ENS 40787: Difference between revisions

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| event date = 06/02/2004 12:30 EDT
| event date = 06/02/2004 12:30 EDT
| last update date = 06/02/2004
| last update date = 06/02/2004
| title = Plant Shutdown Was Initiated To Comply With Tech Spec. 3.6.1.1. Primary Containment Integrity.
| title = Plant Shutdown Was Initiated to Comply with Tech Spec. 3.6.1.1. Primary Containment Integrity.
| event text = At 1230 hours the service water isolation valve to the Turbine Building Area (1SW26) was declared inoperable due to the inability to close the valve.  This condition was identified while investigating a low service water pressure in the turbine building during start up activities from the Salem 1 sixteenth refueling outage.
| event text = At 1230 hours the service water isolation valve to the Turbine Building Area (1SW26) was declared inoperable due to the inability to close the valve.  This condition was identified while investigating a low service water pressure in the turbine building during start up activities from the Salem 1 sixteenth refueling outage.
With 1SW26 inoperable, Technical Specification 3.6.1.1 requires that the inoperable valve be restored to operable within one hour or be in hot standby within the next 6 hours and in cold shutdown in the next 30 hours.  Since the valve cannot be restored to operable within  the one hour action statement time, PSEG commenced a unit shutdown at 1330 hours.  
With 1SW26 inoperable, Technical Specification 3.6.1.1 requires that the inoperable valve be restored to operable within one hour or be in hot standby within the next 6 hours and in cold shutdown in the next 30 hours.  Since the valve cannot be restored to operable within  the one hour action statement time, PSEG commenced a unit shutdown at 1330 hours.  

Latest revision as of 22:23, 1 March 2018

ENS 40787 +/-
Where
Salem PSEG icon.png
New Jersey (NRC Region 1)
Reporting
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Time - Person (Reporting Time:+-1.33 h-0.0554 days <br />-0.00792 weeks <br />-0.00182 months <br />)
Opened: Marty Malony
15:10 Jun 2, 2004
NRC Officer: John Mackinnon
Last Updated: Jun 2, 2004
40787 - NRC Website
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