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{{#Wiki_filter:I ACCELERATED DTRIBUTION                           DEMONS~TION               SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
{{#Wiki_filter:I ACCELERATED DTRIBUTION DEMONS~TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9103060340             DOC.DATE:   90/12/31   NOTARIZED: NO             DOCKET FACIL:50-400 Shearon Harris Nuclear Power Plant,               Unit   1, Carolina     05000400 AUTH. NAME           AUTHOR     AFP'ILIATION RICHEY,R.B.         Carolina Power & Light Co.
ACCESSION NBR:9103060340 DOC.DATE: 90/12/31 NOTARIZED:
  'RECIP. NAME         RECIPIENT AFFILIATION Document Control Branch (Document           Control Desk)
NO DOCKET FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina 05000400 AUTH.NAME AUTHOR AFP'ILIATION RICHEY,R.B.
                                                                                        ~A7 wi/ R
Carolina Power
& Light Co.
'RECIP. NAME RECIPIENT AFFILIATION
~A7 w Document Control Branch (Document Control Desk) i/ R


==SUBJECT:==
==SUBJECT:==
Annual 10CFR50.59           rept for 1990,includinq summaries of, l
Annual 10CFR50.59 rept for 1990,includinq summaries of, I
I changes to procedures           &/or plant mods who.ch change plant. as described in FSAR.                                                                 D DISTR1BUTION CODE: 1E47D           COPIES RECEIVED:LTR       ENCL      SIZE:
changes to procedures
TITLE: 50.59 Annual Report of Changes, Tests or               xperiments   Made W/out Approv NOTES:Application for permit renewal filed.                                           05000400 A
&/or plant mods who.ch change plant. as described in FSAR.
RECIPIENT               COPIES          RECIPIENT          COPIES ID CODE/NAME PD2-1 LA LTTR ENCL 1     0 ID CODE/NAME PD2-1 PD LTTR ENCL 5    5 D
D DISTR1BUTION CODE:
BECKER,D                    1    0                                                D INTERNAL: ACRS                          6    6    AEOD/DOA               1    1 AEOD/DSP/TPAB                1    1      &QDM?       FB11       1    1 NRR/DOEA/OEAB11              1    1    REG FIL       02     1     1 RGN2    FILE 01            1     1 EXTERNAL: NRC PDR                        1     1     NSIC                    1     1 D
1E47D COPIES RECEIVED:LTR ENCLl SIZE:
TITLE: 50.59 Annual Report of Changes, Tests or xperiments Made W/out Approv NOTES:Application for permit renewal filed.
05000400 A
RECIPIENT ID CODE/NAME PD2-1 LA BECKER,D INTERNAL: ACRS AEOD/DSP/TPAB NRR/DOEA/OEAB11 RGN2 FILE 01 EXTERNAL: NRC PDR COPIES LTTR ENCL 1
0 1
0 6
6 1
1 1
1 1
1 1
1 RECIPIENT ID CODE/NAME PD2-1 PD AEOD/DOA
&QDM?
FB11 REG FIL 02 NSIC COPIES LTTR ENCL 5
5 1
1 1
1 1
1 1
1 D
D D
NOTE TO ALL"RIDS" RECIPIENTS:
D D
D D
NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
TOTAL NUMBER OF COPIES REQUIRED: LTTR               21 ENCL   19
TOTAL NUMBER OF COPIES REQUIRED:
LTTR 21 ENCL 19


Carolina Power & Light Company P. O. Box t65 ~ New kill, N, C. 27562 R. B. RICHEY Vice President Harris NUclear Project FEB       2'7 1991 Letter           Number:     HO-910015   (0)                                 10CFR50.59 U.S. Nuclear Regulatory Commission ATTN:           NRC Document Control Desk Washington,             DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO. 50-400 LICENSE NO. NPF-63                   t REPORT IN ACCORDANCE WITH 10CFR50.59 Gentlemen.'n accordance   with 10CFR50.59,         the following report is submitted for the year of 1990. This report contains brief summaries                           of changes to procedures and/or plant modifications, which change                       the plant as it is described in the FSAR. There were no tests                             or experiments               conducted   during this interval, which are               not described in the FSAR and require reporting in this report.
Carolina Power & Light Company P. O. Box t65 ~ New kill,N, C. 27562 R. B. RICHEY Vice President Harris NUclear Project FEB 2'7 1991 Letter Number:
Very   truly yours, jd Vice President Harris Nuclear Project MGW:gcm Enclosure cc.         Mr. S. D. Ebneter     (NRC RII)
HO-910015 (0) 10CFR50.59 U.S. Nuclear Regulatory Commission ATTN:
Mr. J. E. Tedrow     (NRC SHNPP) r(prj'1 MEM/HO-9100150/1/Osl 9103060340 901231 PDR               ADOCK 05000400 R                               PDR
NRC Document Control Desk Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO. 50-400 LICENSE NO. NPF-63 t
REPORT IN ACCORDANCE WITH 10CFR50.59 Gentlemen.'n accordance with 10CFR50.59, the following report is submitted for the year of 1990.
This report contains brief summaries of changes to procedures and/or plant modifications, which change the plant as it is described in the FSAR.
There were no tests or experiments conducted during this
: interval, which are not described in the FSAR and require reporting in this report.
Very truly yours, jd Vice President Harris Nuclear Project MGW:gcm Enclosure cc.
Mr. S. D. Ebneter (NRC RII)
Mr. J.
E. Tedrow (NRC SHNPP)
MEM/HO-9100150/1/Osl 9103060340 901231 PDR ADOCK 05000400 R
PDR r(prj'1


Change to Plant as Described -in the FSAR Title.       PCR-000214,   Addition of HVAC to Waste Processing     Building (WPB)
Change to Plant as Described -in the FSAR Title.
Control   Room Locker Area and Toilet Facility.
PCR-000214, Addition of HVAC to Waste Processing Building (WPB)
Functional   Summar III This plant modification installed a bathroom and locker facility adjacent to the WPB Control Room. FSAR Section 9.4.3 discusses the WPB Control Room HVAC
Control Room Locker Area and Toilet Facility.
Functional Summar III This plant modification installed a bathroom and locker facility adjacent to the WPB Control Room.
FSAR Section 9.4.3 discusses the WPB Control Room HVAC
'System which will now supply air to the added bath/locker facility.
'System which will now supply air to the added bath/locker facility.
The WPB   Control   Room HVAC system is a non-safety system   and  is not required for safe     shutdown of the plant.     The system provides     cooling to the WPB Control Room and pressurization for radiation protection       of operators. This change does not affect the systems ability to perform its       intended function.
The WPB Control Room HVAC system is a non-safety system for safe shutdown of the plant.
This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.         Thus, no unreviewed safety question exls'ts ~
The system provides Control Room and pressurization for radiation protection change does not affect the systems ability to perform its and is not required cooling to the WPB of operators.
FSAR   Reference'.
This intended function.
This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.
: Thus, no unreviewed safety question exls'ts
~
FSAR Reference'.
Section 9.4.3 and Figure 9,.4.3-4 MEM/HO-9100150/2/OS1
Section 9.4.3 and Figure 9,.4.3-4 MEM/HO-9100150/2/OS1


~ '
~
Change to Plant as Described   in the   FSAR Title.'PCR-001546,               Use of Nukon Fiberglass Insulation Inside Containment Functional           Summar :
 
This plant modification approved the replacement of the metal reflective insulation inside containment with Nukon Fiberglass Insulation (Owens-Corning Fiberglass Corp.) on a one-for-,one basis, as deemed necessary to replace defective insulation.
Change to Plant as Described in the FSAR Title.'PCR-001546, Use of Nukon Fiberglass Insulation Inside Containment Functional Summar This plant modification approved the replacement of the metal reflective insulation inside containment with Nukon Fiberglass Insulation (Owens-Corning Fiberglass Corp.)
In a letter dated December 8, 1978, the NRC staff accepted the use of Nukon insulation inside nuclear containments.                       "Based     on     quantitative and qualitative tests performed by or for Owens-Corning Fiberglass, the staff concluded that the Owens-Corning Fiberglass Corporation's nuclear containment insulation .system (Nu'k'on) is capable of retarding heat loss from piping and equipment in containment areas, and that the overall integrity of the bl'ankets will not be adversely affected by the conditions found during the lifetime of the pl,ant.             It was concluded that during a loss-of-coolantto interfere    accident, the with Owens-Corning Fiberglass insulation system               is not   expected the operation of the emergency             r'ecirculation   system."     The   staff's acceptance was based           on Topical Report OCF-1 (dated December, 1978), developed by Owens-
on a
one-for-,one
: basis, as deemed necessary to replace defective insulation.
In a letter dated December 8,
: 1978, the NRC staff accepted the use of Nukon insulation inside nuclear containments.
"Based on quantitative and qualitative tests performed by or for Owens-Corning Fiberglass, the staff concluded that the Owens-Corning Fiberglass Corporation's nuclear containment insulation.system (Nu'k'on) is capable of retarding heat loss from piping and equipment in containment
: areas, and that the overall integrity of the bl'ankets will not be adversely affected by the conditions found during the lifetime of the pl,ant.
It was concluded that during a loss-of-coolant
: accident, the Owens-Corning Fiberglass insulation system is not expected to interfere with the operation of the emergency r'ecirculation system."
The staff's acceptance was based on Topical Report OCF-1 (dated
: December, 1978),
developed by Owens-
'Corning Fiberglass Corporation which adequately addressed the six concerns stated below.
'Corning Fiberglass Corporation which adequately addressed the six concerns stated below.
: 1)     Release         of airborne particles leading to       a radiation health hazard in service,')
1)
      . Stress corrosion cracking of the austenitic stainless                   steel surfaces that comes in contact with the insulation',
Release of airborne particles leading to a radiation health hazard in service,')
E
. Stress corrosion cracking of the austenitic stainless steel surfaces that comes in contact with the insulation',
: 3)     Deterioration of the thermal properties during normal plant operation, complicating operation and control of the plant;
E 3)
: 4)       Presenting a fire hazard in the containment               area   that could interfere with safe operation of the plant;
Deterioration of the thermal properties during normal plant operation, complicating operation and control of the plant; 4)
: 5)         Interference with the emergency spray system in the event of a LOCA;
Presenting a fire hazard in the containment area that could interfere with safe operation of the plant; 5)
: 6)       Blocking of pressure relief ports in the event of an accident; Additional plant specific analysis was conducted to confirm that llukon insulation does not pose any additional threat to containment sump screen blockage at SHNPP.
Interference with the emergency spray system in the event of a LOCA; 6)
This change does not increase the probability or consequences of'nalyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.                 Thus, no unreviewed safety question exists           a FSAR         Reference-Section 6.2.2 MEM/H0-9100150/3/OS1
Blocking of pressure relief ports in the event of an accident; Additional plant specific analysis was conducted to confirm that llukon insulation does not pose any additional threat to containment sump screen blockage at SHNPP.
This change does not increase the probability or consequences of'nalyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.
: Thus, no unreviewed safety question exists a FSAR Reference-Section 6.2.2 MEM/H0-9100150/3/OS1


Change to Plant as Described in the   FSAR
Change to Plant as Described in the FSAR


==Title:==
==Title:==
PCR-001887,   Reconfiguration of the Fuel Handling Building (FHB) Fuel Pool A to Allow Increased   Storage of BWR and PWR Fuel Assemblies.
PCR-001887, Reconfiguration of the Fuel Handling Building (FHB) Fuel Pool A to Allow Increased Storage of BWR and PWR Fuel Assemblies.
Functional   Summar This plant modification allows the reracking of the FHB Fuel Pool A to allow for storage of BWR and PWR fuel assemblies. Pool A is being transformed from a new fuel storage area for PWR fuel only into a composite PWR and BWR irradiated fuel storage area. This change also allows the contents of the
Functional Summar This plant modification allows the reracking of the FHB Fuel Pool A to allow for storage of BWR and PWR fuel assemblies.
Pool A is being transformed from a
new fuel storage area for PWR fuel only into a
composite PWR and BWR irradiated fuel storage area.
This change also allows the contents of the
'Spent Fuel Pool B to be transferred into the A pool in order to perform liner repairs on the B pool.
'Spent Fuel Pool B to be transferred into the A pool in order to perform liner repairs on the B pool.
Fuel Pool   A is designed for the stor'age of new and'pent PWR fuel. Since the llX11   BWR rack modules are interchangeable with 7X7 PWR rack modules           it is acceptable   to store spent BWR fuel in the A pool. The A pool meets   all of the design and performance requirements as the B pool and can be used as a spent fuel pool with no changes to its cooling or purification capability.
Fuel Pool A is designed for the stor'age of new and'pent PWR fuel.
Rearrangement     of the racks in the   A pool has no effect on the maximum stored criticality since the individual racks are designed to maintain a subcritical array regardless of rack arrangement or boron concentration.               The maximum intended heat load from the proposed rack arrangement         would be less   than the heat load     if   all PWR fuel were stored in the A pool since         the   PWR   fuel constitutes a greater heat load when compared with the BWR fuel.
Since the llX11 BWR rack modules are interchangeable with 7X7 PWR rack modules it is acceptable to store spent BWR fuel in the A pool.
This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.           Thus, no unreviewed safety question exists.
The A pool meets all of the design and performance requirements as the B pool and can be used as a spent fuel pool with no changes to its cooling or purification capability.
FSAR Reference.
Rearrangement of the racks in the A pool has no effect on the maximum stored criticality since the individual racks are designed to maintain a subcritical array regardless of rack arrangement or boron concentration.
The maximum intended heat load from the proposed rack arrangement would be less than the heat load if all PWR fuel were stored in the A pool since the PWR fuel constitutes a greater heat load when compared with the BWR fuel.
This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.
: Thus, no unreviewed safety question exists.
FSAR Reference.
Section 9.1 HEM/HO-9100150/4/OS1
Section 9.1 HEM/HO-9100150/4/OS1


