ENS 40198: Difference between revisions

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Created page by program invented by Mark Hawes
 
Created page by program invented by StriderTol
 
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| event date = 09/25/2003 EDT
| event date = 09/25/2003 EDT
| last update date = 11/10/2003
| last update date = 11/10/2003
| title = Initiation Of A Technical Specification Required Shutdown At Peach Bottom 2
| title = Initiation of a Technical Specification Required Shutdown at Peach Bottom 2
| event text = On 09/25/03 @ 2210, while restoring reactor vessel instrumentation to service on Unit 3, an invalid ECCS actuation, (reactor vessel lo-lo-lo) occurred which caused all four (4) EDG to automatically start. All eight (8) 4 KV buses remained supplied from offsite sources. The Unit 3 ECCS pump auto starts were previously defeated per plant procedure and were not required to be operable per Tech Specs. The invalid ECCS initiation signal caused the offsite power Loss-of-Power instrumentation setpoints to transfer to the degraded voltage LOCA setpoints. With the degraded voltage LOCA setpoints initiated, the 4 KV E-bus fast transfer capability on a degraded voltage-NON-LOCA condition is defeated. With the inability to fast transfer the 4 KV E-buses on a degraded voltage NON-LOCA condition, both offsite sources are inoperable. Prior to restoring the reactor vessel level instrumentation, the E-2 diesel generator was inoperable. With both offsite source.; and one EDG inoperable, LCO 3.8.1 Required Action H.1 requires an entry into LCO 3.0.3 for Unit 2.  
| event text = On 09/25/03 @ 2210, while restoring reactor vessel instrumentation to service on Unit 3, an invalid ECCS actuation, (reactor vessel lo-lo-lo) occurred which caused all four (4) EDG to automatically start. All eight (8) 4 KV buses remained supplied from offsite sources. The Unit 3 ECCS pump auto starts were previously defeated per plant procedure and were not required to be operable per Tech Specs. The invalid ECCS initiation signal caused the offsite power Loss-of-Power instrumentation setpoints to transfer to the degraded voltage LOCA setpoints. With the degraded voltage LOCA setpoints initiated, the 4 KV E-bus fast transfer capability on a degraded voltage-NON-LOCA condition is defeated. With the inability to fast transfer the 4 KV E-buses on a degraded voltage NON-LOCA condition, both offsite sources are inoperable. Prior to restoring the reactor vessel level instrumentation, the E-2 diesel generator was inoperable. With both offsite source.; and one EDG inoperable, LCO 3.8.1 Required Action H.1 requires an entry into LCO 3.0.3 for Unit 2.  
With Unit 3 in MODE 5, LCO 3.0.3 is not applicable.
With Unit 3 in MODE 5, LCO 3.0.3 is not applicable.

Latest revision as of 21:24, 1 March 2018

ENS 40198 +/-
Where
Peach Bottom 
Pennsylvania (NRC Region 1)
Reporting
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown

10 CFR 50.72(b)(3)(iv)(A), System Actuation

10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation
Time - Person (Reporting Time:+21.42 h0.893 days <br />0.127 weeks <br />0.0293 months <br />)
Opened: Todd Strayer
01:25 Sep 26, 2003
NRC Officer: Rich Laura
Last Updated: Nov 10, 2003
40198 - NRC Website
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