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{{#Wiki_filter:CATEGORY 1~REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDE)ACCESSTON NBR:9608020352 DOC.DATE: 96/07/24 NOTARIZED:
{{#Wiki_filter:CATEGORY 1 REGULATORY INFORMATION DISTRIBUTION SYSTEM
NO FACI.:.-50-335 St.Luci,e Plant, Unit 1, Florida Power&Light Co.50-389 St.Lupie P3;ant, Unit 2, Florida Power 6 Light Co.AUTH.NAME AUTHOR AFFILIATION STALL,J.A.
                                                                      ~      (RIDE)
Florida Power s Light Co.RECIP.NAME REC1'PIENT AFFILIAT10N Document Control Branch (Document Control Desk)DOCKET 05000335 05000389
ACCESSTON     NBR:9608020352               DOC.DATE: 96/07/24     NOTARIZED: NO       DOCKET FACI.: .-50-335   St. Luci,e Plant, Unit 1, Florida Power & Light Co.                 05000335 50-389 St. Lupie P3;ant, Unit 2, Florida Power 6 Light Co.                   05000389 AUTH. NAME           AUTHOR           AFFILIATION STALL,J.A.           Florida           Power s Light Co.
RECIP.NAME           REC1'PIENT AFFILIAT10N Document Control Branch (Document Control Desk)


==SUBJECT:==
==SUBJECT:==
Transmits copy of matls reviewed during 960719 FPL St.Lucie Status Meeting including key performance indicators for St.Lucie Plant.DISTRIBUTION CODE: A001D COPIES RECEIVED:LTR ENCL SIZE: TITLE: OR Submittal:
Transmits copy of matls reviewed during 960719 FPL St. Lucie Status Meeting including key performance indicators for St.
General Distribution NOTES: RECIPIENT ID CODE/NAME PD2-3 LA WIENSFL.COPIES LTTR ENCL 1 1 1 1 RECIPIENT ID CODE/NAME PD2-3 PD COPIES LTTR ENCL 1 1 INTERNAL: ACRS NRR/DE/EMCB NRR/DSSA/SPLB NUDOCS-ABSTRACT
Lucie Plant.
'XTERNAL: NOAC 1 1 1 1 1 1 1 1 1 1 FILE CENTER 01 NR ICB NRR/DSSA/SRXB OGC/HDS3 NRC PDR 1 1 1 1 1 1 1 0 1 1 D N NOTE TO ALL"RIDS" RECIPIENTS:
DISTRIBUTION CODE: A001D                 COPIES RECEIVED:LTR       ENCL     SIZE:
PLEASE HELP UP TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN 5D-5(EXT.415-2083)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!TOTAL NUMBER OF COPIES REQUIRED: LTTR 13 ENCI 12 0 f v-~i+l]f (4 Florida Power 5 Light Company, P.O.Box 128, Fort Pierce, FL 34954-0128 July 24, 1996 L-96-193 10 CFR 50.4 U.S.Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 RE: St.Lucie Units 1 and 2 Docket Nos.50-335 and 50-389 St.Lucie Status Meetin-Jul 1996 During a November 1995 meeting with the NRC, Florida Power and Light Company (FPL)reviewed the progress made in completing activities outlined in the St.Lucie Plan to Improve Operational Performance.
TITLE:   OR Submittal: General Distribution NOTES:
FPL stated that meetings to review performance would be held monthly and would include a detailed review of the plant's key performance indicators.
RECIPIENT                 COPIES          RECIPIENT          COPIES ID CODE/NAME               LTTR ENCL      ID  CODE/NAME      LTTR ENCL PD2-3 LA                       1     1     PD2-3 PD               1    1 WIENSFL.                        1     1 INTERNAL: ACRS                               1    1    FILE  CENTER    01    1    1 NRR/DE/EMCB                     1    1    NR          ICB      1    1 NRR/DSSA/SPLB                   1     1     NRR/DSSA/SRXB         1     1 NUDOCS-ABSTRACT                1     1     OGC/HDS3              1     0 NOAC              'XTERNAL:
In the November meeting, FPL committed to provide the monthly review materials to the NRC.Attached is a copy of the materials reviewed during the July 19, 1996, FPL St.Lucie Status Meeting including the key performance indicators for St.Lucie Plant.We look forward to NRC presence and feedback at these monthly meetings.If you have any questions on this material, please contact us.Very truly yours, J.A.Stall Vice President St.Lucie Plant JAS/EJW Attachment c c: Stewart D.Ebneter, Regional Administrator, USNRC, Region II Ellis W.Merschoff, Director, DRP, USNRC, Region II Kerry D.Landis, Branch Chief, USNRC, Region II Senior Resident Inspector, USNRC, St.Lucie Plant L.A.Wiens, Senior Project Manager, USNRC, NRR 9608020352 960724 PDQ(l'ADOCK 05000335 P'PDR an FPL Group company ST.LUCIE STATUS MEETING AGENDA JULY 19, 1996 9:30 AM SSB ROOM 2200 J.Scarola A.Pell GOALS vs.PERFORMANCE SCOPE COMPLETED EQUIPMENT UPGRADES NEAR MISS ENERGIZING 1B2 4160v BUS UNIT 2 MANUAL TRIP ON 6/6 DUE TO GENERATOR TEMPERATURE INADVERTENT SIAS ACTUATION ON 6/8 STEAM GENERATOR LOSS OF BUDGET CONTROL RAYTHEON CONTRACT MISMANAGMENT B.Korte J.Price R.Filipek G.Boissy~R.Heroux J.Marchese OPERATIONS MAINTENANCE ENGINEERING/TECHNICAL MATERIALS MANAGEMENT SERVICES CORRECTIVE ACTIONS QUALITY ASSURANCE LICENSING H.Johnson J.Marchese D.Denver G.Boissy C.Burton B.Dawson W.Bladow E.Weinkam'...960802Q35$
1     1     NRC PDR                1   1 D
0 e ox zmTIzg azvoav e
N NOTE TO ALL "RIDS" RECIPIENTS:
Unit1 Equivalent Availability DAILY EQUIVALENT AVAILABIUTY 0 Days orartne as of 7/I5/96.'%~V'1 II j, 4"r'.,4+I/u 4 nrul 2&if'+%0~,~sf ii<<sl 4'I/0 t+t ri/'ut/lith/o>6 5 IT'l/lit'',"'''9 a'', I gw at~I a~2~2''yu&#xc3;I-444~@I0f~t'~~~+-NT74+O,".""-4/i
PLEASE HELP UP TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN 5D-5(EXT. 415-2083) TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
~n4 tet<<<~44l&#xc3;t<~II~~:4~<<fa I q)/~'~45~i+I t 4 I%21~'~45~q-"EIL~~N a&=0/10/QO 0/la/90 0/20IQO OI22/90 0/24/90 0/20/90 0/24/90 0/Xrte 7/2/90 7/4/90 7/tvas 7/0/te 7/10/90 7/12/te 7/14/90 7/10/90 Monthly Average EAFaOOAXN Lost Generation Date MWH Loss 0/1000/te 4020%tech/44/o Oi/faye 1$dare Reason Besot ea a Mtaaiae/a e/ttdatse capassy of 029 Mw EQUIVALENT AVAILABILITY FACTOR-UNIT 1 949 QSA Tan/ct e705 Bett Aaa'etta/e a 740~Ate/at---Ta/Qet 4--Best ttaeatse 75 704 aa 50 Ie 0 Fat/Mar Apr May tun Jul Aug Sep Oct Nov Dec Date Unit 2 Equivalent Availability DAILY EQUIVALENT AVAILABILITY 32 Days on4ne Bs of 7/I5/96.P 00 n-D a 00 ryT!g ion 0*.+ac'$y I~i to nI'44 5 rs 4*'v r 24 g r4 l$20/IO 5/2?/90 5/24/90 5/25/90 5/25/te Shoss 7/2/90 7/4/90 7/5/90 7/5/90 Tha/90 Th2/90 Tlin/90 7h5/95 Date Monthly At/erage EAF&5.9250 Lost Generation Date 5/1025he 5/2405/90 5/2740/90 MWH Loss Reason 2B IlFW ito0.V/na Hi Vhr.yo/ona SP.-747 Hi BP/rn/S.V/r/5/m.t/t Bnsce on 5 54annun opnnsoon eooncar or 059 Mw EQUIVALENT AVAILABILITY FACTOR-UNIT 2 75 Tor9et~95.0.Good.47 a 50~O Feb Mar Apr May tun Date AUTOMATIC REAGTOR TRIPS Legend 5-~Actual 4 rn CL l 3 0 0 R 2.Good.-..0-Oct Dec Jan'SS Mar May Date Jul Sep Nov Data Source: Hugh Johnson  
TOTAL NUMBER OF COPIES REQUIRED: LTTR                   13   ENCI     12
 
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Florida Power 5 Light Company, P.O. Box 128, Fort Pierce, FL 34954-0128 July 24, 1996 L-96-193 10 CFR 50.4 U. S.     Nuclear Regulatory Commission Attn:     Document Control Desk Washington,         DC 20555 RE:     St. Lucie Units       1 and 2 Docket Nos. 50-335 and 50-389 St. Lucie Status Meetin               Jul     1996 During       a November 1995     meeting with the NRC, Florida Power and Light     Company     (FPL) reviewed     the progress made in completing activities outlined in the St. Lucie Plan to Improve Operational Performance.           FPL stated that meetings to review performance would be held monthly and would include a detailed review of the plant's key performance indicators. In the November meeting, FPL committed to provide the monthly review materials to the NRC.
Attached       is a copy of the materials reviewed during the July 19, 1996, FPL       St. Lucie Status Meeting including the key performance indicators for St. Lucie Plant.
We look forward to NRC presence                 and feedback at these monthly meetings.         If you have any questions on this material, please contact us.
Very     truly     yours, J. A. Stall Vice President St. Lucie Plant JAS/EJW Attachment c c:     Stewart D. Ebneter, Regional Administrator, USNRC, Region Ellis     W. Merschoff, Director, DRP, USNRC, Region II II Kerry D. Landis, Branch Chief, USNRC, Region II Senior Resident Inspector, USNRC, St. Lucie Plant L. A. Wiens, Senior Project Manager, USNRC, NRR 9608020352 960724 PDQ(l'ADOCK 05000335
    '
P                       PDR an FPL Group company
 
