ENS 56280
ENS Event | |
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04:33 Nov 12, 2022 | |
Title | 60-DAY Telephonic Notification |
Event Description | The following information was provided by the licensee via email:
This 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(1) and 50.73(a)(2)(iv)(A) for an invalid actuation of a primary containment isolation signal affecting more than one system. On November 11, 2022, at 2333 hours0.027 days <br />0.648 hours <br />0.00386 weeks <br />8.877065e-4 months <br /> EST, Peach Bottom experienced an unplanned loss of the #343 Off-Site Startup Source. Due to the temporary loss of power during automatic bus transfers, several systems experienced Primary Containment Isolation System (PCIS) Group II and Group III (GP II/III) isolation signals. Plant Systems impacted by isolation valve closure included: Reactor Water Clean Up (RWCU), Containment Atmospheric Control (CAC), Traversing In-Core Probe (TIP) Purge, Primary Containment Floor and Equipment Drains, and the Instrument Nitrogen system. All equipment responded as designed. Plant conditions which initiate PCIS GP II isolation signals are Reactor Vessel Low Water Level, High Drywell Pressure, RWCU system High Flow or RWCU Non-Regenerative Heat Exchanger High Outlet Temperature. The PCIS GP III actuations are initiated by the Reactor Vessel Low Water Level, Primary Containment High Pressure, Reactor Building Ventilation High Radiation or Refuel Floor Ventilation High Radiation. At the time of the event, none of these actual plant conditions existed; therefore, the actuation of the PCIS was invalid. The loss of the #343 Off-Site Startup Source was caused by a failed printed circuit card in the programable logic controller (PLC) for the 3435 breaker. There is no time-based maintenance strategy for PLC replacement. The PLC circuit card was replaced, and the breaker restored to full qualification and service. Preventive maintenance strategy will be enhanced to address the identified vulnerability. The licensee has notified the NRC Resident Inspector. |
Where | |
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Peach Bottom Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+896.28 h37.345 days <br />5.335 weeks <br />1.228 months <br />) | |
Opened: | Tim Grimme 12:50 Dec 19, 2022 |
NRC Officer: | Brian Lin |
Last Updated: | Dec 19, 2022 |
56280 - NRC Website
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Unit 3 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 562802022-11-12T04:33:00012 November 2022 04:33:00
[Table view]10 CFR 50.73(a)(1), Submit an LER 60-DAY Telephonic Notification ENS 548202020-06-08T08:24:0008 June 2020 08:24:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation ENS 529612017-07-14T18:53:00014 July 2017 18:53:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Valves ENS 519622016-03-28T17:20:00028 March 2016 17:20:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation ENS 500892014-03-09T21:13:0009 March 2014 21:13:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification for an Invalid Actuation of an Emergency Service Water System ENS 479072012-03-13T20:04:00013 March 2012 20:04:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Report - Invalid Primary Containment Isolation System Actuation ENS 449402009-03-02T15:55:0002 March 2009 15:55:00 10 CFR 50.73(a)(1), Submit an LER Invalid Primary Containment Isolation Signal Due to Maintenance Error ENS 444652008-07-24T03:25:00024 July 2008 03:25:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuation Due to Loss of One Offsite Power Circuit to Safety Buses ENS 439102007-12-11T21:45:00011 December 2007 21:45:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Notification of an Invalid Actuation of Units 2 and 3 Primary Containment Isolation Systems ENS 411932004-09-28T06:00:00028 September 2004 06:00:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation Due to Bus Voltage Dip During Recirc Mg Start ENS 411922004-09-18T08:57:00018 September 2004 08:57:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation Due to Off Site Power Source Fast Transfer ENS 408192004-04-25T05:05:00025 April 2004 05:05:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuation ENS 401982003-09-25T04:00:00025 September 2003 04:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.73(a)(1), Submit an LER Initiation of a Technical Specification Required Shutdown at Peach Bottom 2 ENS 401042003-07-27T22:39:00027 July 2003 22:39:00 10 CFR 50.73(a)(1), Submit an LER 60 Day Optional Report 2022-11-12T04:33:00 | |