05000364/LER-1999-001, Forwards LER 99-001-00 Re Reactor Trip Due to Loss of Condenser Vacuum Steam Dump Drain Line Failure.Commitments Made by Licensee,Listed: Difference between revisions
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| Title = Forwards LER 99-001-00 Re Reactor Trip Due to Loss of Condenser Vacuum Steam Dump Drain Line Failure.Commitments Made by Licensee,Listed | | Title = Forwards LER 99-001-00 Re Reactor Trip Due to Loss of Condenser Vacuum Steam Dump Drain Line Failure.Commitments Made by Licensee,Listed | ||
| Plant = | | Plant = | ||
| Reporting criterion = | | Reporting criterion = 10 CFR 50.73(a)(2)(iv) | ||
| Power level = | | Power level = | ||
| Mode = | | Mode = | ||
| Docket = 05000364 | | Docket = 05000364 | ||
| LER year = | | LER year = 1999 | ||
| LER number = 1 | | LER number = 1 | ||
| LER revision = | | LER revision = 0 | ||
| Event date = | | Event date = | ||
| Report date = | | Report date = | ||
| Line 33: | Line 33: | ||
=text= | =text= | ||
{{#Wiki_filter:f. | {{#Wiki_filter:f. | ||
r | r Dave Morey, | ||
Dave Morey , | Southera Nuclear i.. | ||
t t | t t | ||
_ Vice President Operating Compary. Inci farley Project Post Office Box 1295 - | |||
Birmingham, Alabama 35201 Tel 205 932.5131! | Birmingham, Alabama 35201 Tel 205 932.5131! | ||
SOUTHERN July 2,1999 | |||
. COMPANY Energy to Serve hur World" Docket No.: | |||
50-364 NEL-99-0258 U. S. Nuclear Regulatory Commission ATrN: Document Control Desk - | |||
Washington, D, C, 20555-0001 Joseph M. Farley Nuclear Plant - Unit 2 Licensee Event Report 99-001-00 Reactor Trip Due to Loss of Condenser Vacuum On Steam Dumo Drain Line Failure Ladies and Gentlemen: | Washington, D, C, 20555-0001 Joseph M. Farley Nuclear Plant - Unit 2 Licensee Event Report 99-001-00 Reactor Trip Due to Loss of Condenser Vacuum On Steam Dumo Drain Line Failure Ladies and Gentlemen: | ||
Joseph M. Farley Nuclear Plant - Unit 2 Licensee Event Report No. 99-001-00 is being submitted in accordance with 10 CFR 50.73(a)(2)(iv). | Joseph M. Farley Nuclear Plant - Unit 2 Licensee Event Report No. 99-001-00 is being submitted in accordance with 10 CFR 50.73(a)(2)(iv). | ||
The following four NRC commitments are included in the Corrective Action section of this LER; no other NRC commitments are contained in this letter. | The following four NRC commitments are included in the Corrective Action section of this LER; no other NRC commitments are contained in this letter. | ||
: 1. An every two weeks preventive maintenance task has 'been implemented to perform visual and acousticci observations of steam dump drain lines until the next Unit 2 refueling outage. | : 1. An every two weeks preventive maintenance task has 'been implemented to perform visual and acousticci observations of steam dump drain lines until the next Unit 2 refueling outage. | ||
: 2. , A design change to further reduce the stress on the steam dump drain lines will be | : 2., A design change to further reduce the stress on the steam dump drain lines will be J | ||
: 3. Additional inspections will be performed on the Unit I steam dump drain lines, and the existing Unit I stress analysis will be reviewed. Ifnecessary, appropriate changes | implemented during the next Unit 2 refueling outage. | ||
will be implemented before the end of the next Unit I refueling outage. | I | ||
: 3. Additional inspections will be performed on the Unit I steam dump drain lines, and the existing Unit I stress analysis will be reviewed. Ifnecessary, appropriate changes | |||
) | |||
will be implemented before the end of the next Unit I refueling outage. | |||
1 | |||