ST. LUCIE STATUS MEETING AGENDA JULY 19, 1996 9:30 AM SSB ROOM 2200 J. Scarola A. Pell GOALS vs. PERFORMANCE SCOPE COMPLETED EQUIPMENT UPGRADES NEAR MISS ENERGIZING 1B2 4160v BUS                   B. Korte UNIT 2 MANUALTRIP ON 6/6 DUE TO GENERATOR TEMPERATURE J. Price INADVERTENT SIAS ACTUATION ON 6/8                     R. Filipek STEAM GENERATOR                                      G. Boissy ~
LOSS OF BUDGET CONTROL                                R. Heroux RAYTHEON CONTRACT MISMANAGMENT                        J. Marchese OPERATIONS                                                   H. Johnson MAINTENANCE                                                  J. Marchese ENGINEERING/TECHNICAL                                        D. Denver MATERIALS MANAGEMENT                                          G. Boissy SERVICES                                                      C. Burton CORRECTIVE ACTIONS                                            B. Dawson QUALITYASSURANCE                                              W. Bladow LICENSING                                                    E. Weinkam
                            '...960802Q35$
 
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Unit1 Equivalent Availability
            '%~V'       1 II j, 4 "r'.,4+I/ u 4 DAILYEQUIVALENTAVAILABIUTY nrul 2&if'+%0 ~,~sf ii<<sl 4'I/ 0 t     +t ri/'ut   /lith/o >6 5 IT     'l /lit'',         "'''9 a '', I 0 Days orartne as of 7/I5/96.
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  ~ I a
  ~2
              ~2 ''yu &#xc3;I-444~@I0f~t'~~~+-NT74+O,".""-4/i~                       n4 tet< <<~44l&#xc3;t <~II~~:4~<<fa I q )/ ~'~45~i+I                   t 4     I%21     ~'~45~q-"EIL~~N         a &=
0/10/QO     0/la/90     0/20IQO     OI22/90   0/24/90   0/20/90   0/24/90   0/Xrte   7/2/90       7/4/90       7/tvas       7/0/te         7/10/90     7/12/te   7/14/90     7/10/90 Monthly Average EAFaOOAXN Lost Generation Date         MWH Loss                                                 Reason 0/1000/te         4020%       tech/44/o Oi/faye 1$ dare Besot ea a Mtaaiae/a e/ttdatse   capassy of 029 Mw EQUIVALENTAVAILABILITY                    FACTOR - UNIT 1
                                                                                                                                                                        ~Ate/at 949           QSA Tan/ct e705                                 --4--- Ta/Qet Bett Aaa'etta/e a 740                                   Best ttaeatse 75 704 aa Ie 50 0
Fat/         Mar           Apr           May       tun             Jul             Aug               Sep             Oct         Nov             Dec Date
 
Unit 2 Equivalent Availability DAILYEQUIVALENTAVAILABILITY                                      32 Days on4ne Bs of 7/I5/96.
g I~ i to      nI P   00 ryT                                                                                    rs 4*
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            !
g                                                                                         24                                  l ion   0*. +ac'$
y                                   5
                                  $ 20/IO   5/2?/90 5/24/90     5/25/90   5/25/te   Shoss     7/2/90   7/4/90   7/5/90 7/5/90     Tha/90   Th2/90   Tlin/90   7h5/95 Date                         Monthly At/erage EAF&5.9250 Lost Generation Date       MWH Loss                        Reason 5/1025he                       2B IlFWito0. V/na 5/2405/90                     Hi Vhr.yo/ona SP.
5/2740/90          -747       Hi BP/rn/S.V/r/5/m.t/t Bnsce on 5 54annun opnnsoon eooncar or 059 Mw EQUIVALENTAVAILABILITY                  FACTOR - UNIT 2 Tor9et ~ 95.0 75                                                                                                                                          .Good .
47 a
50
    ~O Feb         Mar           Apr           May       tun Date
 
AUTOMATICREAGTOR TRIPS Legend 5-                                                       ~Actual 4
                                                                .Good  .-..
rn CL l
03 0
R 2
0-Oct Dec Jan 'SS Mar May Jul Sep Nov Date Data Source: Hugh Johnson
 
-
-
ST.LUGI ANT Equipment Causes Operations to Maneuver Plant 20 15.10 0'u 0 0.1 QTR 95 2 QTR 3 QTR Date 4 QTR 1 QTR 96 2 QTR  
ST. LUGI         ANT Equipment Causes Operations to Maneuver Plant 20 15.
10 0
'u 0
0.
1 QTR 2 QTR             3 QTR               4 QTR       1 QTR 2 QTR Date                  96 95


T 1 ovrAGE 8 1996 SPRING OUTAGE GOALS gNIT 1 I Personnel Safety-Lost Time Injuries Goal~~~~~~~~~~0 Actual 0 2.Doctor Case Injuries~~~~~~~~~~~~~~~~~~~.<6 12 3.NRC Violations......................................
T 1 ovrAGE 8
0 0 4.Outage Duration~..............
 
~.~................
1996 SPRING OUTAGE GOALS gNIT 1 I                                                           Goal  Actual Personnel Safety - Lost Time Injuries                     ~ ~ ~ ~ ~ ~ ~ ~ ~ ~   0   0
~49 85 5.Personnel Radiation Exposure........-...., 6.Personnel Contaminations (any Contamination Resulting in a Skin Dose)...............-..
: 2. Doctor Case Injuries             ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~     . <6     12
....~310Mrem~~~~~~~~~o 5 1 0 366 7.Contaminated Floor Space within 14 Days PostOutage.................,.............,.
: 3.     NRC   Violations...................................... 0                                 0
<1,500ft'BD 9.Outage Budget........,..........
: 4.     Outage Duration ~..............     ~ . ~................ ~ 49                         85
.:....~$25 Million 8.Cubic Feet of Radiological Waste Gen.............
: 5.     Personnel Radiation Exposure........-...., .... ~ 310Mrem                                366
<6,300 ft3 11,935 ft3 31.6 Million 10.Unit Performance
: 6.     Personnel Contaminations (any Contamination Resulting in a Skin   Dose)...............-..     ~ ~ ~ ~ ~ ~ ~ ~ ~ o   5   1 0 Contaminated Floor Space within 14 Days PostOutage.................,.............,. <1,500ft'BD 7.
-60 days Post Outage Availability...
: 8.     Cubic Feet of Radiological Waste Gen............. < 6,300 ft3                            11,935 ft3
>93 TBD outgoal.wpd July 17, 1996 Duration Plant Modifications*
: 9.      Outage Budget........,..........               .:.... ~ $ 25 Million                    31.6 Million
NPWOs Activities CRs OWAs S/G Tubes P.lugged S/G Tubes Staked S/6 PAPs*12 Major 8 69 Minor Original Schedule 46 72 1769 5243 N/A 17 50 500 Actual 85 81 2556 9170 978 17 2081 163 500 Difference 39 787 3927 N/A 0 2031 156 0 10 Year Reactor Vessel Exam&Core Barrel Inspections Main Generator End Winding Module&Through Bolt Repairs Incore Instrument Assembly Replacement Polar Crane Load Test Diesel Generator Governor&Radiator Replacements RCP Seal Replaced Westinghouse S/G Tube Plug Repair (PAPs)&S/G Tube Plugs Pressurizer Code Safety Valve Replacements
: 10. Unit Performance
.HP Turbine Seal Ring Replacement Condenser Tube Cleaning System RPS NIS Upgrade V071 61&Bypass Replacement RCGVS Valve Replacements
        - 60 days Post Outage Availability...                                       >   93   TBD outgoal.wpd   July 17, 1996
&Piping Mod Rx Head 0-ring Upgrade Outage Progress Chart St.Lucie Unit 1 Cycle 14 Refueling 100 0-1 00-200-300 g-400:.,Expanded MRPC~~~~~~'.Free Span Added MRPC~~~~g~Cunent Outage Dunttion 85 Days 3 Koum-500-600~Kours Ahead or Behind 1pp%MRPC-700~t~-800-900~0 S/8 Rework';
 
Outage Progress Chart Legend Gains 8 Losses (Hours)Date 4/29 4/30 5/1 5/2 5/3 5/4 5/5 5/6 5n 5/8 5/9 5/10 5/11 5/12 5/13 5/14 5/15 Thru 5/26 5/2?Thru 6/3 6I4 Thru 7/5 7/6 Thru 7/12 7/13 7/14 7/15 7/16 7/17 Day 1 2 3 4'6 7 89 10 11 12 13 14 15 16 17 27 28 35 36 68 69 74 75 76 77 78 79 Hours 6 Loss 8 Gain 3 Loss 8 Loss 14 Gain 26 Gain 14 Loss 34 Gain 41 Loss 3 Loss 5 Loss 8 Gain 189 Loss 148 Loss Free Span Added MRPC 480 Loss 100%MRPC r 130 Loss S/G Rework 6 Loss 13 Loss 20 Loss 11 Loss 11 Loss CEDM Venting RCP 1A2 Seal Leakoff Flange Leak Valve Ql-II's 8 Retesting HVS-1B Cooler Leak HVS-1B Cooler Repair Discription Delayed Shutdown CEA&#xb9;1 Beaming Metal Temperature Satisfactory Generator Disassembly Blower Gas Baffle Removal Blower Gas Baffle Removal Generator Blower Disassembly Rotor Removal Asbestos Abatement Wedge Replacement Scope Expansion:
Original Actual Difference Schedule Duration               46        85      39 Plant Modifications*     72      81 NPWOs                 1769    2556      787 Activities             5243    9170    3927 CRs                     N/A      978      N/A OWAs                     17      17        0 S/G Tubes P.lugged       50    2081    2031 S/G Tubes Staked                 163      156 S/6 PAPs               500      500        0
Low Torque on Through Bolts Generator Disassembly Generator Disassembly Support Ring Removal Support Ring Removal Support Ring Removal Support Ring Removal Expanded MRPC Hours Lost From Original 46 Day Outage Total Duration: 85 Days (Projected)
*12 Major 8 69 Minor
Original Schedule:.46 Days Hours Days System Description
 
