ENS 41832
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ENS Event | |
|---|---|
07:18 Jul 10, 2005 | |
| Title | Turbine Trip Resulting in Rps Actuation and Automatic Reactor Scram |
| Event Description | This non-emergency 4-hour and 8-hour report is pursuant to 10CFR50.72(b)(2) and 10CFR50.72(b)(3). On 7/10/05 at 0318 hours0.00368 days <br />0.0883 hours <br />5.257936e-4 weeks <br />1.20999e-4 months <br />, Unit 2 experienced a turbine trip and subsequent reactor scram. An RPS actuation occurred, as expected, following the turbine trip. RPS responded normally and reactor power is 0%. Reactor water level went below 1 inch, as expected, following a reactor scram from 100% power. At a reactor level of less than 1 inch, PCIS Group 2 and 3 isolations occurred. Reactor water level has been restored above 1 inch to the normal level using the normal reactor feedwater system. All safety systems responded as designed.
An investigation is in progress to determine the cause of the turbine trip and to initiate appropriate corrective actions. During the scram the RCS experienced a high pressure condition which caused both recirculation pumps to trip and 3 SRVs to lift and reseat. The licensee is presently depressurizing primary system in order to restart one of the recirculation pumps. Current RCS parameters: Pressure - 320 psig; Temperature - 428 F; and Level - +23 inches. All rods fully inserted. Prior to the turbine trip the licensee was conducting a routine weekly "Mechanical Trip Valve Test. The licensee notified the NRC Resident Inspector. |
| Where | |
|---|---|
| Peach Bottom Pennsylvania (NRC Region 1) | |
| Reporting | |
| 10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
| Time - Person (Reporting Time:+-0.6 h-0.025 days <br />-0.00357 weeks <br />-8.2188e-4 months <br />) | |
| Opened: | Alan Raush 06:42 Jul 10, 2005 |
| NRC Officer: | John Knoke |
| Last Updated: | Jul 10, 2005 |
| 41832 - NRC Website
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Unit 2 | |
|---|---|
| Reactor critical | Critical |
| Scram | A/R |
| Before | Power Operation (100 %) |
| After | Hot Shutdown (0 %) |
Peach Bottom | |
WEEKMONTHYEARENS 572212024-07-10T11:28:00010 July 2024 11:28:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram Due to Manual Turbine Trip ENS 569362024-01-29T17:02:00029 January 2024 17:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram ENS 558992022-05-16T19:52:00016 May 2022 19:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Scram Due to Electrical Transients ENS 555752021-11-14T10:25:00014 November 2021 10:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Trip Due to Lowering Main Condenser Vacuum ENS 536302018-09-30T04:00:00030 September 2018 04:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Automatic Scram Due to a Loss of Two Condensate Pumps ENS 472862011-09-21T14:20:00021 September 2011 14:20:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Relay Malfunction Resulted in a Valid Undervoltage Signal ENS 453482009-09-14T02:44:00014 September 2009 02:44:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram Due to Short Period During Plant Shutdown ENS 428892006-10-07T21:50:0007 October 2006 21:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded, 10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material Technical Specification Required Shutdown Due to Loss of Primary Containment Integrity ENS 418322005-07-10T07:18:00010 July 2005 07:18:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Turbine Trip Resulting in Rps Actuation and Automatic Reactor Scram ENS 412772004-12-22T09:55:00022 December 2004 09:55:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Reactor Scram and Eccs Injection Following Opening of Turbine Bypass Valves ENS 405372004-02-22T20:10:00022 February 2004 20:10:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Scram at Peach Bottom 2 Due to Decreasing Condenser Vacuum ENS 401982003-09-25T04:00:00025 September 2003 04:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.73(a)(1), Submit an LER Initiation of a Technical Specification Required Shutdown at Peach Bottom 2 2024-07-10T11:28:00 | |
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