Change   to Plant as Described in the FSAR
Change to Plant as Described in the FSAR


==Title:==
==Title:==
PCR-001993,   Primary Sample Panel   '1A'entilation Modifications.
PCR-001993, Primary Sample Panel '1A'entilation Modifications.
Functional   Summar The Primary Sampling       System (PSS) is designed to collect fluid and gaseous samples   contained   in the Reactor Coolant System and Safety Injection System.
Functional Summar The Primary Sampling System (PSS) is designed to collect fluid and gaseous samples contained in the Reactor Coolant System and Safety Injection System.
It is     also   designed   to   collect fluid samples from the Boron Thermal Regeneration System,       Chemical   and Volume Control System, Steam Generator Blowdown System, residual heat removal heat exchangers, and a gas sample from the volume control tank and main steam.               The PSS provides samples in two sampling rooms in the Reactor Auxiliary Building, and brings them to a common location in the sampling rooms via 1A and 1B Primary Sample panels for analysis by the plant operating staff.
It is also designed to collect fluid samples from the Boron Thermal Regeneration
This plant modification increased the air flow rate exhausted from the Primary Sample Panel lA in order to assure proper capture velocity of contaminants generated during sampling. The air flow rate exhausted was increased from 300 CFM to 1000 CFM with all hood doors open.               This increase in air flow was accomplished by reducing air flow quantity to be exhausted from the service water discharge pipe tunnel without adversely affecting the pipe tunnel design space temperature.       Ductwork internal to the primary sample panel 1A from the sample vessel enclosure to the common exhaust header was increased from three inch to seven inch diameter.
: System, Chemical and Volume Control
This modification affects two Q-Class E systems.             1) The Reactor Auxiliary Building (RAB) Ventilation System (exhaust side) and, 2) the Primary Sampling
: System, Steam Generator Blowdown System, residual heat removal heat exchangers, and a gas sample from the volume control tank and main steam.
, System (ventilation portion only). Neither of the two systems are initiating or mitigating systems.
The PSS provides samples in two sampling rooms in the Reactor Auxiliary Building, and brings them to a common location in the sampling rooms via 1A and 1B Primary Sample panels for analysis by the plant operating staff.
The   subject   air flow changes do not effect structural integrity of the seismic designed     portion of ductwork of the RAB Normal Ventilation System as the operating pressure remains unchanged.
This plant modification increased the air flow rate exhausted from the Primary Sample Panel lA in order to assure proper capture velocity of contaminants generated during sampling.
This change does not increase levels of airborne contamination (radioactivity) released via the RAB vent stack nor does       it result in releases via unmonitored release points. The revision does result in more positive capture of airborne contaminants generated during sampling which increases safety of operations personnel.     The reduction in the exhaust flowrate from the service water discharge pipe tunnel does not result in space temperature increases above current design.
The air flow rate exhausted was increased from 300 CFM to 1000 CFM with all hood doors open.
This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment. malfunction than already evaluated in the FSAR.             Thus, no unreviewed safety question exls'ts ~
This increase in air flow was accomplished by reducing air flow quantity to be exhausted from the service water discharge pipe tunnel without adversely affecting the pipe tunnel design space temperature.
FSAR  
Ductwork internal to the primary sample panel 1A from the sample vessel enclosure to the common exhaust header was increased from three inch to seven inch diameter.
This modification affects two Q-Class E systems.
1)
The Reactor Auxiliary Building (RAB) Ventilation System (exhaust side)
: and, 2) the Primary Sampling
, System (ventilation portion only).
Neither of the two systems are initiating or mitigating systems.
The subject air flow changes do not effect structural integrity of the seismic designed portion of ductwork of the RAB Normal Ventilation System as the operating pressure remains unchanged.
This change does not increase levels of airborne contamination (radioactivity) released via the RAB vent stack nor does it result in releases via unmonitored release points.
The revision does result in more positive capture of airborne contaminants generated during sampling which increases safety of operations personnel.
The reduction in the exhaust flowrate from the service water discharge pipe tunnel does not result in space temperature increases above current design.
This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment. malfunction than already evaluated in the FSAR.
: Thus, no unreviewed safety question exls'ts
~
FSAR  


==Reference:==
==Reference:==
Figure 9.4.3-1 MEM/HO-9100150/5/OS1
Figure 9.4.3-1 MEM/HO-9100150/5/OS1


Change to Plant as Described in the FSAR Title'. PCR-002252, Snubber Reductions
Change to Plant as Described in the FSAR Title'.
.Functional Summar This plant modification abandons in place mechanical snubbers No. CS-H-963 and CS-H-968 from the Chemical and Volume Control System in the Reactor Auxiliary Building Elevation 261'-0. The snubbers were abandoned as part of a snubber reduction effort to reduce maintenance cost and man-rem exposure during testing and repair work.
PCR-002252, Snubber Reductions
This modification does not impact the function or operation of the Chemical and Volume Control System. The stress analysis and structural acceptability show that the abandonment of the snubbers is acceptable.
.Functional Summar This plant modification abandons in place mechanical snubbers No. CS-H-963 and CS-H-968 from the Chemical and Volume Control System in the Reactor Auxiliary Building Elevation 261'-0.
This change   does not increase the probability or consequences   of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR. Therefore, no unreviewed safety questions exists.
The snubbers were abandoned as part of a snubber reduction effort to reduce maintenance cost and man-rem exposure during testing and repair work.
FSAR
This modification does not impact the function or operation of the Chemical and Volume Control System.
The stress analysis and structural acceptability show that the abandonment of the snubbers is acceptable.
This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.
Therefore, no unreviewed safety questions exists.
FSAR  


==Reference:==
==Reference:==
Table 3.9.3-16 MEM/HO-9100150/6/OS1
Table 3.9.3-16 MEM/HO-9100150/6/OS1


Change to Plant as Described in the   FSAR
Change to Plant as Described in the FSAR


==Title:==
==Title:==
PCR-002290,       Waste Gas Analyzers Replacement Functional                 Summar
PCR-002290, Waste Gas Analyzers Replacement Functional Summar
                                    .'ach Hydrogen Recombiner Package of the Gaseous Waste Processing System (GWPS) includes a Gas Analyzer System. This plant modification replaces the existing Bendix Hydrogen and Oxygen Analyzer with functionally equivalent Teledyne analyzers for both non-safety A and B trains of the Catalytic Hydrogen Recombiner Package.
.'ach Hydrogen Recombiner Package of the Gaseous Waste Processing System (GWPS) includes a Gas Analyzer System.
The   analyzer changeout facilitated "installation of new flow control panels, rework of the existing tubing from the hydrogen recombiner skids to the gas analyzer racks and an increase in the compressor suction line size to minimize system backpressure.                           Also, the new Teledyne analyzers cannot be damaged during no-flow conditions (system shut-down), therefore, deleting the need for low flow de-energization of the analyzers.
This plant modification replaces the existing Bendix Hydrogen and Oxygen Analyzer with functionally equivalent Teledyne analyzers for both non-safety A
This plant modification incorporates                           changes to improve the GWPS performance and   reliability.                       The electrical portion of this   system is fed from a non-ESF supply which is not required to operate during an emergency shutdown.                                 The instrumentation and control functions of the GWPS as described in FSAR Section 11.3.2.2.2 have not been affected by the Teledyne Analyzer changeout.
and B trains of the Catalytic Hydrogen Recombiner Package.
Control signal failure probability has been decreased due to the deletion of the low-flow analyzer shutdown, which is not required for the Teledyne Analyzers. Leaving the Teledyne Analyzers energized during system shutdown or no-flow conditions will have no adverse impact on the analyzers themselves nor system operation or availability.
The analyzer changeout facilitated "installation of new flow control panels, rework of the existing tubing from the hydrogen recombiner skids to the gas analyzer racks and an increase in the compressor suction line size to minimize system backpressure.
: Also, the new Teledyne analyzers cannot be damaged during no-flow conditions (system shut-down), therefore, deleting the need for low flow de-energization of the analyzers.
This plant modification incorporates changes to improve the GWPS performance and reliability.
The electrical portion of this system is fed from a non-ESF supply which is not required to operate during an emergency shutdown.
The instrumentation and control functions of the GWPS as described in FSAR Section 11.3.2.2.2 have not been affected by the Teledyne Analyzer changeout.
Control signal failure probability has been decreased due to the deletion of the low-flow analyzer
: shutdown, which is not required for the Teledyne Analyzers.
Leaving the Teledyne Analyzers energized during system shutdown or no-flow conditions will have no adverse impact on the analyzers themselves nor system operation or availability.
The increase in the compressor suction line size has no adverse affect on the
The increase in the compressor suction line size has no adverse affect on the
'system or plant operation. The line is designed and constructed in accordance with the original codes.                               The two lines being moved are designed         and constructed to the original codes.                           The relocation   will not adversely affect any system.                     The redesigned lines are not routed over any safety related equipment.                   No new crossties between equipment or systems are being made by this plant modification.
'system or plant operation.
The GWPS performs no function related to the safe shutdown of the                           plant. This change                   does not increase           the probability or consequences       of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.                               Thus, no unreviewed safety question
The line is designed and constructed in accordance with the original codes.
,exists.
The two lines being moved are designed and constructed to the original codes.
The relocation will not adversely affect any system.
The redesigned lines are not routed over any safety related equipment.
No new crossties between equipment or systems are being made by this plant modification.
The GWPS performs no function related to the safe shutdown of the plant.
This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.
: Thus, no unreviewed safety question
,exists.
PSAR
PSAR
        'Reference.'ection 11.3.2 and 9.5 HEM/H0-9100150/7/OSl
'Reference.'ection 11.3.2 and 9.5 HEM/H0-9100150/7/OSl


Change to Plant As Described in the FSAR
Change to Plant As Described in the FSAR


==Title:==
==Title:==
PCR-002297,   Corrosion. Product Sampler Install'ation Functi'onal       Summar This plant modification to the Secondary Sampling System               installs iron and copper corrosion monitors on the following sample lines'.
PCR-002297, Corrosion. Product Sampler Install'ation Functi'onal Summar This plant modification to the Secondary Sampling System installs iron and copper corrosion monitors on the following sample lines'.
a)   Condensate pump discharge b)   High pressure heater drains c)   Feedwater to the steam generators These         monitors are installed to determine the volume of corrosion products entering the steam generators. The monitors also provide an indication of the source of the majority of corrosion products.
a)
The       corrosion products monitors are designed to meet or exceed the secondary sample system design pressures             and temperatures with one exception.     The feedwater to the steam generators sample point design pressure is 2000 psig while the corrosion monitor design pressure is 1500 psig. A pressure relief valve set at 1500 psig maximum is installed per this modification on the corrosion monitor inlet sample line to prevent monitor overpressurization in the event the sample line pressure exceeds 1500 psig. The secondary sample system is Quality Classification E which is assumed to fail during a seismic event and release any sample liquid to the equipment drains for processing.
Condensate pump discharge b)
Failure of the corrosion monitors will not increase the consequences of a radioactive release over what is presently analyzed. The corrosion monitors are designed using stainless steeL materials to minimize corrosion and erosion. The table on which the corrosion monitors are mounted is designed to capture any leakage from the monitors and direct it to the equipment drain.
High pressure heater drains c)
This change does not increase the probability or consequences af analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.               Thus, no unreviewed safety question exists'SAR
Feedwater to the steam generators These monitors are installed to determine the volume of corrosion products entering the steam generators.
The monitors also provide an indication of the source of the majority of corrosion products.
The corrosion products monitors are designed to meet or exceed the secondary sample system design pressures and temperatures with one exception.
The feedwater to the steam generators sample point design pressure is 2000 psig while the corrosion monitor design pressure is 1500 psig.
A pressure relief valve set at 1500 psig maximum is installed per this modification on the corrosion monitor inlet sample line to prevent monitor overpressurization in the event the sample line pressure exceeds 1500 psig.
The secondary sample system is Quality Classification E which is assumed to fail during a seismic event and release any sample liquid to the equipment drains for processing.
Failure of the corrosion monitors will not increase the consequences of a
radioactive release over what is presently analyzed.
The corrosion monitors are designed using stainless steeL materials to minimize corrosion and erosion.
The table on which the corrosion monitors are mounted is designed to capture any leakage from the monitors and direct it to the equipment drain.
This change does not increase the probability or consequences af analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.
: Thus, no unreviewed safety question exists'SAR