-793-33 Steam Generators Expansion of MRPC 8 Tube Plugging Scope-96-22-20-0.92-0.83 Steam Generators Component Cooling Water Sy'tem ECCS 8 RCS Rework-Missing "8" S/G H/L Plug 8 2"A" S/G H/L Stakes HVS-1B Cooler Leak Valve Ql-II's 8 Retesting-13-6 960-.0.64-0.25 39.5 Rx Coolant System RCP 1A2 Seal Leakoff Flange Leak Rx Coolant System CEDM Venting TOTAL The Major Schedule Impact Behind The Steam Generators Hours 912 456 72 64 Days 38 3 System Nuclear Instrumentation Resources Fuel Pool System Process Delays/Problems Description Wide Range Nl's 8 RPS Nl Upgrade Project Reduced Primary&Secondary Resources Behind Steam Generators Fuel Transfer Gate Valve V-4111 Clearances, Housekeeping, Paperwork, Procedures 0 c ILGZL8~Pre-outage Planning&Preparations Pre-outage Milestones Must be Met for Upcoming Outages Earlier Delivery of NPWO's, PCM's 8 Procedures Continue to Improve Organization's Schedule Adherence Freeze Organizational
10 Year Reactor Vessel Exam & Core Barrel Inspections Main Generator End Winding Module & Through Bolt Repairs Incore Instrument Assembly Replacement Polar Crane Load Test Diesel Generator Governor & Radiator Replacements RCP Seal Replaced Westinghouse S/G Tube Plug Repair (PAPs) & S/G Tube Plugs Pressurizer Code Safety Valve Replacements
&Process Changes Earlier (Pre-outage)
.
~Scope Control~20/30 MRB~Budget Controls~Manpower Schedule Set Earlier~13 Week Rolling Schedule~Scheduled CMMs, Perform Daily Work Out of Outage~Improve Organization's Schedule Adherence~Eliminate Periods of Inactivity
HP Turbine Seal Ring Replacement Condenser Tube Cleaning System RPS NIS Upgrade V071 61 & Bypass Replacement RCGVS Valve Replacements & Piping Mod Rx Head 0-ring Upgrade
~Improve Communications 8 Handoffs~Ensure Procedures are Ready~~~~~Continue to Improve Contingency Planning azC~~y~ACTIONS
 
.NEAR MISS ENERGIXING 1B2 4160V BUS On June 1, 1996, the Electrical Maintenance outage shift supervisor (peakshift) released the 1B2 4160V bus clearance with a grounding breaker installed in the Auxiliary Transformer feeder breaker cubicle.During the bus restoration by Operations, the peakshift Chief Electrician discovered the grounding breaker and alerted operations to stop the restoration.
Outage Progress Chart St. Lucie Unit 1 Cycle 14 Refueling 100 Cunent Outage Dunttion 85 Days 3 Koum 0
CA E (ERT TEAM FINDINGS)Bi Failure of the Supervisor to ensure the equipment was ready for service: Unaware of the configuration of the feeder stabs and the bus stabs Did nof read the caution tag installed on the grounding breaker indicating the bus was grounded Did not review all work orders associated with the work on the bus or related equipment The clearance order did not have the work order number associated with the bus work on the clearance N All Electrical Maintenance Shift Supervisors are not required to be trained in the high voltage grounding training Clearance orders do not list work orders against the clearance Clearance orders do not list grounds on the clearance order There is no labeling at the bus cubicles that identify that grounds are installed13 NEAR MISS ENERGIZING IB2 4160V BUS RRECT A COML.DAYK.DISCIPLINARY ACTION TO THE SUPERVISOR SAFETY MEETING REVIEW REVISE THE CLEARANCE PROCEDURE TO TRACK GROUNDS AS PART OF THE CLEARANCE ORDER ISSUE NEW CLEARANCE PROCEDURE (F.R.G.)UPDATE DRAWINGS TO NOTE BUS CONFIGURATIONS 6/3/96 6/20/96 6/30/96 7/30/96 7/30/96 ANNUAL HIGH VOLTAGE GROUNDING TRAINING 8/2/96 FOR SUPERVISORS ADD PLACARDS/VISUAL AIDS TO BREAKER CUBICLE WHEN GROUNDED REVISE THE CAUTION TAG PROCEDURE TO REFLECT SPECIFIC LOCATION OF GROUNDS 8/30/96 7/15/96 14 MANUAL REACTOR TRIP DUE TO HIGH COLD GAS TEMPERATURE At 1209 on June 6, 1996 the GENERATOR TEMPERATURE MONITOR annunciator (N49)alarm was received.The Kaye computer, which records main generator temperature showed that average cold gas temperature was above normal at 48.8 degrees but was decreasing.
:.,Expanded MRPC
The annunciator cleared one minute later and all temperatures returned to normal and were stable.TCV-13-15 (hydrogen cooler outlet temperature control valve)was in automatic and appeared to be controlling at setpoint.At 1232, the control room noted average cold gas temperature rising as displayed on the Kaye computer.Within seconds the temperature reached 53 degrees, which is above the procedurally required reactor trip level of 52 degrees.The Operators tripped the reactor and turbine.Initial investigation indicated that TCV-13-15 had failed closed, and that the positioner feedback arm had vibrated loose and fell off.~~~~~~This is the second event in 1996 in which closure of TCV-13-15 had caused a Manual trip.This issue was addressed in PR-96-001 and was attributed to improper setting of the derivation setting.ROOT CAUSE (ERT FINDINGS)TCV-13-15 has high level of system induced vibration.
  -1 00
Positioner linkage fasteners are below level of design.DevCon material was used as locking mechanism and periodically inspected.
                                ~ ~ ~~
                                        ~~
  -200
                                                  '. Free Span Added MRPC
  -300
                                          ~~ ~ ~ g~
g -400
  -500   ~Kours Ahead or Behind 1pp% MRPC
  -600
  -700                                                                                 ~ t~
  -800                                               ~
0 S/8 Rework ';
  -900
 
Outage Progress Chart Legend Gains 8 Losses (Hours)
Date Day  Hours    Discription 4/29 1   6 Loss    Delayed Shutdown CEA &#xb9;1 4/30 2   8 Gain    Beaming Metal Temperature Satisfactory 5/1  3  3 Loss    Generator Disassembly 5/4'  8 Loss    Blower Gas Baffle Removal 5/3                Blower Gas Baffle Removal 5/6   14 Gain  Generator Blower Disassembly 5/5   7  26 Gain  Rotor Removal 5/6  8  14 Loss  Asbestos Abatement 5n    9  34 Gain  Wedge Replacement 5/8  10 41 Loss  Scope Expansion: Low Torque on Through Bolts 5/11 3 Loss    Generator Disassembly 5/10  12 5 Loss    Generator Disassembly 5/11  13 8 Gain    Support Ring Removal 5/12  14           Support Ring Removal 5/13  15           Support Ring Removal 5/14  16            Support Ring Removal 5/15  17  189 Loss  Expanded MRPC Thru 5/26  27 5/2? 28  148 Loss  Free Span Added MRPC Thru 6/3   35 6I4   36  480 Loss  100% MRPC Thru 7/5   68                r 7/6   69  130 Loss  S/G Rework Thru 7/12 74 7/13 75  6 Loss    CEDM Venting 7/14 76  13 Loss  RCP 1A2 Seal Leakoff Flange Leak 7/15 77  20 Loss  Valve Ql-II's 8 Retesting 7/16 78  11 Loss  HVS-1B Cooler Leak 7/17 79  11 Loss  HVS-1B Cooler Repair
 
Total Duration:        85 Days (Projected)
Hours Lost From Original 46 Day Outage            Original Schedule:  . 46 Days Hours      Days          System                            Description
-793        -33    Steam Generators  Expansion of MRPC 8 Tube Plugging Scope Steam Generators  Rework-Missing "8" S/G H/L Plug 8 2 "A" S/G H/L
  -96 Stakes Component        HVS-1B Cooler Leak
  -22      -0.92    Cooling Water Sy'tem
  -20      -0.83    ECCS 8 RCS        Valve Ql-II's 8 Retesting
  -13      -.0.64  Rx Coolant System RCP 1A2 Seal Leakoff Flange Leak
  -6      -0.25    Rx Coolant System CEDM Venting 960        39.5    TOTAL
 
The Major Schedule Impact Behind The Steam Generators Hours     Days         System                           Description Nuclear            Wide Range Nl's 8 RPS Nl Upgrade Project 912        38 Instrumentation Resources          Reduced Primary & Secondary Resources Behind 456                                  Steam Generators 72              Fuel Pool System    Fuel Transfer Gate Valve V-4111 Process            Clearances, Housekeeping, Paperwork, Procedures 64          3 Delays/Problems
 
0 c      ILGZL8
~ Pre-outage Planning & Preparations Pre-outage Milestones Must be Met for Upcoming Outages Earlier Delivery of NPWO's, PCM's 8 Procedures Continue to Improve Organization's Schedule Adherence Freeze Organizational & Process Changes Earlier (Pre-outage)
~ Scope Control
  ~    20/30 MRB
  ~    Budget Controls
  ~    Manpower Schedule Set Earlier
~ 13 Week Rolling Schedule
  ~    Scheduled CMMs, Perform Daily Work Out of Outage
  ~    Improve Organization's Schedule Adherence
~ Eliminate Periods of Inactivity
  ~    Improve Communications 8 Handoffs
  ~    Ensure Procedures are Ready
  ~    Continue to Improve Contingency Planning
                ~    ~
    ~    ~
 
azC        ~
    ~y~ ACTIONS
 
.                NEAR MISS ENERGIXING 1B2 4160V BUS On June 1, 1996, the Electrical Maintenance outage shift supervisor (peakshift) released the 1B2 4160V bus clearance with a grounding breaker installed in the Auxiliary Transformer feeder breaker cubicle. During the bus restoration by Operations, the peakshift Chief Electrician discovered the grounding breaker and alerted operations to stop the restoration.
CA      E              (ERT TEAM FINDINGS)
Bi Failure of the Supervisor to ensure the equipment was ready for service:
Unaware of the configuration of the feeder stabs and the bus stabs Did nof read the caution tag installed on the grounding breaker indicating the bus was grounded Did not review all work orders associated with the work on the bus or related equipment The clearance order did not have the work order number associated with the bus work on the clearance N
AllElectrical Maintenance Shift Supervisors are not required to be trained in the high voltage grounding training Clearance orders do not list work orders against the clearance Clearance orders do not list grounds on the clearance order There is no labeling at the bus cubicles that identify that grounds are installed 13
 
NEAR MISS ENERGIZING IB2 4160V BUS
                                                  .
RRECT      A COML. DAYK DISCIPLINARYACTION TO THE SUPERVISOR      6/3/96 SAFETY MEETING REVIEW                    6/20/96 REVISE THE CLEARANCE PROCEDURE TO TRACK  6/30/96 GROUNDS AS PART OF THE CLEARANCE ORDER ISSUE NEW CLEARANCE PROCEDURE (F.R.G.)    7/30/96 UPDATE DRAWINGS TO NOTE BUS              7/30/96 CONFIGURATIONS ANNUALHIGH VOLTAGE GROUNDING TRAINING 8/2/96 FOR SUPERVISORS ADD PLACARDS/VISUALAIDS TO BREAKER        8/30/96 CUBICLE WHEN GROUNDED REVISE THE CAUTION TAG PROCEDURE TO      7/15/96 REFLECT SPECIFIC LOCATIONOF GROUNDS 14
 