: 4. Appropriate design individuals will be trained on this event by August 31,1999. | : 4. Appropriate design individuals will be trained on this event by August 31,1999. | ||
If you have any questions, please advise. | If you have any questions, please advise. | ||
l Respectfully submitted, | l Respectfully submitted, | ||
.f }}}yyt | |||
~ * - | |||
MGE/ cit:99-001(2). doc Enclosure 9907140083 990702 PDR~.ADOCK 05000364 S | Dave Morey O/ | ||
MGE/ cit:99-001(2). doc Enclosure 9907140083 990702 PDR~.ADOCK 05000364 S | |||
PDR-a a | |||
1 Page 2 | 1 Page 2 U. S. Nuclear Regulatory Commission Southern Nuclear Oneratine Company ec: | ||
U. S. Nuclear Regulatory Commission | Mr. L. M. Stinson, General Manager - Farley U. S. Nuclear Renulatory Commission. Washincton. D. C. | ||
Mr. L. M. Padovan, Licensing Project Manager - Farley U. S. Nuclear Reculatory Commission. Recion II Mr. L. A. Reyes, Regional Administrator Mr. T. P. Johnson, Senior Resident Inspector - Farley | Mr. L. M. Padovan, Licensing Project Manager - Farley U. S. Nuclear Reculatory Commission. Recion II Mr. L. A. Reyes, Regional Administrator Mr. T. P. Johnson, Senior Resident Inspector - Farley | ||
}} | }} | ||
{{LER-Nav}} | {{LER-Nav}} | ||
Latest revision as of 18:16, 6 December 2024
| ML20209D919 | |
| Person / Time | |
|---|---|
| Site: | Farley |
| Issue date: | 07/02/1999 |
| From: | Dennis Morey SOUTHERN NUCLEAR OPERATING CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| Shared Package | |
| ML20209D923 | List:
|
| References | |
| NEL-99-0258, NEL-99-258, NUDOCS 9907140083 | |
| Download: ML20209D919 (2) | |
| Event date: | |
|---|---|
| Report date: | |
| Reporting criterion: | 10 CFR 50.73(a)(2)(iv), System Actuation |
| 3641999001R00 - NRC Website | |
text
f.
r Dave Morey,
Southera Nuclear i..
t t
_ Vice President Operating Compary. Inci farley Project Post Office Box 1295 -
Birmingham, Alabama 35201 Tel 205 932.5131!
SOUTHERN July 2,1999
. COMPANY Energy to Serve hur World" Docket No.:
50-364 NEL-99-0258 U. S. Nuclear Regulatory Commission ATrN: Document Control Desk -
Washington, D, C, 20555-0001 Joseph M. Farley Nuclear Plant - Unit 2 Licensee Event Report 99-001-00 Reactor Trip Due to Loss of Condenser Vacuum On Steam Dumo Drain Line Failure Ladies and Gentlemen:
Joseph M. Farley Nuclear Plant - Unit 2 Licensee Event Report No. 99-001-00 is being submitted in accordance with 10 CFR 50.73(a)(2)(iv).
The following four NRC commitments are included in the Corrective Action section of this LER; no other NRC commitments are contained in this letter.
- 1. An every two weeks preventive maintenance task has 'been implemented to perform visual and acousticci observations of steam dump drain lines until the next Unit 2 refueling outage.
- 2., A design change to further reduce the stress on the steam dump drain lines will be J
implemented during the next Unit 2 refueling outage.
I
- 3. Additional inspections will be performed on the Unit I steam dump drain lines, and the existing Unit I stress analysis will be reviewed. Ifnecessary, appropriate changes
)
will be implemented before the end of the next Unit I refueling outage.
1
- 4. Appropriate design individuals will be trained on this event by August 31,1999.
If you have any questions, please advise.
l Respectfully submitted,
.f}yyt ~ * - Dave Morey O/ MGE/ cit:99-001(2). doc Enclosure 9907140083 990702 PDR~.ADOCK 05000364 S PDR-a a
1 Page 2 U. S. Nuclear Regulatory Commission Southern Nuclear Oneratine Company ec: Mr. L. M. Stinson, General Manager - Farley U. S. Nuclear Renulatory Commission. Washincton. D. C. Mr. L. M. Padovan, Licensing Project Manager - Farley U. S. Nuclear Reculatory Commission. Recion II Mr. L. A. Reyes, Regional Administrator Mr. T. P. Johnson, Senior Resident Inspector - Farley }}