==Reference:==
==Reference:==
Section 9.3.2.2.2 MEN/HO-9100150/8/OS1
Section 9.3.2.2.2 MEN/HO-9100150/8/OS1


Line 131: Line 230:
v 1
v 1


Change to Plant as Described in the         FSAR
Change to Plant as Described in the FSAR


==Title:==
==Title:==
PCR-003701,     Removal of Flow Switches FS-7001A and FS-7001B from the Environmental Qualification Program.
PCR-003701, Removal of Flow Switches FS-7001A and FS-7001B from the Environmental Qualification Program.
Functional   Summar This plant modification was issued to remove Flow Switches FS-7001A and FS-7001B from the Environmental Qualification (EQ) Program.                   FS-7001A and FS-7001B function as redundant,           ,safety-grade instrumentation monitoring the component cooling water (CCW) flow via a common header (3CC6-201SN"1) from all three reactor coolant pumps. If 'CCW flow decreases to the low flow setpoint, alarms are initiated at the monitor light boxes (MLB-4A and MLB-4B) and ERFIS messages for Points FRC-7001C and FRC-7001D are generated.                   Low CCW flow to the RCP oil coolers requires Operator action to restore the CCW flow or to take other steps, as deemed appropriate by Operations.                 The flow switches are located in the Reactor Auxiliary Building above Elevation 236'n Line 3CC6-201SN-1. This location makes         it difficult for plant technicians to perform EQ mandated   calibrations.
Functional Summar This plant modification was issued to remove Flow Switches FS-7001A and FS-7001B from the Environmental Qualification (EQ)
As   detailed above,     FS-7001A and FS-7001B         monitor CCW flow from the reactor coolant pumps     bearing oil coolers.         The   flow switches are safety grade and during normal operation, the location of FS-7001A and FS-7001B is mild for both temperature and radiation.           Therefore, the only time the flow switches are subjected to a harsh environment is post design basis accident (DBA). If there is a spurious loss of CCW, not associated with a DBA, FS-7001A and
Program.
~FS-7001B will function as designed,             and there will be no change in their operating environment.
FS-7001A and FS-7001B function as redundant,
In the event of a DBA the containment will be placed in Phase "A" isolation either by the initiation of Safety Injection or manually from the Main Control Board. Phase "A" isolation does not isolate the CCW from the reactor coolant pumps (RCPs).     This allows these pumps to operate during safety injection and will also allow the operators sufficient time to shutdown the RCP's prior to Phase "B" isolation which does secure the component cooling water.                   The RCP's however,   are not safety related   devices   and as such cannot be considered   to be available   following   a DBA. In   addition,   there   is no postulated   accident   in which the RCPs   are utilized   for   accident   mitigation. Therefore,   the basis for removing FS-7001A and FS-7001B from the EQ Program is, they will perform their safety function prior to an accident in a mild environment.                     They are not required to operate after a Design         Basis   accident   when a harsh environment   is created.
,safety-grade instrumentation monitoring the component cooling water (CCW) flow via a common header (3CC6-201SN"1) from all three reactor coolant pumps.
This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than 'lready evaluated in the FSAR.               Thus, no unreviewed safety question exls'ts FSAR  
If 'CCW flow decreases to the low flow setpoint, alarms are initiated at the monitor light boxes (MLB-4A and MLB-4B) and ERFIS messages for Points FRC-7001C and FRC-7001D are generated.
Low CCW flow to the RCP oil coolers requires Operator action to restore the CCW flow or to take other steps, as deemed appropriate by Operations.
The flow switches are located in the Reactor Auxiliary Building above Elevation 236'n Line 3CC6-201SN-1.
This location makes it difficult for plant technicians to perform EQ mandated calibrations.
As detailed
: above, FS-7001A and FS-7001B monitor CCW flow from the reactor coolant pumps bearing oil coolers.
The flow switches are safety grade and during normal operation, the location of FS-7001A and FS-7001B is mild for both temperature and radiation.
Therefore, the only time the flow switches are subjected to a harsh environment is post design basis accident (DBA). If there is a
spurious loss of
: CCW, not associated with a
: DBA, FS-7001A and
~FS-7001B will function as
: designed, and there will be no change in their operating environment.
In the event of a DBA the containment will be placed in Phase "A" isolation either by the initiation of Safety Injection or manually from the Main Control Board.
Phase "A" isolation does not isolate the CCW from the reactor coolant pumps (RCPs).
This allows these pumps to operate during safety injection and will also allow the operators sufficient time to shutdown the RCP's prior to Phase "B" isolation which does secure the component cooling water.
The RCP's however, are not safety related devices and as such cannot be considered to be available following a DBA.
In addition, there is no postulated accident in which the RCPs are utilized for accident mitigation.
Therefore, the basis for removing FS-7001A and FS-7001B from the EQ Program is, they will perform their safety function prior to an accident in a mild environment.
They are not required to operate after a Design Basis accident when a harsh environment is created.
This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than 'lready evaluated in the FSAR.
: Thus, no unreviewed safety question exls'ts FSAR  


==REFERENCE:==
==REFERENCE:==
Table 3.11.0-7 MEM/H0-9100150/9/OS1
Table 3.11.0-7 MEM/H0-9100150/9/OS1


Change to Plant as Described in the   FSAR
Change to Plant as Described in the FSAR


==Title:==
==Title:==
PCR-003754, Chemical and Volume Control System (CVCS) Heat Exchanger Performance Thermometer Deletion.
PCR-003754, Chemical and Volume Control System (CVCS) Heat Exchanger Performance Thermometer Deletion.
Functional   Summar This plant modification removed         temperature   indicators associated   with the CVCS,due to ALARA concerns.
Functional Summar This plant modification removed temperature indicators associated with the CVCS,due to ALARA concerns.
Temperature     indicators TI-Ol-CS-7241, TI-01-CS-7243, and TI-Ol-CS-7244 are located in high radiation areas and present ALARA implications during ILRT and
Temperature indicators TI-Ol-CS-7241, TI-01-CS-7243, and TI-Ol-CS-7244 are located in high radiation areas and present ALARA implications during ILRT and
,routine calibration activities. These Dresser dial thermometers provide local indication of CVCS Regenerative and Excess Letdown Heat Exchanger performance; however, this temperature monitoring is not utilized for performance trending due to local exposure rates.         Temperature elements TE-01-CS-0123, TE-01-CS-0139, and   TE-01-CS-0140   provide Main'"control Room monitoring of Heat Exchanger outlet temperature making the subject       indicators expendable.
,routine calibration activities.
The subject indicators have been removed and threaded pipe plugs installed in the existing thermowells with necessary sealant.
These Dresser dial thermometers provide local indication of CVCS Regenerative and Excess Letdown Heat Exchanger performance; however, this temperature monitoring is not utilized for performance trending due to local exposure rates.
The   affected thermometers     are installed at the   CVCS Regenerative and Excess Letdown Heat Exchangers,     monitoring inlet/outlet temperature. These devices, providing performance related local indications, render no control functions and are not necessary for Plant Process Display or Post Accident Monitoring.
Temperature elements TE-01-CS-0123, TE-01-CS-
: 0139, and TE-01-CS-0140 provide Main'"control Room monitoring of Heat Exchanger outlet temperature making the subject indicators expendable.
The subject indicators have been removed and threaded pipe plugs installed in the existing thermowells with necessary sealant.
The affected thermometers are installed at the CVCS Regenerative and Excess Letdown Heat Exchangers, monitoring inlet/outlet temperature.
These
: devices, providing performance related local indications, render no control functions and are not necessary for Plant Process Display or Post Accident Monitoring.
This modification, deleting unnecessary instrumentation, does not degrade plant safety considering its effect on accident-initiating systems; accident-mitigating systems, or key safety considerations.
This modification, deleting unnecessary instrumentation, does not degrade plant safety considering its effect on accident-initiating systems; accident-mitigating systems, or key safety considerations.
This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.           Thus, no unreviewed safety question exists.
This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.
FSAR
: Thus, no unreviewed safety question exists.
FSAR  


==Reference:==
==Reference:==
Figure 9.3.4-1 MEM/HO-9100150/10/Osl
Figure 9.3.4-1 MEM/HO-9100150/10/Osl


Change to Plant as Described in the   FSAR Title.'CR       004192, Replacement     of Turbine Trip Condenser   Vacuum Switches.
Change to Plant as Described in the FSAR Title.'CR 004192, Replacement of Turbine Trip Condenser Vacuum Switches.
Functional   Summar This     plant modification was necessary             due   to the poor performance characteristics of the turbine trip condenser vacuum switches PS-4131AV thru DV and the fact that Westinghouse           revised the vacuum trip setpoint.       New turbine vacuum pressure switches and circuitry have been installed.
Functional Summar This plant modification was necessary due to the poor performance characteristics of the turbine trip condenser vacuum switches PS-4131AV thru DV and the fact that Westinghouse revised the vacuum trip setpoint.
New turbine vacuum pressure switches and circuitry have been installed.
Specifically, this modification replaces the existing United Electric pressure
Specifically, this modification replaces the existing United Electric pressure
.switches with Static 'O'ing (SOR) pressure switches which have proven more reliable, adds a separate pressure switch for pre-trip alarm and revised control circuitry such that a setpoint change occurs at an increase of approximately   60% power from the low     setpoint (5.0 InHg) to the high setpoint (7.5 InHg).
.switches with Static 'O'ing (SOR) pressure switches which have proven more
Presently during the summer months reactor power reduction is required to prevent a turbine trip on low condenser vacuum. This has been attributed in part to the reduction in cooling tower efficiency and miscellaneous water chemistry make up.         Per Westinghouse recommendation, at approximately 60%
: reliable, adds a
separate pressure switch for pre-trip alarm and revised control circuitry such that a
setpoint change occurs at an increase of approximately 60%
power from the low setpoint (5.0 InHg) to the high setpoint (7.5 InHg).
Presently during the summer months reactor power reduction is required to prevent a turbine trip on low condenser vacuum.
This has been attributed in part to the reduction in cooling tower efficiency and miscellaneous water chemistry make up.
Per Westinghouse recommendation, at approximately 60%
power the condenser vacuum turbine trip setpoint should be increased from 5.0 InHg to 7.5 InHg to allow the unit to operate at full power production.
power the condenser vacuum turbine trip setpoint should be increased from 5.0 InHg to 7.5 InHg to allow the unit to operate at full power production.
This has been achieved by installing a relay which will energize at approx.
This has been achieved by installing a relay which will energize at approx.
60X power and switch the dual Hi-Lo SOR pressure switch from the low setpoint to the high setpoint.           New alarm pressure     switch PS-4131EV will also be switched via the same relay to provide operators pre-trip warning at 4.0 InHg below 60X power and 6.5 InHg above 60% power. The additional alarm relay will replace one of the DEH fluid low pressure trip switches.
60X power and switch the dual Hi-Lo SOR pressure switch from the low setpoint to the high setpoint.
This enhancement       does   not effect   the original design intent of the low condenser   vacuum   trip circuit as     discussed in FSAR 10.2.5 but allows for increased unit   reliability and availability.
New alarm pressure switch PS-4131EV will also be switched via the same relay to provide operators pre-trip warning at 4.0 InHg below 60X power and 6.5 InHg above 60% power.
This change   does not increase the probability or consequences         of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.             Thus, no,unreviewed safety question exists.
The additional alarm relay will replace one of the DEH fluid low pressure trip switches.
FSAR
This enhancement does not effect the original design intent of the low condenser vacuum trip circuit as discussed in FSAR 10.2.5 but allows for increased unit reliability and availability.
This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.
: Thus, no,unreviewed safety question exists.
FSAR  


==Reference:==
==Reference:==
Figures 10.2.2-08, 10.2.2-10 MEM/HO-9100150/11/OS1
Figures 10.2.2-08, 10.2.2-10 MEM/HO-9100150/11/OS1