MANUALREACTOR TRIP DUE TO HIGH COLD GAS TEMPERATURE At 1209 on June 6, 1996 the GENERATOR TEMPERATURE MONITOR annunciator (N49) alarm was received. The Kaye computer, which records main generator temperature showed that average cold gas temperature was above normal at 48.8 degrees but was decreasing. The annunciator cleared one minute later and all temperatures returned to normal and were stable. TCV-13-15 (hydrogen cooler outlet temperature control valve) was in automatic and appeared to be controlling at setpoint.
At 1232, the control room noted average cold gas temperature rising as displayed on the Kaye computer. Within seconds the temperature reached 53 degrees, which is above the procedurally required reactor trip level of 52 degrees. The Operators tripped the reactor and turbine.
Initial investigation indicated that TCV-13-15 had failed closed, and that the positioner feedback arm had vibrated loose and fell off.
This is the second event in 1996 in which closure of TCV-13-15 had caused a
      ~
Manual trip. This issue was addressed in PR-96-001 and was attributed to
          ~        ~
            ~
                                  ~
improper setting of the derivation setting.
                              ~
ROOT CAUSE (ERT FINDINGS)
TCV-13-15 has high level of system induced vibration.
Positioner linkage fasteners are below level of design. DevCon material was used as locking mechanism and periodically inspected.
This particular failure was not precluded using this practice of fastener retention.
This particular failure was not precluded using this practice of fastener retention.
Fail close mechanism under current design does not allow sufficient time for operator intervention.
Fail close mechanism under current design does not allow sufficient time for operator intervention. Operation in bypass will provide adequate control under varying system dynamic changes with some operator action.
Operation in bypass will provide adequate control under varying system dynamic changes with some operator action.
 
MANUAL REACTOR TRIP DUE TO HIGH COLD GAS TEMPERATURE CORRECTIVE ACTIONS Isolate TCV-13-15 and operate in manual bypass.Modify positioner to a direct mounted device eliminating linkage failure mechanisms.
MANUALREACTOR TRIP DUE TO HIGH COLD GAS TEMPERATURE CORRECTIVE ACTIONS Isolate TCV-13-15 and operate in manual bypass.           Complete Modify positioner to a direct mounted device             Complete eliminating linkage failure mechanisms.
Four valves per unit affected.Complete Complete Review system and component requirements for PMAI Due 8/31/96 optimizing TCW control under v'arying load conditions.
Four valves per unit affected.
PM 96-06~7 Provide design changes as necessary to eliminate TCV failures as plant trip initiators while in automatic, or continue manual operation.
Review system and component requirements for             PMAI Due 8/31/96 optimizing TCW control under v'arying load conditions. PM 96-06~7 Provide design changes as necessary to eliminate         Working TCV failures as plant trip initiators while in automatic, or continue manual operation.
Working 16  
16
.INADVERTENT SIAS ACTUATION ON 6/8/96 EVENT SEQUENCE a6/8/96-INADVERTENT ACTUATION OF'B'HANNEL SIAS AND CIAS RECEIVED WHEN IBC MAINTENANCE REPLACED POWER SUPPLY REGULATING CARD.ERT TEAM ESTABLISHED.
 
~SENSITIVE SYSTEMS PROCEDURES INVOKED FOR TROUBLESHOOTING.
.                 INADVERTENTSIAS ACTUATIONON 6/8/96 EVENT SEQUENCE a6/8/96 - INADVERTENTACTUATION OF 'B'HANNEL SIAS AND CIAS RECEIVED WHEN IBC MAINTENANCE REPLACED POWER SUPPLY REGULATING CARD.
IDENTIFIED POTENTIAL FOR CSAS 8 RAS ACTUATION DURING TROUBLESHOOTING BUT THAT WAS INADVERTENTLY COMMUNICATED TO THE OPERATING CREW ON 7/3/96.~7/3/96-INADVERTENT ACTUATION OF'B'HANNEL CSAS&RAS RECEIVED WHILE TROUBLESHOOTING PREVIOUS ACTUATION.-
ERT TEAM ESTABLISHED.
ROOT CAUSE INVESTIGATION RESULTS 6/8/96 ACTUATION aAUCTIONEERED POWER SUPPLIES BOTH FAILED CAUSING INITIAL ACTUATION.
              ~ SENSITIVE SYSTEMS PROCEDURES INVOKED FOR TROUBLESHOOTING. IDENTIFIED POTENTIAL FOR CSAS 8 RAS ACTUATION DURING TROUBLESHOOTING BUT THAT WAS INADVERTENTLYCOMMUNICATED TO THE OPERATING CREW ON 7/3/96.
S3 SUPPLY HAD CROWBARED DURING ADJUSTMENTS OR INSTALLATION OF REGULATING CARD.M3 SUPPLY FUSE BLEW WHILE INSERTING REGULATING CARD.LOSS OF BOTH POWER SUPPLIES CAUSED ACTUATION RELAYS TO DE-ENERG IZE.~ESFAS ACTUATION MODULE POWER SUPPLIES NOT WIRED PER-DRAWINGS.BY DESIGN SIAS&CIAS ARE POWERED FROM POWER SUPPLIES INDEPENDENT FROM THOSE THAT FAILED.17 ROOT CAUSE/NVEST/GAT/ON RESUl TS 7/3/98 ACTUATION+MISCOMMUNICATION OF SENSITIVE SYSTEMS TO THE OPERATING CREW.aMISUNDERSTANDING OF WHAT"ENERGIZE TO ACTUATE" MEANS IN REGARDS TO CSAS AND RAS.DUE TO ACTUATION MODULE DESIGN, THE ACTUATION RELAYS WILL ENERGIZE IF+15V POWER IS LOST BUT+24V REMAINS.WHEN+15V POWER WAS REMOVED DURING TROUBLESHOOTING, CSAS AND RAS ACTUATED.WHILE THIS IS AN ACCEPTABLE DESIGN, THE MISUNDERSTANDING WAS THAT IT WAS ASSUMED THAT"ANY" LOSS OF VOLTA'GE WOULD NOT CAUSE AN"ENERGIZE TO ACTUATE" SYSTEM TO ACTUATE.CORRECTIVE ACTIONS+READJUSTED POWER SUPPLIES REWIRED ESFAS SA AND SB CABINETS PER DESIGN DOCUMENTATION
      ~ 7/3/96- INADVERTENTACTUATION OF   'B'HANNELCSAS  & RAS RECEIVED WHILE TROUBLESHOOTING PREVIOUS ACTUATION.-
'LTHOUGH IT WAS DETERMINED THAT ESFAS WOULD PROPERLY FUNCTION IN THE AS FOUND CONFIGURATION.
ROOT CAUSE INVESTIGATION RESULTS 6/8/96 ACTUATION aAUCTIONEERED POWER SUPPLIES BOTH FAILED CAUSING INITIALACTUATION. S3 SUPPLY HAD CROWBARED DURING ADJUSTMENTS OR INSTALLATIONOF REGULATING CARD. M3 SUPPLY FUSE BLEW WHILE INSERTING REGULATING CARD. LOSS OF BOTH POWER SUPPLIES CAUSED ACTUATION RELAYS TO DE-ENERG IZE.
~PROVIDE GUIDANCE ON WHAT"ENERGIZE TO ACTUATE" MEANS.m 18  
                ~ ESFAS ACTUATION MODULE POWER SUPPLIES NOT WIRED PER
~C I P RR~C~~P~C~P~C~0~~~C PJ C~
            - DRAWINGS. BY DESIGN SIAS & CIAS ARE POWERED FROM POWER SUPPLIES INDEPENDENT FROM THOSE THAT FAILED.
team Generator P ugging Operation+157 Short Tube Stabilizers
17
+4 Long Tube Stabilizers
 
