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| Interim 10 CFR Part 21 Report Regarding Internal Pump Tolerances between the Impeller Hub and a Wear Ring This letter serves as an interim report in accordance with 1O CFR 21.21 pertaining to a potential deviation associated with a Flowserve pump model 6L-SVC back pull out assembly (p/n 11952230) that was supplied to the RE Ginna Nuclear Power Plant. A defect may exist with the assembly tolerances between the impeller hub and the wear ring. The tolerances should have been such that there was an interference fit, but during disassembly, which included removal of the wear ring locking set screws, the wear ring was able to be slid off the hub freely. | | Interim 10 CFR Part 21 Report Regarding Internal Pump Tolerances between the Impeller Hub and a Wear Ring This letter serves as an interim report in accordance with 10 CFR 21.21 pertaining to a potential deviation associated with a Flowserve pump model 6L-SVC back pull out assembly (p/n 11952230) that was supplied to the RE Ginna Nuclear Power Plant. A defect may exist with the assembly tolerances between the impeller hub and the wear ring. The tolerances should have been such that there was an interference fit, but during disassembly, which included removal of the wear ring locking set screws, the wear ring was able to be slid off the hub freely. |
| Evaluation of reportability in accordance with 10 CFR Part 21 is not able to be completed within the 60-day evaluation period due to a request from the Original Equipment Manufacturer (OEM) to have the impeller returned for their evaluation, which was not able to be fulfilled due to the subject impeller being lost in transit from the site to the OEM. The OEM has been requested to determine the impact of the deviation as the site does not have the specific hydraulic knowledge to determine if a substantial safety hazard exists. The evaluation of the identified defect will be performed by the OEM under their Corrective Action tracking number 309092, and will be completed by October 14, 2016. | | Evaluation of reportability in accordance with 10 CFR Part 21 is not able to be completed within the 60-day evaluation period due to a request from the Original Equipment Manufacturer (OEM) to have the impeller returned for their evaluation, which was not able to be fulfilled due to the subject impeller being lost in transit from the site to the OEM. The OEM has been requested to determine the impact of the deviation as the site does not have the specific hydraulic knowledge to determine if a substantial safety hazard exists. The evaluation of the identified defect will be performed by the OEM under their Corrective Action tracking number 309092, and will be completed by October 14, 2016. |
| If you have any questions or need any other clarifying information, please contact Thomas Harding, Regulatory Assurance Manager, at (315) 791-5219. | | If you have any questions or need any other clarifying information, please contact Thomas Harding, Regulatory Assurance Manager, at (315) 791-5219. |
| cc: NRC Regional Administrator, Region 1 NRC Project Manager, Ginna NRC Resident Inspector, Ginna}} | | cc: NRC Regional Administrator, Region 1 NRC Project Manager, Ginna NRC Resident Inspector, Ginna}} |
Latest revision as of 17:10, 10 November 2019
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Bill Carsky Plant Manager R.E. Ginna Nuclear Power Plant
) y Exelon Generation 1503 Lake Rd.
Ontario, NY 14519 315 791 5205 Office 215 605 9364 Mobile www.exeloncorp.com william.carsky@exeloncorp.com August 15, 2016 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555-0001 R.E. Ginna Nuclear Power Plant Renewed Facility Operating License No. DPR-18 NRC Docket No. 50-244
Subject:
Interim 10 CFR Part 21 Report Regarding Internal Pump Tolerances between the Impeller Hub and a Wear Ring This letter serves as an interim report in accordance with 10 CFR 21.21 pertaining to a potential deviation associated with a Flowserve pump model 6L-SVC back pull out assembly (p/n 11952230) that was supplied to the RE Ginna Nuclear Power Plant. A defect may exist with the assembly tolerances between the impeller hub and the wear ring. The tolerances should have been such that there was an interference fit, but during disassembly, which included removal of the wear ring locking set screws, the wear ring was able to be slid off the hub freely.
Evaluation of reportability in accordance with 10 CFR Part 21 is not able to be completed within the 60-day evaluation period due to a request from the Original Equipment Manufacturer (OEM) to have the impeller returned for their evaluation, which was not able to be fulfilled due to the subject impeller being lost in transit from the site to the OEM. The OEM has been requested to determine the impact of the deviation as the site does not have the specific hydraulic knowledge to determine if a substantial safety hazard exists. The evaluation of the identified defect will be performed by the OEM under their Corrective Action tracking number 309092, and will be completed by October 14, 2016.
If you have any questions or need any other clarifying information, please contact Thomas Harding, Regulatory Assurance Manager, at (315) 791-5219.
cc: NRC Regional Administrator, Region 1 NRC Project Manager, Ginna NRC Resident Inspector, Ginna