Change to Plant as Described in the   FSAR Title.'CR-004506, Deactivation of           the Chlorine Detection System.
Change to Plant as Described in the FSAR Title.'CR-004506, Deactivation of the Chlorine Detection System.
Functional   Summar This plant modification deactivated the chlorine detection system. Technical Specification 3.3.3.7, Amendment 8, stated that two independent chlorine detection trains be operable whenever liquid chlorine is present at the onsite chlorine storage area in quantities greater than 20 lbs. SHNPP no longer stores chlorine in large quantities on site, therefore, this system is no longer required. Amendment ten (10) of the SHNPP Technical Specifications deleted the Chlorine detection System from Technical Specifications.
Functional Summar This plant modification deactivated the chlorine detection system.
The Chlorine Detection System consisted of two independent chlorine detector trains with each train consisting of a detector at each Control Room System intake (both normal and emergency) and a detector at the   Area'entilation chlorine storage area.
Technical Specification 3.3.3.7, Amendment 8,
The storage   area detectors   alarm and isolate the control room in the event of a release. of chlorine at the storage area.           CP&L does not store large quantities (i.e., quantities greater than 20 pounds) of liquid chlorine onsite at Harris. Therefore, the accidental onsite release of such a small quantity of chlorine would not affect the plant operators. As such, deletion of the storage area chlorine detectors will not increase the consequences             of an accidental onsite release of chlorine.           The deactivation of the Chlorine Detection System will also avoid inadvertent control room isolations.
stated that two independent chlorine detection trains be operable whenever liquid chlorine is present at the onsite chlorine storage area in quantities greater than 20 lbs.
The   chlorine detectors located at the Control Room Area Ventilation System intakes are intended to provide protection in the event of an accidental offsite release of chlorine.           A probabilistic risk assessment     (PRA) was performed to determine the probability of an accidental chlorine release in the vicinity of Harris.         The results of the analysis showed that offsite chlorine release accidents have such a low probability that they are not considered to be credible events.
SHNPP no longer stores chlorine in large quantities on site, therefore, this system is no longer required.
This change   does   not increase   the probability or consequences of analyzed
Amendment ten (10) of the SHNPP Technical Specifications deleted the Chlorine detection System from Technical Specifications.
'ccidents, nor introduce       a different type of accident or equipment malfunction than already     evaluated   in the   FSAR. Thus, no unreviewed safety question exists.
The Chlorine Detection System consisted of two independent chlorine detector trains with each train consisting of a detector at each Control Room Area'entilation System intake (both normal and emergency) and a detector at the chlorine storage area.
FSAR
The storage area detectors alarm and isolate the control room in the event of a
release.
of chlorine at the storage area.
CP&L does not store large quantities (i.e., quantities greater than 20 pounds) of liquid chlorine onsite at Harris.
Therefore, the accidental onsite release of such a small quantity of chlorine would not affect the plant operators.
As such, deletion of the storage area chlorine detectors will not increase the consequences of an accidental onsite release of chlorine.
The deactivation of the Chlorine Detection System will also avoid inadvertent control room isolations.
The chlorine detectors located at the Control Room Area Ventilation System intakes are intended to provide protection in the event of an accidental offsite release of chlorine.
A probabilistic risk assessment (PRA) was performed to determine the probability of an accidental chlorine release in the vicinity of Harris.
The results of the analysis showed that offsite chlorine release accidents have such a
low probability that they are not considered to be credible events.
This change does not increase the probability or consequences of analyzed
'ccidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.
: Thus, no unreviewed safety question exists.
FSAR  


==Reference:==
==Reference:==
Sections 1.8, 2.2, 3 1, 6.4, 7.2, 7.3, 9.4, 9.5 MEM/HO-9100150/12/OS1


Sections 1.8, 2.2,    3 1, 6.4, 7.2, 7.3, 9.4, 9.5 MEM/HO-9100150/12/OS1
Title.
 
Change to Plant as Described in the FSAR PCR-004695, Removal of the Main Steam Power Operated Relief Valve (PORV) Actuators from the Environmental Qualification (EQ) Program.
Change   to Plant as Described in the FSAR Title. PCR-004695,   Removal of the Main Steam Power Operated   Relief Valve (PORV) Actuators from the Environmental Qualification     (EQ) Program.
Functional Summar The Main Steam
Functional Summar The Main Steam   PORVs,   located in the Main Steam Tunnel,   utilize an Electro-Hydrologic   actuator   manufactured by Paul Monroe-Enertech.         This plant modification   removed   these actuators from the Harris Plants EQ Program. The requirement for these actuators to be environmentally qualified was re-evaluated by this modification.       It was determined that the subject actuators are not required to mitigate any       FSAR Chapter 15 analyzed event that could result in an elevated temperature or pressure in the area of the steam tunnel.
: PORVs, located in the Main Steam Tunnel, utilize an Electro-Hydrologic actuator manufactured by Paul Monroe-Enertech.
Since these   actuators are not required to mitigate a Chapter 15 event that could cause an elevated temperature or pressure in the steam tunnel, it is unnecessary to maintain their EQ status.
This plant modification removed these actuators from the Harris Plants EQ Program.
This change does not increase the probability or consequences of analyzed accidents, no introduce a different type of accident or equipment malfunction than already evaluated in the FSAR. Thus, no unreviewed safety question exists.
The requirement for these actuators to be environmentally qualified was re-evaluated by this modification. It was determined that the subject actuators are not required to mitigate any FSAR Chapter 15 analyzed event that could result in an elevated temperature or pressure in the area of the steam tunnel.
FSAR Reference.
Since these actuators are not required to mitigate a
Chapter 15 event that could cause an elevated temperature or pressure in the steam tunnel, it is unnecessary to maintain their EQ status.
This change does not increase the probability or consequences of analyzed accidents, no introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.
: Thus, no unreviewed safety question exists.
FSAR Reference.
Table 3.11.0-2 MEM/HO-9100150/13/OS1
Table 3.11.0-2 MEM/HO-9100150/13/OS1


Change to Plant as Described in the FSAR
Change to Plant as Described in the FSAR


==Title:==
==Title:==
PCR-004930,     Instrument Air Check Valve.
PCR-004930, Instrument Air Check Valve.
Functional                   Summar This plant modification installs a 3" 1508 carbon steel welded swing check valve i'n the Instrument Air (IA) System. The check valve is installed in the main supply header into the Radiation Control Areas (RCA) (i.e., Reactor Auxiliary Building, Containment Building) to prevent any reverse flow. in the system flow path.
Functional Summar This plant modification installs a
During routine plant shutdown surveillance testing, improper work activities by test personnel caused radiological contamination of various piping sections of the IA system. This situation created immediate concerns due to IA system flow path contamination inside the RCA, along with potential problems regarding leakage paths outside the RCA via the IA supply header which crosses
3" 1508 carbon steel welded swing check valve i'n the Instrument Air (IA) System.
The check valve is installed in the main supply header into the Radiation Control Areas (RCA) (i.e.,
Reactor Auxiliary Building, Containment Building) to prevent any reverse flow. in the system flow path.
During routine plant shutdown surveillance
: testing, improper work activities by test personnel caused radiological contamination of various piping sections of the IA system.
This situation created immediate concerns due to IA system flow path contamination inside the
: RCA, along with potential problems regarding leakage paths outside the RCA via the IA supply header which crosses
. the RCA boundary.
. the RCA boundary.
The   immediate                   problems were resolved       by flushing the affected piping until samples showed contamination levels                         within acceptable levels inside the RCA boundary and by restricting use of                         the Emergency Breathing Air System. The potential problem regarding IA system leakage paths outside the RCA boundary is being addressed by the instaLlation of the subject check valve.
The immediate problems were resolved by flushing the affected piping until samples showed contamination levels within acceptable levels inside the RCA boundary and by restricting use of the Emergency Breathing Air System.
The   IA system,                   a part of the Compressed Air System originates in the Turbine Building and provides "instrument quality" air via piping to the Turbine Building, Reactor Auxiliary Building, and Containment Building.
The potential problem regarding IA system leakage paths outside the RCA boundary is being addressed by the instaLlation of the subject check valve.
The Compressed                       Air System   (CAS) is not required for the initiation of any engineered safety feature systems, safe shutdown system, or any other safety-related system.                       Therefore, the CAS is considered non-nuclear safety except for the containment penetrations and the valve accumulators.
The IA system, a part of the Compressed Air System originates in the Turbine Building and provides "instrument quality" air via piping to the Turbine Building, Reactor Auxiliary Building, and Containment Building.
A major                 piping or component failure in the Turbine Building could cause rapid depressurization of the IA flow path, thereby creating a reverse flow to outside the RAB and RCA. 'This event could cause release of radioactive contamination to the environment. The installation of the subject check valve provides means to prevent this type of occurrence.
The Compressed Air System (CAS) is not required for the initiation of any engineered safety feature
During and                   after an accident there are no air-operated valves that require cycling                 to   bring the plant to safe shutdown. The accident analyses does not assume                 the   instrument air system to be operable and does not take credit for the system.
: systems, safe shutdown
This change                     does   not increase the probability or consequences of analyzed accidents, nor                   introduce   a different type of accident or equipment malfunction than already evaluated                       in the FSAR. Thus, no unreviewed safety question exists.
: system, or any other safety-related system.
Therefore, the CAS is considered non-nuclear safety except for the containment penetrations and the valve accumulators.
A major piping or component failure in the Turbine Building could cause rapid depressurization of the IA flow path, thereby creating a
reverse flow to outside the RAB and RCA.
'This event could cause release of radioactive contamination to the environment.
The installation of the subject check valve provides means to prevent this type of occurrence.
During and after an accident there are no air-operated valves that require cycling to bring the plant to safe shutdown.
The accident analyses does not assume the instrument air system to be operable and does not take credit for the system.
This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.
: Thus, no unreviewed safety question exists.
FSAR Reference.'igure 9.3.1-3 MEM/HO-9100150/14/OS1
FSAR Reference.'igure 9.3.1-3 MEM/HO-9100150/14/OS1


V
V
    'V V
'V V
yt
yt


Change to Plant as Described in the       FSAR
Change to Plant as Described in the FSAR


==Title:==
==Title:==
PCR-004984, Emergency   Service Water   (ESW) System Minimum   Flows/Plow Balancing Functional     Summar Engineering Evaluation PCR-004984 established revised minimum service water flow requirements for various ESW loads and evaluated flow balances for acceptability based on the new',miftimum flows. As previously designed, no margin existed in the configuration of the ESW system to allow for degradation due to the highly conservative f'low requirements.             The new flow values were established for the worst-case condition with the ESW pumps aligned to the Main Reservoir with a level of 205.7 feet mean sea level with a water temperature of 95'F (Tech. Spec. 3/4.7.5).
PCR-004984, Emergency Service Water (ESW)
A summary     of required FSAR Table 9.2.1-1 changes is as follows'.
System Minimum Flows/Plow Balancing Functional Summar Engineering Evaluation PCR-004984 established revised minimum service water flow requirements for various ESW loads and evaluated flow balances for acceptability based on the new',miftimum flows.
~corn onent                         Old Value               New  Value Component    Cooling              12,000 gpm             9,000   gpm Water Heat Exchanger Standby Diesel                       1,250 gpm               900 gpm Generator Coolers Containment Fan                     3,000 gpm             2,850 gpm Coolers Reactor Auxiliary Bldg.             2,500 gpm             2,420 gpm HVAC  Chillers The ESW   system is an accident mitigating system. The reduced flow rates             still provide adequate margin for accident mitigation.                   This change- does not increase the probability       of consequences   of analyzed   accidents, nor introduce a different type of     accident   or equipment   malfunction   than already   evaluated in the FSAR. No unreviewed safety         question   exists.
As previously
FSAR  
: designed, no margin existed in the configuration of the ESW system to allow for degradation due to the highly conservative f'low requirements.
The new flow values were established for the worst-case condition with the ESW pumps aligned to the Main Reservoir with a
level of 205.7 feet mean sea level with a
water temperature of 95'F (Tech.
Spec. 3/4.7.5).
A summary of required FSAR Table 9.2.1-1 changes is as follows'.
~corn onent Component Cooling Water Heat Exchanger Old Value 12,000 gpm New Value 9,000 gpm Standby Diesel Generator Coolers 1,250 gpm 900 gpm Containment Fan Coolers 3,000 gpm 2,850 gpm Reactor Auxiliary Bldg.
HVAC Chillers 2,500 gpm 2,420 gpm The ESW system is an accident mitigating system.
The reduced flow rates still provide adequate margin for accident mitigation.
This change-does not increase the probability of consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.
No unreviewed safety question exists.
FSAR  


==Reference:==
==Reference:==
Table 9.2.1-1 MEM/HO-9100150/15/Osl
Table 9.2.1-1 MEM/HO-9100150/15/Osl


Change to Plant as Described in the     FSAR
Change to Plant as Described in the FSAR