+1021 Tubes Plugged in Steam Generator"A"+1060 Tubes Plugged in Steam Generator"B"+2 Welded Plug Repairs+Corner Cover Plates Modifications for Plugging+Scheduled Finnish of Plugging Operations
ROOT CAUSE /NVEST/GAT/ON RESUl TS 7/3/98 ACTUATION
-7/12/96+Finished Plugging Operation on 7/5/96 0 Original Base Scope of Work+3 Plenum Effort Dual Guide Tube during PAP Installation, than 4 Plenum Operation+100%0 Bobbin Coil Testing+100'/o Hot Leg MRPC+20'lo Cold Leg MRPC+Inspection Schedule k PAP Installation
            +MISCOMMUNICATIONOF SENSITIVE SYSTEMS TO THE OPERATING CREW.
-15 Days+Steam Generator Work Started-5/7/96+Completed Original Base Scope of Work-5/18/96+Completed 3 Days Ahead of Schedule.+Includes 1 Day Delay for PAP Installation Revise Scope of Wor+100/0 Cold Leg MRPC+Diagnostic Testing Program+Limited Free Span Testing+100/0 of P9 k 010 Support Plates+100'/0 Free Span Testing+Extended Outage Duration from 5/19/96-6/26/96+Combinations of Inspection and Plugging Operations in progress.during this period.+Equipment Expansion-Platforms Modifications, dditional Genesis Equip:nt Added (10 Stations)-
aMISUNDERSTANDING OF WHAT "ENERGIZE TO ACTUATE" MEANS IN REGARDS TO CSAS AND RAS. DUE TO ACTUATION MODULE DESIGN, THE ACTUATION RELAYS WILL ENERGIZE IF+ 15V POWER IS LOST BUT+24V REMAINS. WHEN +15V POWER WAS REMOVED DURING TROUBLESHOOTING, CSAS AND RAS ACTUATED. WHILE THIS IS AN ACCEPTABLE DESIGN, THE MISUNDERSTANDING WAS THAT IT WAS ASSUMED THAT "ANY" LOSS OF VOLTA'GE WOULD NOT CAUSE AN "ENERGIZE TO ACTUATE" SYSTEM TO ACTUATE.
I team Generator C oseout Process+Missing (2)Short Stabilizers in Steam Generator"A"-Transcription Error+Missing Hot Leg Plug in Steam Generator"B"-Shift Supervisor Interpretation Error LOSS OF BUDGET CONTROL Problems Encountered Poor contract administration practices Budget inadequate Budget does not mirror site organization Budget disconnected from tracking Departments not familiar with approved budget Resource Controls Staff not independent Expectations not clear O.Enhanced Controls Contract Administration Enforcement of NP 1100 Authorization Matrix Discipline for Violations Eliminate"covenience contractors" Full time Phone Tech and Plumber Service agreements Good Practice-NC performed by PSL Maintenance Reduce Overtime Eliminate Exempt Overtime Confine Non Exempt overtime to LCO and,Techspec Eliminate Discretionary Spending Subscriptions, Painting, Tool Purchases Office Supplies, Luncheons, Consummables Budget Reconstitute 1996 08 M Budget$24 Million in budgeted funds for the balance of 1996 Must reduce to'bare bones'otal recovery is not possible New Process for 1997 MRB to determine Project Scope during budget cycle Resource Controls will issue department targets Departments may challenge assumptions Departments may submit additions for consideration Budget will be signed by Cognizant Owners 24 I.dentification of vent/Current ituation Raytheon contract P.O.B92914-20017 is out of funds on 5/19/96 and expires 6/30/96.A contract amendment to extend the contract expiration date to 8/30/96 was authorized, however, additional funding was not authorized on the amendment.
CORRECTIVE ACTIONS
Woik is currently being performed without authorized funds to cover the subject work.II.ack round 6/30/92 Contract issued for$57,000,000.00 to Raytheon Constructors, Inc.4/11/96 Projects determined there was not suQicient authorized funding in the contract to cover the SLl-14 outage and a contract extension would also be required since the contract termination date was 6/30/96 and the SLl-14 outage could still be in progress or just completed.
    +READJUSTED POWER SUPPLIES REWIRED ESFAS SA AND SB CABINETS PER DESIGN DOCUMENTATION
A Contract Change Order for$8,000,000.00 and contract extension to 9/30/96 was initiated.
  'LTHOUGH IT WAS DETERMINED THAT ESFAS WOULD PROPERLY FUNCTION IN THE AS FOUND CONFIGURATION.
4/18/96 CCO approved by the Site Services Manager.PSL Vice President identified need for cover letter and returned the CCO to the Site Services Manager.Budgets analyzed available funds, projected outage work, and new fund requirements.
    ~ PROVIDE GUIDANCE ON WHAT "ENERGIZE TO ACTUATE" MEANS.
Maintenance Manager reduced amount of new CCO to$5,000,000.
m 18
from$8,000,000., and shortened the contract extension date based on original scheduled outage scope and returned to Services Manager 5/19/96 Contract dollar limit reached on subject contract.5/22/96 Projects re-identified inadequate funding and Maintenance Budget or Maintenance Projects Resource Control generated a new CCO with reduced dollar amount ($5,000,000.00) sinceprevious CCO had pen and ink changes.DWA 0165340 R4 for$5,000,000.00 was initiated on 5/22/96 authorized by the Services Manager of 5/28/96.DWA also extended the expiration date to 8/30/96.5/23/96 Contract Amendment No.4 was initiated and approved by the Site Vice President to extend contract expiration date to 8/30/96.25 5/27/96 New CCO which added$5,000,000.00 approved by the Maintenance Manager 5/31/96 Approved by Resource Control Supervisor.
 
Rejected by Plant Manager because date on new CCO not correct in that it didn't show that the original CCO was initiated on 4/11/96.6/6/96 CCO returned to Resource Control Supervisor for revision to reflect appropriate dates.6/7/96 All PSI.Signatures obtained.Invoice for period 6/5 through 5/19 paid.Insufficient contract funding remaining to pay for work completed since 5/19/96.XQ.Xdentification of the Cau e s A.R C~Failure to follow procedure NP-1100 and established site policies regarding authorized contract funding.Failure of site organizations to process CCO in a timely manner or provide timely feedback to appropriate groups.B.'ntri uti actors~Failure of site to strictly enforce procedure NP1100 and established site requirements regarding authorized contract funding.~DWA on 5/22/96 applied to work already complete (through 5/19)and Rev 4 Amendment to contract without funding authorization.
                            ~ C     I P
V.Corrective Action 1.Review all other site contracts for similar occurrences, insufficient contract funding or contract authorization dates.Complete 2.Re-enforce NP-1100 policy/site requirements to ensure adequate control of contract authorization amounts.Complete 3.Due to increased outage and SG support, re-evaluate dollar amount to ensure adequate funding until new contract is awarded.Complete 4.Approve CCO for additional funding.5.Strengthen cost tracking for contracted work.0-26 OPERATXGNB f r r Annunciator response procedures Procedure upgrade prioritization Conf iguration management process changes EOOS procedure Surveillance tracking Equipment clearance Operations personnel performance 27 OPERATOR WORK AROUNDS Updated and Submitted by: OST-Fuiford MONTH Aug.95 Sep-95 Oct-95 Nov-95 Deo-95 Jan-98 Feb-96 Mar-98 APr-98 May-98 Jun.98 Jui.98 Aug.98 Sep.98 Oct-98 Nov-96 Dec-98 TARGET 45 OPEN 79 96 103 101 96 41 55 47 4e 48 43 37 43 40 38 32 38 30 20 18 17 18 15 120 operator ln performing duties within the approved procedures or In accordance with the Intended design.100-Decrease due to separation of OWAs from Operator Inconveniences.
RR ~ C
80 60~OPEN..0..TARGET 40.-Year End Target"-15 20 Aug-95 Oct-95 Dec-95 Feb-96 Apr-96 Jun-96, Aug-96 Oct-96 Dec-96 Time (Nlonth)
                              ~ ~ P
OPERATOR WORK AROUNDS WORKING LIST 0 pdated and Submitted by: OST FuifordNPWOI CR NO.96424111 9642<58 0-960091 PCM 017-196 63-2868 9&4817 9602-228 864356 634559 96-5386 9642-403 96434I68 9641718 9643448 9643-256 964 34I68 9643443 9642C00 9&03-255 9603477 9&0~14 DESCRIPTION UNIT-COMMON Pull-to-lock PCM defeats SIAS on ICW/CCW kcally RCGVS leak-Replace Unit 1 (V1441~)Lvl Cntrl Viva position iixficators destroyed during maint.UNIT 1 Lrg P p starts cause btry chrgr 8, instr buss to alarm Turbine latch pushbutton on RTGB is not operable Turbine turning gear anil not engage from control room L/D pressure control viva are notable to control press Spurious RTGB gmds have caused many annundators GEARS indicating wrong positionduring dwnpwr causing airm Rad mon pwr failure alarms frequently 1B fire Pp start causes battery chrgr to alarm SB 13306 is vibrating, this will enlarge keyway again~HP stub shaft has a bow, causing eccen to be beyond design Pressurizer code salties have leaked frequenfiy DEH filters do not remain full during normal ops.Vented 1/shit PCV-12-50 does not work according to procedure Auto-sync feature of DEH is Inadequate CST kep seal gets pushed out w/no fitl in progress.Alarms Annun"gland seal stm press hillo" comes in frequently Root cause of gas surge tk moisture trap failure Main generator vibration is approx 17 mila UNIT 2 DEPT MM PM IC'C IC IC IC IC IC JPN MM SCE SCE SCE SCE SCE STATUS NEED PMT NEED PMT SCHD NEED PMT NEED PMT NEED PMT SCHD SCHD NEED PMT SCHD NEED PMT NEED PMT NEED PMT NEED PMT NEED PMT NEED PMT NEED PMT SCHD NEED PMT NEED PMT NEED PMT SCHD START 3/1/96 4/29/96 4/29/96 4/29/96 4/29/96 5/1 5/96 4/1 5/96 4/29/96 4/29/96 4/29/96 4/29/96 4/29/96 4/29/96 4/29/96 4/29/96 SCHD COMPLETION 7/11/96'/30/96'/30/98 6/19/96 6/30/96'/1 5/96'0/1 5/96 7/30/96 6/31/96'/31/96 6/15/96'/6/96 6/1/96'/30/96'/30/96'/1/96 6/30/96'4/1/97 6/30/96'/30/96 6/15/96~23 960~64 PCM 086-292 9&03-702 PCM 251-295 96-1880 9602-287 9642'1 9643413 9643459 2A 8 2B D/G tachometer provide unreliable readings D/G pyrometers 8 thermocoupies have chronic loose conn.PC-11 kep 3 comm failure causes failure of audible alanna PCV4kh879 gland seal reg does control pressure SR-14350 lifted while testing CCW N hdr isolation vlvs V4111, iso fuel transfer tube, leaks by seat Restore PIA-1140 to original ccnfiguraticn when RCGVS is fixd V4217 Ls leaking by the seat causing the 2A2 Sl hdr to press.MFW Pp sucfion relief viva fail repeatedly Extraction stm trap bypass viva wig not dose e 100%pwr TIC-2223, UD TCV Is swinging causing L/D temp to be unstable'C Mh~MM SCE SCE SCE SCE NEED MRB SCHD SCHD SCHD NONE SCHD NONE SCHD SCHD SCHD SCHD 9/30/97 8/31/96 11/30/96 10/30/96 9/30/97 9/30/97 9/30/97 9/30/97 Work complete, waiting PMT 29 Man Rem 400 I 300 E 200 Unit 1 Refueling Outage Outage Budget=310 1=335.r~~~~~0 Pi A a+Target~Aalual 100-0 Jan Feb Mar Apr-May Jun Jul Aug Sept Oct Nov Dec Time (Month)Personnel Contamlnatlons 100 90 80 e 70.C 60 50 E 40 o 30 20 Unit 1 Refueling Outage~~e'er r fe e e e 92~..ge.g A Target~Aalual.10 0 r~~r r Jan Feb Mar Apr May Jun Jul Aug Sept Oct Nov Dec Time (Month)
~ C
ST.LUCIE PLANT CONTAMINATEO FLOOR SPACE 4500 4000 3500 3000 a 2500 ro 2000 8 1500.1000 500 lnrrcceeek48 elec fottowtng Benchmertdng with Turkey Poktl end keeping wkh industry precgcee.Post outage recovery of contaminated floor space.Unit 1 Refueling Outage~Aclual------Target Sep-Oct Nov Dec Jan-Feb Mar Apr May June Jul Aug Sept Oct Nov Dec 95 95 Time (month)
  ~ P                     ~ C
Unit 1 CPI (Chemistry Performance Index)Unit Shutdown For Refueling Outage 120 K EJ INPO GOAL~125 1.10"""DAILYCPI QTR AVG CPI I5I5mII5I5I/5flml151I5I5q<5555/55m 1.50 Unit 2 CPI (Chemistry Performance Index)INPO GOAL<1.25 1.10~~~~.~DAILY CPI~OTR AVG CPI I 5 I 5 5 I I 5 I I I 5 5 I 5 I (511m<f 5 5 5 I f 5 5 I 32 IMPROVEMENTS/ACTIONS r vement Pro Status Update:~Maintenance Procedure Upgrade Pmj ect Plant Material Condition (Key Performance Indicator):
        ~ 0 ~
~PWO Backlog (Power Block/Total)
              ~   ~
~Control Room Green Tags (C-Tags)~Aged PWOs (>12 months-Golden Oldies)~Leaks (Primary/Secondary)
C PJ   C   ~
~Temporary Leak Repairs Quarterly Quality Report~Quality by Crews 33 0-ST.LUCI T MAINTENANCE PROCEDU GRADE PROJECT TASK N;DEVELOP PROCEDURES/GUIDELINES FOR FREQUENTLY PERFORMED MAINTENANCE ACTIVITIES WHICH CURRENTLY EMPLOY THE USE OF VENDOR TECHNICAL MANUALS gG vis<2<<'.',j 1$,:y U<<t<AFAS~4"t3doiiiti,L'tuel?'o;c
 
