow service water piping replacement work to continue.
There is no reduction in the margin of safety as defined in the basis for any Technical Specification. (SORC 95-100) 2. UFSAR Change Notices (SCN) SCN 95-74 "Seismic Evaluation Of Service Water/Circulating Water Discharge Piping" -The original plant design provided a buried 24 inch blank "tee" connection in the yard for each of the two underground nuclear discharge headers. In response to FSAR Question 9.34, PSE&G stated that the above buried tees would be opened to establish an alternate discharge path for the Service Water System in the event of a postulated failure of the
- 10CFR50.59 EVALUATIONS MONTH: JANUARY 1996 DOCKET NO: UNIT NAME: 50-272 SALEM 1 02/10/96 R.HELLER 609-339-5162 (Cont'd) SCN95-42 DATE: COlvlPLETED BY: TELEPHONE:
non-seismic circulating water piping during a seismic event. This action would become necessary if the postulated failure of the circulating water piping resulted in blockage of the service water discharge from the plant. However, a recent Engineering Evaluation, S-C-SW-CEE-0955 concludes that the water discharge function of the circulating water piping will not be
- affected by the postulated seismic event. The evaluation concludes that there is no concern that the circulating water piping would fail during a seismic event and block the service water discharge from the plant. Thus, the buried tees located in the yard do not need to be opened during or after a seismic event as anticipated in the original design. This proposal is intended to revise UFSAR Section 9 .2.1 to document the results of the above engineering evaluation and to acknowledge that the buried tees located in the yard do not need to be opened during or after a postulated seismic event as anticipated in the original design. This proposal does not modify any equipment, component(s), system(s) or station procedure(s).
There is no reduction in the margin of safety as defined in the basis for any Technical Specification. (SORC 96-001) "Inconsistent Flood Level References For The Service Water Intake Structure" -This UFSAR update incorporates changes made to the Service Water Intake Structure by DCP lEC-1837, which was approved and completed in 1984. The changes were the result of revised flood levels and maximum wave runup. The changes revised Service Water Intake Structure watertightness up to Elev. 128 ft. Public Service Datum for the air-intake penthouse and watertightness up to Elev. 126 ft. Public Service Datum with wave runup protection up to Elev. 128 ft. Public Service Datum for the air exhausts.
The margins for safety as defined in the Technical Specifications are not changed. The existing Service Water Intake Structure building flood level watertightness and flood wave runup protection satisfies design basis requirements. (SORC 96-002)
- 10CFR50.59 EVALUATIONS MONTH: JANUARY 1996 DOCKET NO: UNIT NAME: 50-272 SALEM 1 02/10/96 4. Safety Evaluation (S/E) ODCM ES-13.010 Rev. 3 ES-13.005 Rev. 4 DATE: COMPLETED BY: TELEPHONE:
R. HELLER 609-339-5162 "Offsite Dose Calculation Manual" Rev. 10 -The purpose of this revision is to incorporate updating information from previous releases.
The changes are mainly editorial in nature. Technical Specifications 3.3.8 and 3.11.1.1 are considered the pertinent sections affected by the changes proposed under Revision 10 to the Salem ODCM. The alarm/trip setpoint calculated under the proposed revision will ensure that the alarm/trip will occur prior to exceeding the limits of 10 CFR Part 20, Appendix B, Table II, Column 2. The changes proposed under Revision 10 to the Salem ODCM do not reduce the margin of safety as defined in the basis for any Technical Specification. (SORC 96-001) "Penetration Overcurrent Protection Coordination Calculation
-Salem Unit 1 and Salem Unit 2 -This is an update to the Penetration Protection Coordination Calculations to add Attachment 3 that provides a summary of the electrical devices that provide redundant electrical protection for the electrical containment penetration feed through conductors as required by Reg Guide 1.63. Modifications to this calculation are made by the Design Change Process as outlined in procedure AP .ZZ-0008(Q).
This calculation is mentioned in Section 8.3.2.4 of the UFSAR regarding a list of Containment Penetration Protection devices. The addition, deletion or modification of the specific protective devices is controlled by the Design Change Process. All devices listed in the subject calculation have been previously reviewed when the calculation was developed or reviewed as part of a Design Change Package that installed them. Therefore, this calculation revision does not reduce the margin of safety as defined in the basis for any Technical Specifications. (SORC 96-011)
- REFUELING INFORMATION MONTH: JANUARY 1996 MONTH : JANUARY 1996
- DOCKET NO: UNIT NAME: DATE: COMPLETED BY: TELEPHONE:
50-272 SALEM 1 02/10/96 R. HELLER 609-339-5162 Refueling information has changed from last month: YES . X . NO,,__. -----'-Scheduled date for next refueling:
09/10/95 Scheduled date for restart following refueling:
06/17 /96 a. Will Technical Specification changes or other license amendments be required?
YES.
NOT DETERMINED TO DATE . X . b. Has the reload fuel design been reviewed by the Station Operating Review Committee?
YES. .NO. X . If no, when is it scheduled? (to be determined ) Scheduled date(s) for submitting proposed licensing action: . n/a Important licensing considerations associated with refueling:
Number of Fuel Assemblies:
- a. Incore b. In Spent Fuel Storage Present licensed spent fuel storage capacity:
Future spent fuel storage capacity:
Date oflast refueling that can be discharged to the spent fuel pool assuming the present licensed capacity:
8-l-7.R4 0 1005 1632 1632 September 2008
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- SALEM GENERATING STATION MONTHLY OPERATING
SUMMARY
-UNIT 1 JANUARY 1996 SALEM UNIT NO. 1 The Unit is in a refueling outage and remained shutdown for the entire period. According to commitments from PSE&G and a subsequent confirmatory action letter from the NRC, the Unit will remain shutdown pending completion of the following actions:
- Appropriately address long standing equipment reliability and operability issues
- After the work is completed, conduct a restart readiness review to determine for ourselves the ability of each Unit to operate in a safe, event free manner
- After the restart review, meet with the NRC and communicate the results of that review