==Title:==
==Title:==
PCR-005021, Engineering Evaluation     of Emergency Core Cooling System (ECCS) Flow Inconsistencies.
PCR-005021, Engineering Evaluation of Emergency Core Cooling System (ECCS)
Functional   Summar In   December   of 1989, Westinghouse informed Carolina Power & Light Company of inconsistencies found between the Harris plant ECCS flow rates assumed in the input to the Westinghouse supplied Loss-Of-Coolant Accident (LOCA) Analyses used to demonstrate compliance with the requirements of 10CFR50.46 and the flows allowed by the Harris Technical Specifications.
Flow Inconsistencies.
Specifically,     the issue of concern was that the Harris Technical Specifications allowed for 31 gpm of reactor coolant pump (RCP) seal injection flow at normal charging pump conditions (at 2250 psia) versus an assumed 24 gpm (at 2250 psia) used in the gene@ation of ECCS flow data for the Harris Safety Analyses.         Since these flow values       correspond     to   specific   seal injection line resistance,         it was   seen   that   the   seal     injection actually line less resistance, associated with the Technical Specifications,             was than that assumed in the calculations. Therefore, additional             charging/SI   flow would be pumped through the seal injection line potentially                 resulting   in a reduction of flow injected into the core.
Functional Summar In December of 1989, Westinghouse informed Carolina Power
Since the potentially lower ECCS flow to the reactor core would ultimately impact the FSAR, Chapter 15, Lost-of-Coolant Accident Analyses provided by Westinghouse,'n evaluation of the discrepancy was performed by Westinghouse.
& Light Company of inconsistencies found between the Harris plant ECCS flow rates assumed in the input to the Westinghouse supplied Loss-Of-Coolant Accident (LOCA) Analyses used to demonstrate compliance with the requirements of 10CFR50.46 and the flows allowed by the Harris Technical Specifications.
Specifically, the issue of concern was that the Harris Technical Specifications allowed for 31 gpm of reactor coolant pump (RCP) seal injection flow at normal charging pump conditions (at 2250 psia) versus an assumed 24 gpm (at 2250 psia) used in the gene@ation of ECCS flow data for the Harris Safety Analyses.
Since these flow values correspond to specific seal injection line resistance, it was seen that the seal injection line resistance, associated with the Technical Specifications, was actually less than that assumed in the calculations.
Therefore, additional charging/SI flow would be pumped through the seal injection line potentially resulting in a
reduction of flow injected into the core.
Since the potentially lower ECCS flow to the reactor core would ultimately impact the
: FSAR, Chapter 15, Lost-of-Coolant Accident Analyses provided by Westinghouse,'n evaluation of the discrepancy was performed by Westinghouse.
The evaluation showed that the increase in peak cladding temperature (PCT),
The evaluation showed that the increase in peak cladding temperature (PCT),
due to the reduction in safety injection flow to the core was within the bounds of the PCT limits as defined in the Harris Technical Specifications.
due to the reduction in safety injection flow to the core was within the bounds of the PCT limits as defined in the Harris Technical Specifications.
Based   on the foregoing evaluation,   it   is determined that, pursuant to the criteria specified in 10CFR 50.59, the       existence   of the discrepancy between the seal injection line resistance allowed by the       Technical     Specifications and that assumed in the safety analysis does not           involve   an   unreviewed safety question.
Based on the foregoing evaluation, it is determined
Because   of the effects of steam/water condensation in the RCS loops, the computer model has been shown to be sensitive to reductions in safety injection flow. As a result FSAR Table 6.2.1-36 (Double Ended Pump Suction Guillotine Min. SI Reflood Mass and Energy Releases) and Table 6.2.1-41 (Double Ended Pump Suction Guillotine Min. SI Post-Reflood               Mass   and Energy Releases) are being revised to reflect new release data.
: that, pursuant to the criteria specified in 10CFR 50.59, the existence of the discrepancy between the seal injection line resistance allowed by the Technical Specifications and that assumed in the safety analysis does not involve an unreviewed safety question.
Because of the effects of steam/water condensation in the RCS
: loops, the computer model has been shown to be sensitive to reductions in safety injection flow.
As a result FSAR Table 6.2.1-36 (Double Ended Pump Suction Guillotine Min.
SI Reflood Mass and Energy Releases) and Table 6.2.1-41 (Double Ended Pump Suction Guillotine Min.
SI Post-Reflood Mass and Energy Releases) are being revised to reflect new release data.
FSAR Reference.
FSAR Reference.
Tables 6.2.1-36 and 6.2.1-41 MEM/HO-9100150/16/OS1
Tables 6.2.1-36 and 6.2.1-41 MEM/HO-9100150/16/OS1


Change to Plant as Described   in the FSAR
Change to Plant as Described in the FSAR


==Title:==
==Title:==
PCR-005157,   Secondary   Protection to   ARP-19B   Electrical   Containment Penetration Circuits.
PCR-005157, Secondary Protection to ARP-19B Electrical Containment Penetration Circuits.
Functional   Summar Electrical Containment Penetration circuits, safety related and non-safety related, are to be protected against overcurrent to prevent penetration conductor damage. In all cases, the penetration circuit protection consist of a primary and back-up (secondary) disconnecting device which can each limit the maximum I t at the penetration to a value less than that required for thermal damage to the penetration conductor.
Functional Summar Electrical Containment Penetration
During   a comparison,   between Maintenance     Surveillance Test   MST-E0007 "120/208 VAC   Molded Case Circuit Breaker Test" and electrical                 Calculation 30-PKR "Electrical Penetration Protection (Reg. guide 1.63), it             was determined that the existing 30 amp breaker did not provide sufficient protection against instantaneous     short   circuit current     to prevent   possible   damage   to   the penetration.
: circuits, safety related and non-safety
This modification adds two dual element" time delay fuses, Bussman type FRN-R20 to the penetration circuits. Existing fuse holders in ARP-19B (SB) were used and only wiring the internal jumpers was required                     to 'implement this modification. New jumper cables will be added and             some will be replaced as a result of this modification.
: related, are to be protected against overcurrent to prevent penetration conductor damage.
The new fuses     will provide sufficient     conductor protection for the       electrical penetrations.
In all cases, the penetration circuit protection consist of a primary and back-up (secondary) disconnecting device which can each limit the maximum I t at the penetration to a value less than that required for thermal damage to the penetration conductor.
The type     of fuse selected is a Buss type FRN-R which is already used for protection on other electrical penetrations. The existing spare fuse holders in the ARP-19B are compatible with the FRN-R Fuse.                   The circuit is not degraded by the addition of the new fus'es.           It provides proper coordination between primary and secondary protection of the electrical penetrations in the event of circuit fault currents.
During a comparison, between Maintenance Surveillance Test MST-E0007 "120/208 VAC Molded Case Circuit Breaker Test" and electrical Calculation 30-PKR "Electrical Penetration Protection (Reg.
This change   does not increase the probability or consequences               of analyzed accidents,   nor introduce   a different type   of accident   or equipment   malfunction than already     evaluated   in the FSAR. Thus,   no unreviewed   safety   question exists.
guide 1.63), it was determined that the existing 30 amp breaker did not provide sufficient protection against instantaneous short circuit current to prevent possible damage to the penetration.
FSAR References.
This modification adds two dual element" time delay fuses, Bussman type FRN-R20 to the penetration circuits.
Existing fuse holders in ARP-19B (SB) were used and only wiring the internal jumpers was required to
'implement this modification.
New jumper cables will be added and some will be replaced as a
result of this modification.
The new fuses will provide sufficient conductor protection for the electrical penetrations.
The type of fuse selected is a
Buss type FRN-R which is already used for protection on other electrical penetrations.
The existing spare fuse holders in the ARP-19B are compatible with the FRN-R Fuse.
The circuit is not degraded by the addition of the new fus'es.
It provides proper coordination between primary and secondary protection of the electrical penetrations in the event of circuit fault currents.
This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.
: Thus, no unreviewed safety question exists.
FSAR References.
Section 8.3.1 and 16.3 MEM/HO-9100150/17/Osl
Section 8.3.1 and 16.3 MEM/HO-9100150/17/Osl


Change to Plant as Described in the FSAR Title'PCR-005264,         New Fuel Dry Storage.
Change to Plant as Described in the FSAR Title'PCR-005264, New Fuel Dry Storage.
Functional   Summar This plant modification installs four 6 x 10 fuel racks in the new fuel inspection pit to allow storage of new fuel during and after receipt inspection. New fuel is already being stored in the new fuel inspection pit in its shipping containers during the receipt inspection process, on a temporary basis. This change will not subject the fuel to any new hazards,       it will just be staying in the fuel inspection pit longer.
Functional Summar This plant modification installs four 6
Safet   Function:
x 10 fuel racks in the new fuel inspection pit to allow storage of new fuel during and after receipt inspection.
Installation of the four       6 x 10 fuel racks in the fuel inspection pit was thoroughly   evaluated. The   pit slab was structurally evaluated and the seismic loading of the racks were considered.
New fuel is already being stored in the new fuel inspection pit in its shipping containers during the receipt inspection
The   current   SHNPP Facility Operating   License requires that fresh fuel be stored with     a minimum   of 12 inches edge-to-edge between adjacent assemblies (when fuel is outside its shipping container or approved storage rack location). The use of four racks with fuel in every-other-cell of every-other row (15 assemblies per rack) satisfies this licensing requirement.
: process, on a
The   license also requires that new fuel assemblies be stored in such a manner that water will drain freely from the assemblies                   in the event of flooding/draining of the fuel storage area. The rack cells each drain freely thru holes in the rack baseplate at each cell location. NUREG-0612 makes it clear that heavy load drop accidents are a concern only for "spent fuel, fuel in the core, or equipment that may be required to achieve safe shutdown or permit continued decay heat removal" (Section 1.1). Consequently, new fuel damage due to load drop accidents is not a safety concern.
temporary basis.
Placing four 6 x 10 racks in the new fuel inspection pit for new fuel dry storage (loading every-other-cell in every-other-row) with 15 new fuel assemblies per rack does not increase the probability or consequences             of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR. Thus, no unreviewed safety question exits.
This change will not subject the fuel to any new hazards, it will just be staying in the fuel inspection pit longer.
FSAR  
Safet Function:
Installation of the four 6
x 10 fuel racks in the fuel inspection pit was thoroughly evaluated.
The pit slab was structurally evaluated and the seismic loading of the racks were considered.
The current SHNPP Facility Operating License requires that fresh fuel be stored with a minimum of 12 inches edge-to-edge between adjacent assemblies (when fuel is outside its shipping container or approved storage rack location).
The use of four racks with fuel in every-other-cell of every-other row (15 assemblies per rack) satisfies this licensing requirement.
The license also requires that new fuel assemblies be stored in such a manner that water will drain freely from the assemblies in the event of flooding/draining of the fuel storage area.
The rack cells each drain freely thru holes in the rack baseplate at each cell location.
NUREG-0612 makes it clear that heavy load drop accidents are a concern only for "spent fuel, fuel in the core, or equipment that may be required to achieve safe shutdown or permit continued decay heat removal" (Section 1.1).
Consequently, new fuel damage due to load drop accidents is not a safety concern.
Placing four 6
x 10 racks in the new fuel inspection pit for new fuel dry storage (loading every-other-cell in every-other-row) with 15 new fuel assemblies per rack does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.
: Thus, no unreviewed safety question exits.
FSAR  


==Reference:==
==Reference:==
Section 9.1.1 and 9.1.4 MEM/HO-9100150/18/OS1
Section 9.1.1 and 9.1.4 MEM/HO-9100150/18/OS1


Change           to Plant as Described in the FSAR
Change to Plant as Described in the FSAR


==Title:==
==Title:==
PCR-005331,   installation of Corrosion         Coupon Racks.
PCR-005331, installation of Corrosion Coupon Racks.
Functional   Summar This   plant modification installs corrosion coupon racks on the Reactor Auxiliary Building Component Cooling Water (CCW) System, Waste Processing Building CCW System, and the Boron Thermal Regeneration (BTRS) Chilled Water System. The racks are required to monitor the effectiveness of the corrosion inhibitor added to these systems.'he corrosion coupon racks are installed on non nuclear safety portions of the CCW   System. Failure of the coupon racks will not deter the op'eration of the safety portion of the CCW System. Corrosion rack components are designed to meet or exceed the Reactor Auxiliary Building and Waste Processing Building CCW design pressures     and temperatures.
Functional Summar This plant modification installs
The coupon     rack is installed on the BTRS Chilled Water System which is a non-nuclear, safety system assumed to fail during an accident situation. This rack will not affect the operation of any safety system. All corrosion coupon rack components are designed to meet or exceed the chiller system design pressure and temperatures.
, corrosion coupon racks on the Reactor Auxiliary Building Component Cooling Water (CCW)
This change     does not increase the probability or consequences             of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.                     Thus, no unreviewed safety question exists FSAR
: System, Waste Processing Building CCW System, and the Boron Thermal Regeneration (BTRS) Chilled Water System.
The racks are required to monitor the effectiveness of the corrosion inhibitor added to these systems.'he corrosion coupon racks are installed on non nuclear safety portions of the CCW System.
Failure of the coupon racks will not deter the op'eration of the safety portion of the CCW System.
Corrosion rack components are designed to meet or exceed the Reactor Auxiliary Building and Waste Processing Building CCW design pressures and temperatures.
The coupon rack is installed on the BTRS Chilled Water System which is a non-nuclear, safety system assumed to fail during an accident situation.
This rack will not affect the operation of any safety system.
All corrosion coupon rack components are designed to meet or exceed the chiller system design pressure and temperatures.
This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.
: Thus, no unreviewed safety question exists FSAR  