,,d.kfb';<~/
team Generator P ugging Operation
t'oyYi&<i',-"y., ttc/l$.40021.: 0<::N4 t80504A'j.'4",8 I&C Spcrl Fuel Pit Levd Swyches 181/90 I&C Ash</oR Press Benches/8 f80 1&C Vers ega Cht Sdl<<fcators 681/90 I&C Mayeetrd Levd Swychcs 68180 I&C V2 Gen Atordo SSO Proc Monk<<6OMS I&C Rosemounl Transmktcrs 98080 I&C Setup Rod Drop C<<itrut<<98080 I&C V2 Gcn Alomtc GMMorftor 98080 I&C U2 GenAIonfc SSL Proc Monil 9808$i&C Ult U2Rcbuikln FCV-12 1 1081/90 I&C Ut Cot Coe Atoo/e Ooi.Iha SI.W&0M 108 1I98 I&C Ut Roil!ore OP Soli Alom Proc Mon 108180 I&C Bench Ca'ibra6on IIO080 I/,C CEDM CaMe Rcpdr 1 IO080'l&C Urft 2 LPM 1 IO080 I&C Ut t 2 Correl of Pros Mani Rdny 118088 I&C I 40006$: Add/few E<sf pment 681/90 MECH C<<6 Comp.Letdown Vhis/Ol/90 I&C Tcc lsohlcrs Calbreyon f28 f80 MECH Teiyd Rock Valves/O1/96 I&C OP-2 I 600029 I&C Procedure IOIRF MECH Hcreypran Valves 68 18S Mo>:ro i'o~%:t<fSCH~~>r~<N.
+ 157 Short Tube Stabilizers
~~4ywg.";I&C I&C Ul leldown U2GenAt<<dc Process Me<<tore PIG Proc Meri/OI80 tOI80 MECH WesSnghouse otrcs 98080 MECH eaton Hyrseutc Valves 108180 MECH/arne sbuy Valves 1IO080 I&C U2 Safcyuards Mdcrs Cel.128180 I&C IT'f Barton Hyd.Ash<slots tOll97 MECH Sory Warner Valves 68180.'I'Il'hts'FW',..>'.
+ 4 Long Tube Stabilizers
500I'u~~i~4 Ecg~<<'~>'g IOI/98 aWi honyeNbe>:>
+ 1021 Tubes Plugged in Steam Generator "A"
N.,"'dN'LLIS
+ 1060 Tubes Plugged in Steam Generator "B"
'i MECH Oraycn Valves MECH Ye<way Valves<9!i%4,4/OI80 g Fsb%>+)g@Mttlcg4%c
+ 2 Welded Plug Repairs
@wg'I2FA (Weft/I@IN'@JtlIIlfl<<9UII agley<<jtt'@g<<@AII+~1 MECH Dresser (Consofdctcdt 98080 8'tttt2/St&#xc3;<<
+ Corner Cover Plates Modifications for Plugging
MECH akor Eny Vdves 1001/90 NOSI0I00f-'.sn MECH Vetch tnc elves I IO080 rtshttt&~MECH 0 bp cmdl/ny PSL.2 Pte Sp d ed5e Procedures 1281/90 j'g)SSItlItITS@
+ Scheduled Finnish of Plugging Operations - 7/12/96
g<<'tdy'futt'8
+ Finished Plugging Operation on 7/5/96 0
'f%'SFGb' e
 
POWER BLOCK PWO BACKLOG Joe Marchese-Maintenance PWO Backlo-PWO backlog are non-outage corrective work orders (Work Type 5 status 22-48)on components/equipment in the power block.Total includes all Work Type 1, Work Type 3 8 Work Type 5.all hold codes 900 600 700 600 0 500 400 300 200 100 TOTAL=" 2056 Good a e s s s s s s~s a a a s a a a a s s s a a e e s a s a a as a s s s s s a t.end-tNT5~una1~Vntt 2~commort-X-Total Terrret Target e 350 Total 175 Mech 155 I&c 20 Hect Sep Oct Nov Dec Jan Feb Mar Apr May Jun Jul Aug Sep Oct Nov Dec'95'96 Date Data Source Passport  
Original Base Scope of Work
+3   Plenum Effort Dual Guide Tube during PAP Installation, than 4 Plenum Operation
+ 100%0 Bobbin Coil Testing
+ 100'/o Hot Leg MRPC
+ 20'lo Cold Leg MRPC
+ Inspection Schedule k PAP Installation - 15 Days
+ Steam Generator Work Started - 5/7/96
+ Completed Original Base Scope of Work - 5/18/96
+ Completed 3 Days Ahead of Schedule.
+ Includes 1 Day Delay for PAP Installation
 
Revise       Scope     of Wor
+ 100/0 Cold Leg MRPC
+ Diagnostic Testing Program
+ Limited Free Span Testing
+ 100/0 of P9 k 010 Support Plates
+ 100'/0 Free Span Testing
+ Extended Outage Duration from 5/19/96 - 6/26/96
+ Combinations of Inspection and Plugging Operations in progress. during this period.
+ Equipment Expansion - Platforms Modifications, dditional Genesis Equip:nt Added (10 Stations)-
I
 
team Generator C oseout Process
+ Missing (2) Short Stabilizers in Steam Generator "A" Transcription Error
+ Missing Hot Leg Plug in Steam Generator "B" Shift Supervisor Interpretation Error
 
LOSS OF BUDGET CONTROL Problems Encountered Poor contract administration practices Budget inadequate O.
Budget does not mirror site organization Budget disconnected from tracking Departments not familiar with approved budget Resource Controls Staff not independent Expectations not clear Enhanced Controls Contract Administration Enforcement of NP 1100 Authorization Matrix Discipline for Violations Eliminate "covenience contractors" Full time Phone Tech and Plumber Service agreements Good Practice - NC performed by PSL Maintenance Reduce Overtime Eliminate Exempt Overtime Confine Non Exempt overtime to LCO and,Techspec Eliminate Discretionary Spending Subscriptions, Painting, Tool Purchases Office Supplies, Luncheons, Consummables Budget Reconstitute 1996 08 M Budget
        $ 24 Million in budgeted funds for the balance of 1996 Must reduce to 'bare   bones'otal recovery is not possible New Process for 1997 MRB to determine Project Scope during budget cycle Resource Controls will issue department targets Departments may challenge assumptions Departments may submit additions for consideration Budget will be signed by Cognizant Owners 24
 
I. dentification of vent/Current       ituation Raytheon contract P.O. B92914-20017 is out of funds on 5/19/96 and expires 6/30/96.
A contract amendment to extend the contract expiration date to 8/30/96 was authorized, however, additional funding was not authorized on the amendment. Woik is currently being performed without authorized funds to cover the subject work.
II. ack round 6/30/92 Contract issued for $ 57,000,000.00 to Raytheon Constructors, Inc.
4/11/96 Projects determined there was not suQicient authorized funding in the contract to cover the SLl-14 outage and a contract extension would also be required since the contract termination date was 6/30/96 and the SLl-14 outage could still be in progress or just completed. A Contract Change Order for $ 8,000,000.00 and contract extension to 9/30/96 was initiated.
4/18/96 CCO approved by the Site Services Manager. PSL Vice President identified need for cover letter and returned the CCO to the Site Services Manager.
Budgets analyzed available funds, projected outage work, and new fund requirements. Maintenance Manager reduced amount of new CCO to
              $ 5,000,000. from $ 8,000,000., and shortened the contract extension date based on original scheduled outage scope and returned to Services Manager 5/19/96 Contract dollar limit reached on subject contract.
5/22/96 Projects re-identified inadequate funding and Maintenance Budget or Maintenance Projects Resource Control generated a new CCO with reduced dollar amount ($ 5,000,000.00) sinceprevious CCO had pen and ink changes.
DWA 0165340 R4 for $ 5,000,000.00 was initiated on 5/22/96 authorized by the Services Manager of 5/28/96. DWA also extended the expiration date to 8/30/96.
5/23/96 Contract Amendment No. 4 was initiated and approved by the Site Vice President to extend contract expiration date to 8/30/96.
25
 
5/27/96 New CCO which added $ 5,000,000.00 approved by the Maintenance Manager 5/31/96 Approved by Resource Control Supervisor. Rejected by Plant Manager because date on new CCO not correct in that it didn't show that the original CCO was initiated on 4/11/96.
6/6/96   CCO returned to Resource Control Supervisor for revision to reflect appropriate dates.
6/7/96   All PSI. Signatures obtained. Invoice for period 6/5 through 5/19 paid.
Insufficient contract funding remaining to pay for work completed since 5/19/96.
XQ. Xdentification of the Cau   e s A. R     C
        ~ Failure to follow procedure NP-1100 and established site policies regarding authorized contract funding.
Failure of site organizations to process CCO in a timely manner or provide timely feedback to appropriate groups.
B.'ntri uti         actors
        ~ Failure of site to strictly enforce procedure NP1100 and established site requirements regarding authorized contract funding.
        ~ DWA on 5/22/96 applied to work already complete (through 5/19) and Rev 4 Amendment to contract without funding authorization.
V. Corrective Action
: 1. Review all other site contracts for similar occurrences, insufficient contract funding or contract authorization dates. Complete
: 2. Re-enforce NP-1100 policy/site requirements to ensure adequate control of contract authorization amounts. Complete
: 3. Due to increased outage and SG support, re-evaluate dollar amount to ensure adequate funding until new contract is awarded. Complete
: 4. Approve CCO for additional funding.
: 5. Strengthen cost tracking for contracted work.
0-26
 
