ENS 40819
ENS Event | |
---|---|
05:05 Apr 25, 2004 | |
Title | Invalid System Actuation |
Event Description | This 60-day optional report, as allowed by 10 CFR 50.73(a)(1), is being made under the reporting requirement in 10CFR50.73(a)(2)(iv)(A) to describe an unplanned, invalid actuation of specified systems, specifically the Units 2 and 3 Primary Containment Isolation Systems (PCIS).
On 4/25/04, at approximately 0105 hours0.00122 days <br />0.0292 hours <br />1.736111e-4 weeks <br />3.99525e-5 months <br />, the 343SU startup source tripped resulting in a fast transfer of expected 4 kV emergency busses to the alternate offsite power source. The fast transfer resulted in a half PCIS Group II isolation on both Units 2 and 3 as expected. The half isolation of PCIS Group II resulted in outboard isolation valves closing on Unit 2 and inboard isolation valves closing on Unit 3. The isolations involved various PCIS Group II process lines such as Reactor Water Cleanup (RWCU), Containment Atmospheric Control (CAC) / Containment Atmospheric Dilution (CAD) and Containment Instrument Nitrogen. The Units 2 and 3 PCIS isolations were reset by approximately 0130 hours0.0015 days <br />0.0361 hours <br />2.149471e-4 weeks <br />4.9465e-5 months <br /> in accordance with procedures. All required isolation valves operated as designed. The offsite source (343SU) was lost as a result of a ground fault. Subsequent investigation determined that a raccoon had climbed a takeoff tower where the startup source transitions from an aerial line to underground cabling. The associated equipment was located in a small fenced area near the plant. The offsite source was inspected, tested and returned to an operable condition by approximately 2220 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.4471e-4 months <br /> on 4/25/04. This issue has been entered into the site Corrective Action Program (CR 216811) for evaluation and implementation of further corrective actions. The licensee notified the NRC Resident Inspector. |
Where | |
---|---|
Peach Bottom Pennsylvania (NRC Region 1) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+1228.15 h51.173 days <br />7.31 weeks <br />1.682 months <br />) | |
Opened: | Dave Foss 09:14 Jun 15, 2004 |
NRC Officer: | Bill Gott |
Last Updated: | Jun 15, 2004 |
40819 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 40819\u003C/a\u003E - \u003Ca href=\"/Peach_Bottom\" title=\"Peach Bottom\"\u003EPeach Bottom\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003EInvalid System Actuation\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 40819 - Peach Bottom\n","link":"","lat":39.75920833333333,"lon":-76.26879444444444,"icon":"/w/images/b/be/Constellation_icon.png"}],"imageoverlays":null} | |
Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
Unit 3 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 562802022-11-12T04:33:00012 November 2022 04:33:00
[Table view]10 CFR 50.73(a)(1), Submit an LER 60-DAY Telephonic Notification ENS 548202020-06-08T08:24:0008 June 2020 08:24:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation ENS 529612017-07-14T18:53:00014 July 2017 18:53:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Valves ENS 519622016-03-28T17:20:00028 March 2016 17:20:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation ENS 500892014-03-09T21:13:0009 March 2014 21:13:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification for an Invalid Actuation of an Emergency Service Water System ENS 479072012-03-13T20:04:00013 March 2012 20:04:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Report - Invalid Primary Containment Isolation System Actuation ENS 449402009-03-02T15:55:0002 March 2009 15:55:00 10 CFR 50.73(a)(1), Submit an LER Invalid Primary Containment Isolation Signal Due to Maintenance Error ENS 444652008-07-24T03:25:00024 July 2008 03:25:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuation Due to Loss of One Offsite Power Circuit to Safety Buses ENS 439102007-12-11T21:45:00011 December 2007 21:45:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Notification of an Invalid Actuation of Units 2 and 3 Primary Containment Isolation Systems ENS 411932004-09-28T06:00:00028 September 2004 06:00:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation Due to Bus Voltage Dip During Recirc Mg Start ENS 411922004-09-18T08:57:00018 September 2004 08:57:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specified System Actuation Due to Off Site Power Source Fast Transfer ENS 408192004-04-25T05:05:00025 April 2004 05:05:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuation ENS 401982003-09-25T04:00:00025 September 2003 04:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.73(a)(1), Submit an LER Initiation of a Technical Specification Required Shutdown at Peach Bottom 2 ENS 401042003-07-27T22:39:00027 July 2003 22:39:00 10 CFR 50.73(a)(1), Submit an LER 60 Day Optional Report 2022-11-12T04:33:00 | |