==Reference:==
==Reference:==
Figures 9.2.2-1, 9.2.10-1, 9.3.4-4 NEN/HO-91001SO/19/OS1
Figures 9.2.2-1, 9.2.10-1, 9.3.4-4 NEN/HO-91001SO/19/OS1


Change to Procedure as Described in the FSAR Title.'PP-509,         Operation of the UFV-260, Underwater Filter/Vacuum Unit.
Change to Procedure as Described in the FSAR Title.'PP-509, Operation of the UFV-260, Underwater Filter/Vacuum Unit.
Functional   Summar The   purpose   of Plant Procedure HPP-509 is to address the control, setup, operation, and maintenance of the Tri-Nuclear Underwater Filter Vacuum Unit, Model UFV-260. The vacuum will primarily be used in the spent fuel pools at the Harris Plant to support receipt of spent fuel from CPEL's Robinson and Brunswick Nuclear Plants.
Functional Summar The purpose of Plant Procedure HPP-509 is to address operation, and maintenance of the Tri-Nuclear Underwater Model UFV-260.
Operation     of this vacuum is in no way related to any FSAR Chapter 15 initiating     event. Although the unit will be operating in the spent fuel pools, the only plant systems that the UVF-260 will interface with are the fuel handling crane systems.         The total vacuum package weighs approximately 600 lbs. (wet), which is well under the maximum capacity of the 3 cranes located in the fuel handling building.
The vacuum will primarily be used in the the Harris Plant to support receipt of spent fuel from Brunswick Nuclear Plants.
The Chapter     15   fuel handling accident,     as well as technical specifications assume that     there is 23 feet of water       above the fuel at all times. FSAR Section 9.1.3 states that siphoning of       the new and spent fuel pools via piping or hose connections to these pools is precluded             by the location of the penetrations,     limitations on hose length, and termination of piping penetrations flush with the liner.             This vacuum utilizes a 100'uction hose. This length of hose could be configured in such a way to allow siphoning. The procedure does not allow the hose to break the surface of the
the control,
~ater while the unit is in operation.           This administrative control (HPP-509) precludes any siphoning which could lower th'e water level in a spent fuel pool. In addition the procedure does not allow the unit to be operated in a pool containing irradiated fuel.
: setup, Filter Vacuum Unit, spent fuel pools at CPEL's Robinson and Operation of this vacuum is in no way related to any FSAR Chapter 15 initiating event.
The   change does not increase the probability or consequences           of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.             Thus, no unreviewed safety question exists.
Although the unit will be operating in the spent fuel
FSAR
: pools, the only plant systems that the UVF-260 will interface
. with are the fuel handling crane systems.
The total vacuum package weighs approximately 600 lbs.
(wet),
which is well under the maximum capacity of the 3
cranes located in the fuel handling building.
The Chapter 15 fuel handling
: accident, as well as technical specifications assume that there is 23 feet of water above the fuel at all times.
FSAR Section 9.1.3 states that siphoning of the new and spent fuel pools via piping or hose connections to these pools is precluded by the location of the penetrations, limitations on hose
: length, and termination of piping penetrations flush with the liner.
This vacuum utilizes a 100'uction hose.
This length of hose could be configured in such a
way to allow siphoning.
The procedure does not allow the hose to break the surface of the
~ater while the unit is in operation.
This administrative control (HPP-509) precludes any siphoning which could lower th'e water level in a
spent fuel pool.
In addition the procedure does not allow the unit to be operated in a pool containing irradiated fuel.
The change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.
: Thus, no unreviewed safety question exists.
FSAR  


==Reference:==
==Reference:==
Section 9.1.3 MEM/HO-9100150/20/OS1
Section 9.1.3 MEM/HO-9100150/20/OS1


'}}
'}}

Latest revision as of 06:52, 7 January 2025

Annual 10CFR50.59 Rept for 1990,including Summaries of Changes to Procedures &/Or Plant Mods Which Change Plant as Described in FSAR
ML18009A824
Person / Time
Site: Harris Duke Energy icon.png
Issue date: 12/31/1990
From: Richey R
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
HL-910015-(O), NUDOCS 9103060340
Download: ML18009A824 (30)


Text

I ACCELERATED DTRIBUTION DEMONS~TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9103060340 DOC.DATE: 90/12/31 NOTARIZED:

NO DOCKET FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina 05000400 AUTH.NAME AUTHOR AFP'ILIATION RICHEY,R.B.

Carolina Power

& Light Co.

'RECIP. NAME RECIPIENT AFFILIATION

~A7 w Document Control Branch (Document Control Desk) i/ R

SUBJECT:

Annual 10CFR50.59 rept for 1990,includinq summaries of, I

changes to procedures

&/or plant mods who.ch change plant. as described in FSAR.

D DISTR1BUTION CODE:

1E47D COPIES RECEIVED:LTR ENCLl SIZE:

TITLE: 50.59 Annual Report of Changes, Tests or xperiments Made W/out Approv NOTES:Application for permit renewal filed.

05000400 A

RECIPIENT ID CODE/NAME PD2-1 LA BECKER,D INTERNAL: ACRS AEOD/DSP/TPAB NRR/DOEA/OEAB11 RGN2 FILE 01 EXTERNAL: NRC PDR COPIES LTTR ENCL 1

0 1

0 6

6 1

1 1

1 1

1 1

1 RECIPIENT ID CODE/NAME PD2-1 PD AEOD/DOA

&QDM?

FB11 REG FIL 02 NSIC COPIES LTTR ENCL 5

5 1

1 1

1 1

1 1

1 D

D D

NOTE TO ALL"RIDS" RECIPIENTS:

D D

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

TOTAL NUMBER OF COPIES REQUIRED:

LTTR 21 ENCL 19

Carolina Power & Light Company P. O. Box t65 ~ New kill,N, C. 27562 R. B. RICHEY Vice President Harris NUclear Project FEB 2'7 1991 Letter Number:

HO-910015 (0) 10CFR50.59 U.S. Nuclear Regulatory Commission ATTN:

NRC Document Control Desk Washington, DC 20555 SHEARON HARRIS NUCLEAR POWER PLANT UNIT 1 DOCKET NO. 50-400 LICENSE NO. NPF-63 t

REPORT IN ACCORDANCE WITH 10CFR50.59 Gentlemen.'n accordance with 10CFR50.59, the following report is submitted for the year of 1990.

This report contains brief summaries of changes to procedures and/or plant modifications, which change the plant as it is described in the FSAR.

There were no tests or experiments conducted during this

interval, which are not described in the FSAR and require reporting in this report.

Very truly yours, jd Vice President Harris Nuclear Project MGW:gcm Enclosure cc.

Mr. S. D. Ebneter (NRC RII)

Mr. J.

E. Tedrow (NRC SHNPP)

MEM/HO-9100150/1/Osl 9103060340 901231 PDR ADOCK 05000400 R

PDR r(prj'1

Change to Plant as Described -in the FSAR Title.

PCR-000214, Addition of HVAC to Waste Processing Building (WPB)

Control Room Locker Area and Toilet Facility.

Functional Summar III This plant modification installed a bathroom and locker facility adjacent to the WPB Control Room.

FSAR Section 9.4.3 discusses the WPB Control Room HVAC

'System which will now supply air to the added bath/locker facility.

The WPB Control Room HVAC system is a non-safety system for safe shutdown of the plant.

The system provides Control Room and pressurization for radiation protection change does not affect the systems ability to perform its and is not required cooling to the WPB of operators.

This intended function.

This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.

Thus, no unreviewed safety question exls'ts

~

FSAR Reference'.

Section 9.4.3 and Figure 9,.4.3-4 MEM/HO-9100150/2/OS1

~

Change to Plant as Described in the FSAR Title.'PCR-001546, Use of Nukon Fiberglass Insulation Inside Containment Functional Summar This plant modification approved the replacement of the metal reflective insulation inside containment with Nukon Fiberglass Insulation (Owens-Corning Fiberglass Corp.)

on a

one-for-,one

basis, as deemed necessary to replace defective insulation.

In a letter dated December 8,

1978, the NRC staff accepted the use of Nukon insulation inside nuclear containments.

"Based on quantitative and qualitative tests performed by or for Owens-Corning Fiberglass, the staff concluded that the Owens-Corning Fiberglass Corporation's nuclear containment insulation.system (Nu'k'on) is capable of retarding heat loss from piping and equipment in containment

areas, and that the overall integrity of the bl'ankets will not be adversely affected by the conditions found during the lifetime of the pl,ant.

It was concluded that during a loss-of-coolant

accident, the Owens-Corning Fiberglass insulation system is not expected to interfere with the operation of the emergency r'ecirculation system."

The staff's acceptance was based on Topical Report OCF-1 (dated

December, 1978),

developed by Owens-

'Corning Fiberglass Corporation which adequately addressed the six concerns stated below.

1)

Release of airborne particles leading to a radiation health hazard in service,')

. Stress corrosion cracking of the austenitic stainless steel surfaces that comes in contact with the insulation',

E 3)

Deterioration of the thermal properties during normal plant operation, complicating operation and control of the plant; 4)

Presenting a fire hazard in the containment area that could interfere with safe operation of the plant; 5)

Interference with the emergency spray system in the event of a LOCA; 6)

Blocking of pressure relief ports in the event of an accident; Additional plant specific analysis was conducted to confirm that llukon insulation does not pose any additional threat to containment sump screen blockage at SHNPP.

This change does not increase the probability or consequences of'nalyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.

Thus, no unreviewed safety question exists a FSAR Reference-Section 6.2.2 MEM/H0-9100150/3/OS1

Change to Plant as Described in the FSAR

Title:

PCR-001887, Reconfiguration of the Fuel Handling Building (FHB) Fuel Pool A to Allow Increased Storage of BWR and PWR Fuel Assemblies.

Functional Summar This plant modification allows the reracking of the FHB Fuel Pool A to allow for storage of BWR and PWR fuel assemblies.

Pool A is being transformed from a

new fuel storage area for PWR fuel only into a

composite PWR and BWR irradiated fuel storage area.

This change also allows the contents of the

'Spent Fuel Pool B to be transferred into the A pool in order to perform liner repairs on the B pool.

Fuel Pool A is designed for the stor'age of new and'pent PWR fuel.

Since the llX11 BWR rack modules are interchangeable with 7X7 PWR rack modules it is acceptable to store spent BWR fuel in the A pool.

The A pool meets all of the design and performance requirements as the B pool and can be used as a spent fuel pool with no changes to its cooling or purification capability.

Rearrangement of the racks in the A pool has no effect on the maximum stored criticality since the individual racks are designed to maintain a subcritical array regardless of rack arrangement or boron concentration.

The maximum intended heat load from the proposed rack arrangement would be less than the heat load if all PWR fuel were stored in the A pool since the PWR fuel constitutes a greater heat load when compared with the BWR fuel.

This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.

Thus, no unreviewed safety question exists.

FSAR Reference.

Section 9.1 HEM/HO-9100150/4/OS1

Change to Plant as Described in the FSAR

Title:

PCR-001993, Primary Sample Panel '1A'entilation Modifications.

Functional Summar The Primary Sampling System (PSS) is designed to collect fluid and gaseous samples contained in the Reactor Coolant System and Safety Injection System.

It is also designed to collect fluid samples from the Boron Thermal Regeneration

System, Chemical and Volume Control
System, Steam Generator Blowdown System, residual heat removal heat exchangers, and a gas sample from the volume control tank and main steam.

The PSS provides samples in two sampling rooms in the Reactor Auxiliary Building, and brings them to a common location in the sampling rooms via 1A and 1B Primary Sample panels for analysis by the plant operating staff.

This plant modification increased the air flow rate exhausted from the Primary Sample Panel lA in order to assure proper capture velocity of contaminants generated during sampling.

The air flow rate exhausted was increased from 300 CFM to 1000 CFM with all hood doors open.

This increase in air flow was accomplished by reducing air flow quantity to be exhausted from the service water discharge pipe tunnel without adversely affecting the pipe tunnel design space temperature.

