ENS 43874
From kanterella
Jump to navigation
Jump to search
ENS Event | |
---|---|
06:31 Dec 29, 2007 | |
Title | Manual Reactor Trip When Five Control Rods Unexpectedly Dropped 20 Inches |
Event Description | At 2320, on 12/28/07, a Reactor Startup was commenced. At 0025, on 12/29/07 Subgroup #15, of Regulating Group #3, was placed on the hold bus. Placing the Subgroup on the hold bus was a pre-planned action that was briefed prior to the reactor startup, in accordance with an approved interim engineering disposition. The interim engineering disposition was written and approved on 12/28/07 for concerns over CEA #1, of Subgroup #15, dropping into the core unexpectedly. Subgroup #15, of Regulating Group #3, contains five CEA's [CEA # 60, 62, 64, 66 and 1]. At 0047, all Regulating Group CEA's, with the exception of Regulating Group #5, were placed at the Upper Electrical Limit [136 inches withdrawn]. Regulating Group #5 was at 120 inches withdrawn in preparation for diluting to criticality. At 0107, the dilution to criticality was commenced. At 0131, all 5 CEA's in Subgroup #15 slipped into the core approximately 20 inches. A manual reactor trip was then ordered by the unit supervisor. 2-EOP-1, 'Standard Post Trip Actions' was then performed. The unit was borated to shutdown boron concentration. All Safety Functions were met satisfactorily and 2-EOP-1 was exited. The unit was in Mode 3 approaching Mode 2 at the time of the trip. The unit is currently stable in Mode 3, Hot Standby.
Reactor coolant pump heat is being removed using the atmospheric steam dumps. The licensee notified the NRC Resident Inspector. |
Where | |
---|---|
Saint Lucie Florida (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+1.38 h0.0575 days <br />0.00821 weeks <br />0.00189 months <br />) | |
Opened: | Calvin Ward 07:54 Dec 29, 2007 |
NRC Officer: | Mark Abramovitz |
Last Updated: | Dec 29, 2007 |
43874 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 43874\u003C/a\u003E - \u003Ca href=\"/Saint_Lucie\" title=\"Saint Lucie\"\u003ESaint Lucie\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003EManual Reactor Trip When Five Control Rods Unexpectedly Dropped 20 Inches\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 43874 - Saint Lucie\n","link":"","lat":27.348672222222223,"lon":-80.24639722222223,"icon":"/w/images/9/9b/NextEra_Energy_icon.png"}],"imageoverlays":null} | |
Unit 2 | |
---|---|
Reactor critical | Not Critical |
Scram | No |
Before | Hot Standby (0 %) |
After | Hot Standby (0 %) |
WEEKMONTHYEARENS 572492024-07-28T22:37:00028 July 2024 22:37:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 560872022-09-03T02:48:0003 September 2022 02:48:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Feed Pump ENS 550782021-01-20T23:22:00020 January 2021 23:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Trip of Motor Control Center ENS 530362017-10-26T06:12:00026 October 2017 06:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Following a Loss of Load ENS 527572017-05-15T22:00:00015 May 2017 22:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Emergency Diesel Generator Signal Generated Upon Loss of 4160V Power ENS 521912016-08-21T23:37:00021 August 2016 23:37:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event - Loss of Offsite Power ENS 514232015-09-17T16:22:00017 September 2015 16:22:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Actuation of Uv Relays Following Loss of Unit 2 Startup Transformer ENS 513022015-08-10T02:15:00010 August 2015 02:15:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip During Testing ENS 506072014-11-12T20:48:00012 November 2014 20:48:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Lowering Steam Generator Water Level ENS 495362013-11-14T17:18:00014 November 2013 17:18:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Low Level in the 2B Steam Generator ENS 483882012-10-08T01:40:0008 October 2012 01:40:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Essential Bus Deenergized While Defueled ENS 483692012-10-03T12:43:0003 October 2012 12:43:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Failure of Startup Transformer Caused Undervoltage Condition on Essential Bus ENS 479152012-05-11T07:55:00011 May 2012 07:55:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Feedwater Control Valve Failure ENS 476572012-02-10T06:34:00010 February 2012 06:34:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Maintenance Activities Cause an Inadvertent Emergency Diesel Generator Start ENS 469282011-06-06T07:29:0006 June 2011 07:29:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Error During Reactor Protection System Surveillance Leads to Reactor Trip ENS 458432010-04-15T19:39:00015 April 2010 19:39:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Manual Reactor Trip ENS 453742009-09-21T17:34:00021 September 2009 17:34:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Manual Reactor Trip During Reactor Startup ENS 449522009-04-01T22:05:0001 April 2009 22:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Manual Reactor Trip ENS 442762008-06-07T12:18:0007 June 2008 12:18:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Following the Trip of a Condensate Pump ENS 438742007-12-29T06:31:00029 December 2007 06:31:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip When Five Control Rods Unexpectedly Dropped 20 Inches ENS 419112005-08-11T14:48:00011 August 2005 14:48:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip on a Condensate Pump Bus Lockout ENS 417152005-05-19T00:59:00019 May 2005 00:59:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Inadvertent De-Energization of 4160 V Safety Related A.C. Bus with Edg Auto Start ENS 412932004-12-25T11:52:00025 December 2004 11:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Manually Tripped to Remove Failing Condensate Pump from Service ENS 410722004-09-26T03:56:00026 September 2004 03:56:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to a Loss of Offsite Power ENS 404032003-12-20T14:49:00020 December 2003 14:49:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Rps Actuation Due to Loss of Turbine Generator Excitation 2024-07-28T22:37:00 | |
Retrieved from "https://kanterella.com/w/index.php?title=ENS_43874&oldid=90451"