OPERATXGNB fr      r Annunciator response procedures Procedure upgrade prioritization Conf iguration management process changes EOOS procedure Surveillance tracking Equipment clearance Operations personnel performance 27
 
OPERATOR WORK AROUNDS Updated and Submitted by: OST - Fuiford MONTH Aug.95   Sep-95 Oct-95   Nov-95 Deo-95 Jan-98   Feb-96     Mar-98     APr-98   May-98     Jun.98     Jui.98   Aug.98   Sep.98   Oct-98 Nov-96     Dec-98 OPEN   79       96   103     101     96     41         55         47       43        37        38        32 TARGET                                          45        4e         48         43       40         38         30       20       18       17     18         15 120 operator ln performing duties within the approved procedures or In accordance with the Intended design.
100 Decrease   due to separation of OWAs from Operator Inconveniences.
80
                                                                                                                                          ~OPEN 60                                                                                                                        .. 0 ..TARGET 40 .-
Year End Target"-15 20 Aug-95     Oct-95     Dec-95     Feb-96         Apr-96         Jun-96,       Aug-96           Oct-96       Dec-96 Time (Nlonth)
 
OPERATOR WORK AROUNDS WORKING LIST                                       0 pdated and Submitted by: OST Fuiford NPWOI                                                                                            SCHD                  SCHD CR NO.                           DESCRIPTION                                    DEPT STATUS    START            COMPLETION UNIT - COMMON 96424111        Pull-to-lock PCM defeats SIAS on ICW/CCW kcally                        NEED PMT  3/1/96              7/11/96 9642<58              RCGVS leak- Replace Unit 1 (V1441~)                        MM    NEED PMT                                    '/30/96 0-960091      Lvl Cntrl Viva position iixficators destroyed during maint.       PM      SCHD                                        '/30/98 UNIT 1 PCM 017-196        Lrg P p starts cause btry chrgr 8, instr buss to alarm               NEED PMT                        6/19/96 63-2868        Turbine latch pushbutton on RTGB is not operable                 IC'C NEED PMT  4/29/96              6/30/96
                                                                                                                                        '/1 9&4817        Turbine turning gear anil not engage from control room                  NEED PMT  4/29/96                    5/96 5/96
                                                                                                                                        '0/1 9602-228      L/D pressure control viva are notable to control press            IC    SCHD    4/29/96 864356      Spurious RTGB gmds have caused many annundators                     IC    SCHD    4/29/96                7/30/96 634559    GEARS indicating wrong positionduring dwnpwr causing         airm     IC  NEED PMT  5/1 5/96              6/31/96 96-5386                Rad mon pwr failure alarms frequently                     IC    SCHD                                          '/31/96 9642-403            1B fire Pp start causes battery chrgr to alarm               IC  NEED PMT                        6/15/96 96434I68        SB 13306 is vibrating, this will enlarge keyway again   ~       JPN  NEED PMT  4/1 5/96                                '/6/96 9641718    HP stub shaft has a bow, causing eccen to be beyond design           MM    NEED PMT  4/29/96                6/1/96 9643448            Pressurizer code salties have leaked frequenfiy                     NEED PMT  4/29/96                        '/30/96 9643-256  DEH filters do not remain full during normal ops. Vented 1/shit             NEED PMT  4/29/96                                '/30/96 964 34I68        PCV-12-50 does not work according to procedure                       NEED PMT  4/29/96                                '/1/96 9643443                Auto-sync feature of DEH is Inadequate                   SCE  NEED PMT  4/29/96                6/30/96            '
9642C00    CST kep seal gets pushed out w/no fitl in progress. Alarms           SCE    SCHD                            4/1/97 9&03-255      Annun "gland seal stm press hillo" comes in frequently           SCE  NEED PMT  4/29/96                6/30/96 9603477            Root cause of gas surge tk moisture trap failure             SCE  NEED PMT  4/29/96                                    '/30/96 9&0~14                Main generator vibration is approx 17 mila                SCE   NEED PMT 4/29/96               6/15/96 UNIT 2
  ~23            2A 8 2B D/G tachometer provide unreliable readings                    NEED MRB 960~64      D/G pyrometers 8 thermocoupies have chronic loose conn.                      SCHD                          9/30/97 PCM 086-292    PC-11  kep 3 comm failure causes failure of audible alanna                  SCHD                          8/31/96 9&03-702        PCV4kh879 gland seal reg does control pressure                          SCHD                          11/30/96 PCM 251-295      SR-14350 lifted while testing CCW N hdr isolation vlvs            Mh~    NONE 96-1880 V4111, iso fuel transfer tube, leaks by seat Restore PIA-1140 to original ccnfiguraticn when RCGVS is fixd
                                                                                'C MM      SCHD NONE 10/30/96 9602-287  V4217  Ls leaking by the seat causing the 2A2 Sl hdr to press.      SCE    SCHD                           9/30/97 9642'1                MFW Pp sucfion relief viva fail repeatedly                SCE    SCHD                            9/30/97 9643413      Extraction stm trap bypass viva wig not dose    e 100% pwr        SCE    SCHD                            9/30/97 9643459  TIC-2223, UD TCV Is swinging causing L/D temp to be unstable          SCE    SCHD                            9/30/97 Work complete, waiting PMT 29
 
Man Rem 400 Unit 1 Refueling Outage                335.
I Outage Budget= 310                                      a+ r ~    ~ ~ ~~ 0 Pi  A 300 1 =
E Target 200
                                                                                                        ~Aalual 100-0 Mar            -            Jun      Jul            Sept  Oct    Nov  Dec Jan    Feb                Apr        May                      Aug Time (Month)
Personnel Contamlnatlons 100 Unit 1 Refueling Outage                        92 90 80 eC  70.                                                          ~..ge.g A 60 Target E
50 e'er  e  e  e
                                                                                                        ~Aalual 40                                ~   ~
o    30                                    r fe 20
    .10                                        r      ~ ~                                rr 0
Jan    Feb        Mar      Apr        May      Jun      Jul    Aug    Sept  Oct    Nov  Dec Time (Month)
 
ST. LUCIE PLANT CONTAMINATEOFLOOR SPACE 4500 4000 Post outage recovery of contaminated floor space.
                                                                                                                    ~Aclual
                                                                                                                    - - - - - -Target 3500 3000 a  2500 Unit 1 Refueling Outage ro 2000    lnrrcceeek48 elec 8          fottowtng 1500 . Benchmertdng with Turkey Poktl end 1000    keeping wkh industry precgcee.
500 Sep-      Oct        Nov  Dec    Jan-    Feb    Mar Apr    May  June Jul Aug      Sept    Oct    Nov Dec 95                                95 Time (month)
 
Unit 1 CPI (Chemistry Performance Index)
Unit Shutdown For Refueling Outage INPO GOAL ~
125 120 K
EJ 1.10
                                                                            """DAILYCPI QTR AVG CPI I5I5mII5I5I/5flml151I5I5q<5555/55m Unit 2 CPI (Chemistry Performance Index) 1.50 INPO GOAL <
1.25
                              ~
1.10                       ~
                                                                              ~ ~ . ~ DAILYCPI
                                                                              ~OTR AVG CPI I 5 I 5 5 I I 5 I I I 5 5 I 5 I ( 511m < f 5          5 5 I      I f5 5 32
 
IMPROVEMENTS/ACTIONS r     vement Pro                Status Update:
      ~     Maintenance Procedure Upgrade Pmj ect Plant Material Condition (Key Performance Indicator):
      ~
PWO Backlog (Power Block/Total)
      ~     Control Room Green Tags (C-Tags)
      ~
Aged PWOs (>12 months - Golden Oldies)
      ~      Leaks (Primary/Secondary)
      ~
Temporary Leak Repairs Quarterly Quality Report
      ~
Quality by Crews 33
 
0-ST. LUCI                      T MAINTENANCE            PROCEDU                        GRADE PROJECT TASK N; DEVELOP PROCEDURES/GUIDELINES FOR FREQUENTLY PERFORMED MAINTENANCEACTIVITIESWHICH CURRENTLY EMPLOY THE USE OF VENDOR TECHNICAL MANUALS gG vis<2<<'.',j 1$ ,:y U<<t<AFAS ~ 4 I&C                                I&C Rosemounl                          Bench t'oyYi&<i',-"y                                                                                                Transmktcrs                      Ca'ibra6on 98080                              IIO080 I&C            1&C              I&C            i&C                I/,C              I&C "t3doiiiti,L'tuel?'o;c                                                                              Spcrl Fuel Pit  Vers ega Cht      Setup Rod Drop Ult U2Rcbuikln      CEDM CaMe          I 40006$ : Add
                        ,,d.kfb';<~/        ., ttc/l$
0 <::N4
                                                      .40021.:                                                            Levd Swyches    Sdl<<fcators      C<<itrut<<      FCV-12  1         Rcpdr              /few E<sfpment t80504A'j.'4",8                            181/90          681/90            98080          1081/90              1 IO080          681/90 I&C              I&C            I&C                'l&C              MECH              MECH Mayeetrd          V2 Gcn Alomtc  Ut Cot Coe Atoo/e  Urft 2 LPM        C<<6 Comp.         Teiyd Rock Levd Swychcs          GMMorftor  Ooi. Iha SI.W&0M                      Letdown Vhis      Valves 68180            98080          108 1I98            1 IO080          /Ol/90            /O1/96 I&C            I&C              I&C            I&C                I&C                I&C                I&C                MECH Ash</oR          V2 Gen Atordo    U2 GenAIonfc  Ut Roil!ore OP Soli Ut  t 2 Correl of Tcc lsohlcrs      OP-2 I 600029      Hcreypran Press Benches  SSO Proc Monk<< SSL Proc Monil    Alom Proc Mon      Pros Mani Rdny    Calbreyon          I&C Procedure     Valves
                                                                                                                          /8 f80          6OMS              9808$          108180              118088            f28 f80            IOIRF              68 18S
                                                                                <fSCH~~>r~<N.                              I&C            I&C              MECH          MECH                MECH              I&C                I&C                MECH Mo>:ro i'o~%:t Ul leldown      U2GenAt<<dc        WesSnghouse      eaton Hyrseutc    /arne sbuy        U2 Safcyuards      IT'f Barton        Sory Warner Process Me<<tore PIG Proc Meri      otrcs        Valves              Valves            Mdcrs Cel.        Hyd. Ash<slots    Valves
                                                                                    ~~4ywg.";                             /OI80          tOI80            98080          108180              1IO080            128180            tOll97            68180 Ecg~<<'~>'g                                                                                        MECH            MECH              MECH          MECH                MECH              MECH Oraycn Valves  Ye<way Valves    Dresser        akor Eny          Vetch tnc          0    bp      cmdl/ny PSL.2 Pte d Sp ed5e Procedures
.'I'Il'hts'FW',..>'.                                                                                                                                        (Consofdctcdt  Vdves                  elves 500I'u~~i~4 IOI/98 honyeNbe>:>
aWi N.,"'dN'LLIS
                                      'i g    Fsb
                                                    <9!i%4,4
                                                            %>+) g@Mttlcg4%c @wg'
                                                                                                                          /OI80 I2FA (Weft/I @IN '@JtlIIlfl<<9UII agley<<jtt '@g <<@AII          +~1 98080 8 'tttt2/St&#xc3;<<
1001/90 NOSI0I00f-'.sn I IO080 rtshttt&~
1281/90 j'g)SSItlItITS@ g<<'tdy'futt'8 'f%'SFGb'
 