Ductwork internal to the primary sample panel 1A from the sample vessel enclosure to the common exhaust header was increased from three inch to seven inch diameter.

This modification affects two Q-Class E systems.

1)

The Reactor Auxiliary Building (RAB) Ventilation System (exhaust side)

and, 2) the Primary Sampling

, System (ventilation portion only).

Neither of the two systems are initiating or mitigating systems.

The subject air flow changes do not effect structural integrity of the seismic designed portion of ductwork of the RAB Normal Ventilation System as the operating pressure remains unchanged.

This change does not increase levels of airborne contamination (radioactivity) released via the RAB vent stack nor does it result in releases via unmonitored release points.

The revision does result in more positive capture of airborne contaminants generated during sampling which increases safety of operations personnel.

The reduction in the exhaust flowrate from the service water discharge pipe tunnel does not result in space temperature increases above current design.

This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment. malfunction than already evaluated in the FSAR.

Thus, no unreviewed safety question exls'ts

~

FSAR

Reference:

Figure 9.4.3-1 MEM/HO-9100150/5/OS1

Change to Plant as Described in the FSAR Title'.

PCR-002252, Snubber Reductions

.Functional Summar This plant modification abandons in place mechanical snubbers No. CS-H-963 and CS-H-968 from the Chemical and Volume Control System in the Reactor Auxiliary Building Elevation 261'-0.

The snubbers were abandoned as part of a snubber reduction effort to reduce maintenance cost and man-rem exposure during testing and repair work.

This modification does not impact the function or operation of the Chemical and Volume Control System.

The stress analysis and structural acceptability show that the abandonment of the snubbers is acceptable.

This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.

Therefore, no unreviewed safety questions exists.

FSAR

Reference:

Table 3.9.3-16 MEM/HO-9100150/6/OS1

Change to Plant as Described in the FSAR

Title:

PCR-002290, Waste Gas Analyzers Replacement Functional Summar

.'ach Hydrogen Recombiner Package of the Gaseous Waste Processing System (GWPS) includes a Gas Analyzer System.

This plant modification replaces the existing Bendix Hydrogen and Oxygen Analyzer with functionally equivalent Teledyne analyzers for both non-safety A

and B trains of the Catalytic Hydrogen Recombiner Package.

The analyzer changeout facilitated "installation of new flow control panels, rework of the existing tubing from the hydrogen recombiner skids to the gas analyzer racks and an increase in the compressor suction line size to minimize system backpressure.

Also, the new Teledyne analyzers cannot be damaged during no-flow conditions (system shut-down), therefore, deleting the need for low flow de-energization of the analyzers.

This plant modification incorporates changes to improve the GWPS performance and reliability.

The electrical portion of this system is fed from a non-ESF supply which is not required to operate during an emergency shutdown.

The instrumentation and control functions of the GWPS as described in FSAR Section 11.3.2.2.2 have not been affected by the Teledyne Analyzer changeout.

Control signal failure probability has been decreased due to the deletion of the low-flow analyzer

shutdown, which is not required for the Teledyne Analyzers.

Leaving the Teledyne Analyzers energized during system shutdown or no-flow conditions will have no adverse impact on the analyzers themselves nor system operation or availability.

The increase in the compressor suction line size has no adverse affect on the

'system or plant operation.

The line is designed and constructed in accordance with the original codes.

The two lines being moved are designed and constructed to the original codes.

The relocation will not adversely affect any system.

The redesigned lines are not routed over any safety related equipment.

No new crossties between equipment or systems are being made by this plant modification.

The GWPS performs no function related to the safe shutdown of the plant.

This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.

Thus, no unreviewed safety question

,exists.

PSAR

'Reference.'ection 11.3.2 and 9.5 HEM/H0-9100150/7/OSl

Change to Plant As Described in the FSAR

Title:

PCR-002297, Corrosion. Product Sampler Install'ation Functi'onal Summar This plant modification to the Secondary Sampling System installs iron and copper corrosion monitors on the following sample lines'.

a)

Condensate pump discharge b)

High pressure heater drains c)

Feedwater to the steam generators These monitors are installed to determine the volume of corrosion products entering the steam generators.

The monitors also provide an indication of the source of the majority of corrosion products.

The corrosion products monitors are designed to meet or exceed the secondary sample system design pressures and temperatures with one exception.

The feedwater to the steam generators sample point design pressure is 2000 psig while the corrosion monitor design pressure is 1500 psig.

A pressure relief valve set at 1500 psig maximum is installed per this modification on the corrosion monitor inlet sample line to prevent monitor overpressurization in the event the sample line pressure exceeds 1500 psig.

The secondary sample system is Quality Classification E which is assumed to fail during a seismic event and release any sample liquid to the equipment drains for processing.

Failure of the corrosion monitors will not increase the consequences of a

radioactive release over what is presently analyzed.

The corrosion monitors are designed using stainless steeL materials to minimize corrosion and erosion.

The table on which the corrosion monitors are mounted is designed to capture any leakage from the monitors and direct it to the equipment drain.

This change does not increase the probability or consequences af analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.

Thus, no unreviewed safety question exists'SAR

Reference:

Section 9.3.2.2.2 MEN/HO-9100150/8/OS1

e I'n t

III ~

v 1

Change to Plant as Described in the FSAR

Title:

PCR-003701, Removal of Flow Switches FS-7001A and FS-7001B from the Environmental Qualification Program.

Functional Summar This plant modification was issued to remove Flow Switches FS-7001A and FS-7001B from the Environmental Qualification (EQ)

Program.

FS-7001A and FS-7001B function as redundant,

,safety-grade instrumentation monitoring the component cooling water (CCW) flow via a common header (3CC6-201SN"1) from all three reactor coolant pumps.

If 'CCW flow decreases to the low flow setpoint, alarms are initiated at the monitor light boxes (MLB-4A and MLB-4B) and ERFIS messages for Points FRC-7001C and FRC-7001D are generated.

Low CCW flow to the RCP oil coolers requires Operator action to restore the CCW flow or to take other steps, as deemed appropriate by Operations.

The flow switches are located in the Reactor Auxiliary Building above Elevation 236'n Line 3CC6-201SN-1.

This location makes it difficult for plant technicians to perform EQ mandated calibrations.

As detailed

above, FS-7001A and FS-7001B monitor CCW flow from the reactor coolant pumps bearing oil coolers.

The flow switches are safety grade and during normal operation, the location of FS-7001A and FS-7001B is mild for both temperature and radiation.

Therefore, the only time the flow switches are subjected to a harsh environment is post design basis accident (DBA). If there is a

spurious loss of

CCW, not associated with a
DBA, FS-7001A and

~FS-7001B will function as

designed, and there will be no change in their operating environment.

In the event of a DBA the containment will be placed in Phase "A" isolation either by the initiation of Safety Injection or manually from the Main Control Board.

Phase "A" isolation does not isolate the CCW from the reactor coolant pumps (RCPs).

This allows these pumps to operate during safety injection and will also allow the operators sufficient time to shutdown the RCP's prior to Phase "B" isolation which does secure the component cooling water.

The RCP's however, are not safety related devices and as such cannot be considered to be available following a DBA.

In addition, there is no postulated accident in which the RCPs are utilized for accident mitigation.

Therefore, the basis for removing FS-7001A and FS-7001B from the EQ Program is, they will perform their safety function prior to an accident in a mild environment.

They are not required to operate after a Design Basis accident when a harsh environment is created.

This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than 'lready evaluated in the FSAR.

Thus, no unreviewed safety question exls'ts FSAR

REFERENCE:

Table 3.11.0-7 MEM/H0-9100150/9/OS1

Change to Plant as Described in the FSAR

Title:

PCR-003754, Chemical and Volume Control System (CVCS) Heat Exchanger Performance Thermometer Deletion.

Functional Summar This plant modification removed temperature indicators associated with the CVCS,due to ALARA concerns.

Temperature indicators TI-Ol-CS-7241, TI-01-CS-7243, and TI-Ol-CS-7244 are located in high radiation areas and present ALARA implications during ILRT and

,routine calibration activities.

These Dresser dial thermometers provide local indication of CVCS Regenerative and Excess Letdown Heat Exchanger performance; however, this temperature monitoring is not utilized for performance trending due to local exposure rates.

Temperature elements TE-01-CS-0123, TE-01-CS-

0139, and TE-01-CS-0140 provide Main'"control Room monitoring of Heat Exchanger outlet temperature making the subject indicators expendable.

The subject indicators have been removed and threaded pipe plugs installed in the existing thermowells with necessary sealant.

The affected thermometers are installed at the CVCS Regenerative and Excess Letdown Heat Exchangers, monitoring inlet/outlet temperature.

These

devices, providing performance related local indications, render no control functions and are not necessary for Plant Process Display or Post Accident Monitoring.

This modification, deleting unnecessary instrumentation, does not degrade plant safety considering its effect on accident-initiating systems; accident-mitigating systems, or key safety considerations.

This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.

Thus, no unreviewed safety question exists.

FSAR

Reference:

Figure 9.3.4-1 MEM/HO-9100150/10/Osl

Change to Plant as Described in the FSAR Title.'CR 004192, Replacement of Turbine Trip Condenser Vacuum Switches.

Functional Summar This plant modification was necessary due to the poor performance characteristics of the turbine trip condenser vacuum switches PS-4131AV thru DV and the fact that Westinghouse revised the vacuum trip setpoint.

New turbine vacuum pressure switches and circuitry have been installed.

Specifically, this modification replaces the existing United Electric pressure

.switches with Static 'O'ing (SOR) pressure switches which have proven more

reliable, adds a

separate pressure switch for pre-trip alarm and revised control circuitry such that a

setpoint change occurs at an increase of approximately 60%

power from the low setpoint (5.0 InHg) to the high setpoint (7.5 InHg).

Presently during the summer months reactor power reduction is required to prevent a turbine trip on low condenser vacuum.

This has been attributed in part to the reduction in cooling tower efficiency and miscellaneous water chemistry make up.

Per Westinghouse recommendation, at approximately 60%

power the condenser vacuum turbine trip setpoint should be increased from 5.0 InHg to 7.5 InHg to allow the unit to operate at full power production.

This has been achieved by installing a relay which will energize at approx.

60X power and switch the dual Hi-Lo SOR pressure switch from the low setpoint to the high setpoint.

New alarm pressure switch PS-4131EV will also be switched via the same relay to provide operators pre-trip warning at 4.0 InHg below 60X power and 6.5 InHg above 60% power.

The additional alarm relay will replace one of the DEH fluid low pressure trip switches.

This enhancement does not effect the original design intent of the low condenser vacuum trip circuit as discussed in FSAR 10.2.5 but allows for increased unit reliability and availability.

This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.

Thus, no,unreviewed safety question exists.

FSAR

Reference:

Figures 10.2.2-08, 10.2.2-10 MEM/HO-9100150/11/OS1

Change to Plant as Described in the FSAR Title.'CR-004506, Deactivation of the Chlorine Detection System.

Functional Summar This plant modification deactivated the chlorine detection system.

Technical Specification 3.3.3.7, Amendment 8,

stated that two independent chlorine detection trains be operable whenever liquid chlorine is present at the onsite chlorine storage area in quantities greater than 20 lbs.

SHNPP no longer stores chlorine in large quantities on site, therefore, this system is no longer required.

Amendment ten (10) of the SHNPP Technical Specifications deleted the Chlorine detection System from Technical Specifications.

The Chlorine Detection System consisted of two independent chlorine detector trains with each train consisting of a detector at each Control Room Area'entilation System intake (both normal and emergency) and a detector at the chlorine storage area.

The storage area detectors alarm and isolate the control room in the event of a

release.

of chlorine at the storage area.

CP&L does not store large quantities (i.e., quantities greater than 20 pounds) of liquid chlorine onsite at Harris.

Therefore, the accidental onsite release of such a small quantity of chlorine would not affect the plant operators.

As such, deletion of the storage area chlorine detectors will not increase the consequences of an accidental onsite release of chlorine.

The deactivation of the Chlorine Detection System will also avoid inadvertent control room isolations.

The chlorine detectors located at the Control Room Area Ventilation System intakes are intended to provide protection in the event of an accidental offsite release of chlorine.

A probabilistic risk assessment (PRA) was performed to determine the probability of an accidental chlorine release in the vicinity of Harris.

The results of the analysis showed that offsite chlorine release accidents have such a

low probability that they are not considered to be credible events.

This change does not increase the probability or consequences of analyzed

'ccidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.

Thus, no unreviewed safety question exists.

FSAR

Reference:

Sections 1.8, 2.2, 3 1, 6.4, 7.2, 7.3, 9.4, 9.5 MEM/HO-9100150/12/OS1

Title.

