ENS 40403: Difference between revisions

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| event date = 12/20/2003 09:49 EST
| event date = 12/20/2003 09:49 EST
| last update date = 01/08/2004
| last update date = 01/08/2004
| title = Rps Actuation Due To Loss Of Turbine Generator Excitation
| title = Rps Actuation Due to Loss of Turbine Generator Excitation
| event text = On December 20, 2003, at 0949 hours, an automatic reactor trip occurred due to a loss of excitation of the turbine generator.  All plant safety functions were maintained throughout the event.  The plant was stabilized in Mode 3.  All plant safety systems responded normally with the exception of the 2C Auxiliary Feedwater Pump (steam driven) which tripped on mechanical overspeed.  The 2A and 2B Auxiliary Feedwater Pumps (electric driven) functioned normally to restore the 2A and 2B Steam Generator levels.  Post trip system anomalies include RCS Letdown isolated, Steam Generator Blowdown isolation valves closed, Control Room ventilation system swapped to recirculation mode, and the Fuel Handling Building ventilation system swapped to the Shield Building.  An Emergency Response Team has been formed to review these conditions prior to plant restart.  This non-emergency notification is being made pursuant to 10 CFR 50.72(b)(2)(iv)(B) due to the automatic RPS Reactor Trip.
| event text = On December 20, 2003, at 0949 hours, an automatic reactor trip occurred due to a loss of excitation of the turbine generator.  All plant safety functions were maintained throughout the event.  The plant was stabilized in Mode 3.  All plant safety systems responded normally with the exception of the 2C Auxiliary Feedwater Pump (steam driven) which tripped on mechanical overspeed.  The 2A and 2B Auxiliary Feedwater Pumps (electric driven) functioned normally to restore the 2A and 2B Steam Generator levels.  Post trip system anomalies include RCS Letdown isolated, Steam Generator Blowdown isolation valves closed, Control Room ventilation system swapped to recirculation mode, and the Fuel Handling Building ventilation system swapped to the Shield Building.  An Emergency Response Team has been formed to review these conditions prior to plant restart.  This non-emergency notification is being made pursuant to 10 CFR 50.72(b)(2)(iv)(B) due to the automatic RPS Reactor Trip.
All controls inserted properly.  Decay heat is being removed using the turbine bypass valves.   
All controls inserted properly.  Decay heat is being removed using the turbine bypass valves.   

Latest revision as of 22:24, 1 March 2018

ENS 40403 +/-
Where
Saint Lucie NextEra Energy icon.png
Florida (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-1.82 h-0.0758 days <br />-0.0108 weeks <br />-0.00249 months <br />)
Opened: Calvin Ward
13:00 Dec 20, 2003
NRC Officer: Bill Gott
Last Updated: Jan 8, 2004
40403 - NRC Website
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