Change to Plant as Described in the FSAR PCR-004695, Removal of the Main Steam Power Operated Relief Valve (PORV) Actuators from the Environmental Qualification (EQ) Program.

Functional Summar The Main Steam

PORVs, located in the Main Steam Tunnel, utilize an Electro-Hydrologic actuator manufactured by Paul Monroe-Enertech.

This plant modification removed these actuators from the Harris Plants EQ Program.

The requirement for these actuators to be environmentally qualified was re-evaluated by this modification. It was determined that the subject actuators are not required to mitigate any FSAR Chapter 15 analyzed event that could result in an elevated temperature or pressure in the area of the steam tunnel.

Since these actuators are not required to mitigate a

Chapter 15 event that could cause an elevated temperature or pressure in the steam tunnel, it is unnecessary to maintain their EQ status.

This change does not increase the probability or consequences of analyzed accidents, no introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.

Thus, no unreviewed safety question exists.

FSAR Reference.

Table 3.11.0-2 MEM/HO-9100150/13/OS1

Change to Plant as Described in the FSAR

Title:

PCR-004930, Instrument Air Check Valve.

Functional Summar This plant modification installs a

3" 1508 carbon steel welded swing check valve i'n the Instrument Air (IA) System.

The check valve is installed in the main supply header into the Radiation Control Areas (RCA) (i.e.,

Reactor Auxiliary Building, Containment Building) to prevent any reverse flow. in the system flow path.

During routine plant shutdown surveillance

testing, improper work activities by test personnel caused radiological contamination of various piping sections of the IA system.

This situation created immediate concerns due to IA system flow path contamination inside the

RCA, along with potential problems regarding leakage paths outside the RCA via the IA supply header which crosses

. the RCA boundary.

The immediate problems were resolved by flushing the affected piping until samples showed contamination levels within acceptable levels inside the RCA boundary and by restricting use of the Emergency Breathing Air System.

The potential problem regarding IA system leakage paths outside the RCA boundary is being addressed by the instaLlation of the subject check valve.

The IA system, a part of the Compressed Air System originates in the Turbine Building and provides "instrument quality" air via piping to the Turbine Building, Reactor Auxiliary Building, and Containment Building.

The Compressed Air System (CAS) is not required for the initiation of any engineered safety feature

systems, safe shutdown
system, or any other safety-related system.

Therefore, the CAS is considered non-nuclear safety except for the containment penetrations and the valve accumulators.

A major piping or component failure in the Turbine Building could cause rapid depressurization of the IA flow path, thereby creating a

reverse flow to outside the RAB and RCA.

'This event could cause release of radioactive contamination to the environment.

The installation of the subject check valve provides means to prevent this type of occurrence.

During and after an accident there are no air-operated valves that require cycling to bring the plant to safe shutdown.

The accident analyses does not assume the instrument air system to be operable and does not take credit for the system.

This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.

Thus, no unreviewed safety question exists.

FSAR Reference.'igure 9.3.1-3 MEM/HO-9100150/14/OS1

V

'V V

yt

Change to Plant as Described in the FSAR

Title:

PCR-004984, Emergency Service Water (ESW)

System Minimum Flows/Plow Balancing Functional Summar Engineering Evaluation PCR-004984 established revised minimum service water flow requirements for various ESW loads and evaluated flow balances for acceptability based on the new',miftimum flows.

As previously

designed, no margin existed in the configuration of the ESW system to allow for degradation due to the highly conservative f'low requirements.

The new flow values were established for the worst-case condition with the ESW pumps aligned to the Main Reservoir with a

level of 205.7 feet mean sea level with a

water temperature of 95'F (Tech.

Spec. 3/4.7.5).

A summary of required FSAR Table 9.2.1-1 changes is as follows'.

~corn onent Component Cooling Water Heat Exchanger Old Value 12,000 gpm New Value 9,000 gpm Standby Diesel Generator Coolers 1,250 gpm 900 gpm Containment Fan Coolers 3,000 gpm 2,850 gpm Reactor Auxiliary Bldg.

HVAC Chillers 2,500 gpm 2,420 gpm The ESW system is an accident mitigating system.

The reduced flow rates still provide adequate margin for accident mitigation.

This change-does not increase the probability of consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.

No unreviewed safety question exists.

FSAR

Reference:

Table 9.2.1-1 MEM/HO-9100150/15/Osl

Change to Plant as Described in the FSAR

Title:

PCR-005021, Engineering Evaluation of Emergency Core Cooling System (ECCS)

Flow Inconsistencies.

Functional Summar In December of 1989, Westinghouse informed Carolina Power

& Light Company of inconsistencies found between the Harris plant ECCS flow rates assumed in the input to the Westinghouse supplied Loss-Of-Coolant Accident (LOCA) Analyses used to demonstrate compliance with the requirements of 10CFR50.46 and the flows allowed by the Harris Technical Specifications.

Specifically, the issue of concern was that the Harris Technical Specifications allowed for 31 gpm of reactor coolant pump (RCP) seal injection flow at normal charging pump conditions (at 2250 psia) versus an assumed 24 gpm (at 2250 psia) used in the gene@ation of ECCS flow data for the Harris Safety Analyses.

Since these flow values correspond to specific seal injection line resistance, it was seen that the seal injection line resistance, associated with the Technical Specifications, was actually less than that assumed in the calculations.

Therefore, additional charging/SI flow would be pumped through the seal injection line potentially resulting in a

reduction of flow injected into the core.

Since the potentially lower ECCS flow to the reactor core would ultimately impact the

FSAR, Chapter 15, Lost-of-Coolant Accident Analyses provided by Westinghouse,'n evaluation of the discrepancy was performed by Westinghouse.

The evaluation showed that the increase in peak cladding temperature (PCT),

due to the reduction in safety injection flow to the core was within the bounds of the PCT limits as defined in the Harris Technical Specifications.

Based on the foregoing evaluation, it is determined

that, pursuant to the criteria specified in 10CFR 50.59, the existence of the discrepancy between the seal injection line resistance allowed by the Technical Specifications and that assumed in the safety analysis does not involve an unreviewed safety question.

Because of the effects of steam/water condensation in the RCS

loops, the computer model has been shown to be sensitive to reductions in safety injection flow.

As a result FSAR Table 6.2.1-36 (Double Ended Pump Suction Guillotine Min.

SI Reflood Mass and Energy Releases) and Table 6.2.1-41 (Double Ended Pump Suction Guillotine Min.

SI Post-Reflood Mass and Energy Releases) are being revised to reflect new release data.

FSAR Reference.

Tables 6.2.1-36 and 6.2.1-41 MEM/HO-9100150/16/OS1

Change to Plant as Described in the FSAR

Title:

PCR-005157, Secondary Protection to ARP-19B Electrical Containment Penetration Circuits.

Functional Summar Electrical Containment Penetration

circuits, safety related and non-safety
related, are to be protected against overcurrent to prevent penetration conductor damage.

In all cases, the penetration circuit protection consist of a primary and back-up (secondary) disconnecting device which can each limit the maximum I t at the penetration to a value less than that required for thermal damage to the penetration conductor.

During a comparison, between Maintenance Surveillance Test MST-E0007 "120/208 VAC Molded Case Circuit Breaker Test" and electrical Calculation 30-PKR "Electrical Penetration Protection (Reg.

guide 1.63), it was determined that the existing 30 amp breaker did not provide sufficient protection against instantaneous short circuit current to prevent possible damage to the penetration.

This modification adds two dual element" time delay fuses, Bussman type FRN-R20 to the penetration circuits.

Existing fuse holders in ARP-19B (SB) were used and only wiring the internal jumpers was required to

'implement this modification.

New jumper cables will be added and some will be replaced as a

result of this modification.

The new fuses will provide sufficient conductor protection for the electrical penetrations.

The type of fuse selected is a

Buss type FRN-R which is already used for protection on other electrical penetrations.

The existing spare fuse holders in the ARP-19B are compatible with the FRN-R Fuse.

The circuit is not degraded by the addition of the new fus'es.

It provides proper coordination between primary and secondary protection of the electrical penetrations in the event of circuit fault currents.

This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.

Thus, no unreviewed safety question exists.

FSAR References.

Section 8.3.1 and 16.3 MEM/HO-9100150/17/Osl

Change to Plant as Described in the FSAR Title'PCR-005264, New Fuel Dry Storage.

Functional Summar This plant modification installs four 6

x 10 fuel racks in the new fuel inspection pit to allow storage of new fuel during and after receipt inspection.

New fuel is already being stored in the new fuel inspection pit in its shipping containers during the receipt inspection

process, on a

temporary basis.

This change will not subject the fuel to any new hazards, it will just be staying in the fuel inspection pit longer.

Safet Function:

Installation of the four 6

x 10 fuel racks in the fuel inspection pit was thoroughly evaluated.

The pit slab was structurally evaluated and the seismic loading of the racks were considered.

The current SHNPP Facility Operating License requires that fresh fuel be stored with a minimum of 12 inches edge-to-edge between adjacent assemblies (when fuel is outside its shipping container or approved storage rack location).

The use of four racks with fuel in every-other-cell of every-other row (15 assemblies per rack) satisfies this licensing requirement.

The license also requires that new fuel assemblies be stored in such a manner that water will drain freely from the assemblies in the event of flooding/draining of the fuel storage area.

The rack cells each drain freely thru holes in the rack baseplate at each cell location.

NUREG-0612 makes it clear that heavy load drop accidents are a concern only for "spent fuel, fuel in the core, or equipment that may be required to achieve safe shutdown or permit continued decay heat removal" (Section 1.1).

Consequently, new fuel damage due to load drop accidents is not a safety concern.

Placing four 6

x 10 racks in the new fuel inspection pit for new fuel dry storage (loading every-other-cell in every-other-row) with 15 new fuel assemblies per rack does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.

Thus, no unreviewed safety question exits.

FSAR

Reference:

Section 9.1.1 and 9.1.4 MEM/HO-9100150/18/OS1

Change to Plant as Described in the FSAR

Title:

PCR-005331, installation of Corrosion Coupon Racks.

Functional Summar This plant modification installs

, corrosion coupon racks on the Reactor Auxiliary Building Component Cooling Water (CCW)

System, Waste Processing Building CCW System, and the Boron Thermal Regeneration (BTRS) Chilled Water System.

The racks are required to monitor the effectiveness of the corrosion inhibitor added to these systems.'he corrosion coupon racks are installed on non nuclear safety portions of the CCW System.

Failure of the coupon racks will not deter the op'eration of the safety portion of the CCW System.

Corrosion rack components are designed to meet or exceed the Reactor Auxiliary Building and Waste Processing Building CCW design pressures and temperatures.

The coupon rack is installed on the BTRS Chilled Water System which is a non-nuclear, safety system assumed to fail during an accident situation.

This rack will not affect the operation of any safety system.

All corrosion coupon rack components are designed to meet or exceed the chiller system design pressure and temperatures.

This change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.

Thus, no unreviewed safety question exists FSAR

Reference:

Figures 9.2.2-1, 9.2.10-1, 9.3.4-4 NEN/HO-91001SO/19/OS1

Change to Procedure as Described in the FSAR Title.'PP-509, Operation of the UFV-260, Underwater Filter/Vacuum Unit.

Functional Summar The purpose of Plant Procedure HPP-509 is to address operation, and maintenance of the Tri-Nuclear Underwater Model UFV-260.

The vacuum will primarily be used in the the Harris Plant to support receipt of spent fuel from Brunswick Nuclear Plants.

the control,

setup, Filter Vacuum Unit, spent fuel pools at CPEL's Robinson and Operation of this vacuum is in no way related to any FSAR Chapter 15 initiating event.

Although the unit will be operating in the spent fuel

pools, the only plant systems that the UVF-260 will interface

. with are the fuel handling crane systems.

The total vacuum package weighs approximately 600 lbs.

(wet),

which is well under the maximum capacity of the 3

cranes located in the fuel handling building.

The Chapter 15 fuel handling

accident, as well as technical specifications assume that there is 23 feet of water above the fuel at all times.

FSAR Section 9.1.3 states that siphoning of the new and spent fuel pools via piping or hose connections to these pools is precluded by the location of the penetrations, limitations on hose

length, and termination of piping penetrations flush with the liner.

This vacuum utilizes a 100'uction hose.

This length of hose could be configured in such a

way to allow siphoning.

The procedure does not allow the hose to break the surface of the

~ater while the unit is in operation.

This administrative control (HPP-509) precludes any siphoning which could lower th'e water level in a

spent fuel pool.

In addition the procedure does not allow the unit to be operated in a pool containing irradiated fuel.

The change does not increase the probability or consequences of analyzed accidents, nor introduce a different type of accident or equipment malfunction than already evaluated in the FSAR.

Thus, no unreviewed safety question exists.

FSAR

Reference:

Section 9.1.3 MEM/HO-9100150/20/OS1

'