e POWER BLOCK PWO BACKLOG Joe Marchese - Maintenance PWO Backlo
                      - PWO backlog are non-outage corrective work orders (Work Type 5 status 22-48) on components/equipment in the power block. Total includes all Work Type 1, Work Type 3 8 Work Type 5.
all hold codes 900 600 700 TOTAL=" 2056 Good          ~  t.
                                                                                                                      ~una1
                                                                                                                      ~commort X
end - tNT5 Vntt 2 Total 600                                                                                                                            Terrret 0  500 400 a e s s s s s s  ~  s a a a s a a a a s s s a a e e s a s a a as a s s s s s a      Target e 350 Total 175 Mech 300                                                                                                                      155 I&c 20 Hect 200 100 Sep     Oct   Nov   Dec Jan   Feb Mar   Apr   May   Jun   Jul Aug Sep     Oct Nov Dec
                '95                         '96                     Date Data Source Passport


==SUMMARY==
==SUMMARY==
STATUS Discipline Mechanical Electrical I&C.ProJects Total Unit 1.47 10 93 152 Unit 2 91 95 198 Common 25 13 0 39 Total 163 22 201 389 CONTROL ROOM DEFICIENCIES C-TAGS Randy Olson-l&C~C.T8 S:-The number of Control Room/Board Green Tags.It provides an indicalion of the I attention given to maintaining control room instruments in an operable condition.
STATUS Discipline           Unit 1.      Unit 2        Common            Total Mechanical                 47          91                25              163 Electrical                 10                                            22 I&C                         93          95                13              201
80~70 80 ol 80 l c)40 0 2o 30 20~" OU'fiGh-7 davit""~H~oso I X Told" Non Odoeo TNeel 10~Moo Odoeo Togd os Sep Oct Nov Dec Jan Feb Mar Apr May Jun Jut Aug Sep Oct Nov Dec'95'98 Date Data: M.Vitae  
                    . ProJects                                                   0 Total                     152         198               39             389
 
CONTROL ROOM DEFICIENCIES C-TAGS Randy Olson - l&C
                ~C.T8 S:
                  - The number of Control Room/Board Green Tags. It provides an indicalion of the I
attention given to maintaining control room instruments in an operable condition.
80 ~                                                       " OU'fiGh-7 70                                                                                                    davit"" ~H~oso X   Told
                                                                                                                        " Non Odoeo TNeel ol 80 I
80 l
c)  40 0
2o  30 20 ~
10 ~
Moo Odoeo Togd os Sep     Oct   Nov   Dec   Jan     Feb   Mar   Apr   May     Jun Jut   Aug   Sep   Oct Nov Dec
              '95                         '98 Date Data: M. Vitae


==SUMMARY==
==SUMMARY==
STATUS Ready to Work or Workln Engineering/RTA AWP Other Holds Total Non-Outage 12 16 Outage Total 18 23 Oldest PWO&#xb9;Unit 1 10/17/94 0137 Unit 2 Discipline EM (OUTAGE)l&C (AGE)
STATUS Non-Outage                Outage                  Total Ready to Work 12                                          18 or Workln Engineering/RTA AWP Other Holds Total                             16                                           23 Unit 1                   Unit 2 Oldest                        10/17/94 PWO    &#xb9;                        0137 Discipline                 EM (OUTAGE)             l&C (     AGE)
AGED PWOs)12 M HS GOLDEN OLDIES e Joe March Maintenance P~Aed PWoe:-Non-outage corrective maintenance work type 1 and work type 5 PWOs older than 12 months.80 70 60 O 350>40 o 30 0 20 10 Work Type 1 Included Gbbtt Legend~una1~unll2~Common-X-Torsi-Te rect Target-.0 Sep Oct'95 Osis Source: Psedrort Nov Dec Jan Feb'96 Mar Apr May Jun Jul Aug Sep Oct Nov Dec Date SUMIIARY STATUS Unlt1 Unit 2 Common Total Mechanical Electrical 1&C Construction Total 20 10 33 26 10 20 57 Oldest PWO//Discipline 10/5/94 2546 ILC 5/12/95 4605 I&C 4/17/95 8676 I&C LEAKS N.Motley Leaks:-Active leaks (primary and secondary) 70 60 50 40 30 R 20 OUTAGE UNIT 1=OUTAGE UNIT 2=24's~~~Legend Good J~~Non.outage Non Outage Target 10 Non.Outage Target~10 0 Sep Oct Nov Dec Jan Feb'95'96 Mar Apr May Jun Jul Aug Sep Oct Nov Dec Date Data Source: Passport  
 
P e
AGED PWOs               ) 12 M               HS GOLDEN OLDIES Joe March       Maintenance
                  ~Aed PWoe:
                      - Non-outage corrective maintenance work type 1 and work type 5 PWOs older than 12 months.
80                                                                                                                   Legend 70                                                                                                       Gbbtt    ~una1
                                                                                                                        ~unll2 60                                                                                                                 ~Common O
350 Work Type   1 Included
 
                                                                                                                        -X-Torsi Te rect
>40 o 30 0
20 Target .0 10 Sep     Oct   Nov   Dec     Jan   Feb     Mar   Apr     May   Jun     Jul   Aug Sep     Oct Nov     Dec
                  '95                          '96                      Date Osis Source: Psedrort SUMIIARYSTATUS Unlt1         Unit 2         Common               Total Mechanical                 20                                                26 Electrical                                                                   10 1&C                       10                                                20 Construction Total                     33                                               57 Oldest                 10/5/94       5/12/95         4/17/95 PWO //                  2546          4605              8676 Discipline              ILC            I&C              I&C
 
LEAKS N. Motley Leaks:
~
                    - Active leaks (primary and secondary) 70 OUTAGE                                    Legend 60                                                     UNIT 1 OUTAGE UNIT 2 = 24
                                                                        =
Good Non.outage 50                                                                                                                  Non Outage Target J
40
                                                    's    ~  ~      ~
30 R
20 10                                                                                                         Non.Outage Target ~ 10 0
Sep     Oct   Nov   Dec     Jan     Feb     Mar   Apr   May   Jun   Jul Aug Sep Oct Nov Dec
              '95                          '96 Date Data Source: Passport


==SUMMARY==
==SUMMARY==
STATUS Unit 1 Unit 2 Total Non-Outage OUTAGE Oldest (Non-Outage)
STATUS Unit 1         Unit 2           Total Non-Outage                       OUTAGE Oldest (Non-Outage)               2/13/95         3/17/95 PWO //                              5224            2832 Status                            READY.            ENG
PWO//Status 2/13/95 5224 READY.3/17/95 2832 ENG LEAK REPAI FITTINGS Neal y Leak Re airs: Leaks that have been temporarily repaired.55 50 45 Le 40 n.35" 30 25 0 20 0 z 15 10 5 0 1.egend-ood G I~Unit1~Unit 2 Sep Oct Nov Dec Jan Feb Mar Apr May Jun Jul Aug Sep Oct Nov Dec'95'96 Date Oata Sovrce: Nell Motley  
 
LEAK REPAI                 FITTINGS Neal     y Leak Re airs:
Leaks that have been temporarily repaired.
55                                                                                                   1.egend-50                                                                                       G ood Le 45 40                                                                                           I      ~
                                                                                                          ~Unit1 Unit 2
: n. 35
"   30 25 0 20 0
z   15 10 5
0 Sep     Oct   Nov   Dec   Jan     Feb Mar   Apr   May Jun     Jul Aug Sep Oct Nov   Dec
                '95                             '96                   Date Oata Sovrce: Nell Motley


==SUMMARY==
==SUMMARY==
STATUS Unit 1 Unit 2 Total Total OUTAGE 10 10 Page 13 ANNUNCIATORS Randy Olson Annunciators:
STATUS Unit 1       Unit 2         Total Total                   OUTAGE           10             10 Page 13
-Annunciators in alarm state.PSL has a darkboard concept, which means any annunciator in the alarm state is unacceptable.
 
14 12 10 0 g s r C 6 0 0 R 4 Good Legend~Vnit 1.~Vnit2-Target Target=0 Sep Oct'95 Nov Dec Jan Feb Mar Apr May Jun Jul Aug Sep.Oct Nov.Dec'96 Date Data Source: R.J.Davis (OM)Unit 1=OutageUnit2=3 614/16Aux Feed Pum 2C, LPM age 10 10 QUALITY FEEDBACK BY CREWS GRAPH REFLECTS 41 CR'S INITIATED BY QAIQC CONTAINING 43 ISSUES I-8 K 0 Q.K 6 R 0 l-Cl 4 R 0 O 0 2 0 VALVES WELDING I&C PROJECTS VENDOR OST'OTATING EM QC HP OTHER (MOTLEY)(JACOBS)(OLSON)(FRECHETTE)(FULFORD)(ENGLISH)(KORTE)(BLADOW)(McCULLERS)
ANNUNCIATORS Randy Olson Annunciators:
~NMM~ISI~JPN~SCE CREWS  
          - Annunciators in alarm state. PSL has a darkboard concept, which means any annunciator in the alarm state is unacceptable.
~.0-I DISTRIBUTION OF QUALITY ISSUES 13 12~10 Q R~s K D Q Q 6 0 0 4 0 PROCEDURE WORK PRACTICES PAPER PROBLEMS PERSONAL ERRORS CONFIGURATION EQUIPMENT DEFECTS OTHER NON-COMPLIANCE (NPWO/JWR)
14 Legend 12 Good          ~    Vnit 1 0
~CHEMICAL CONTROL~TESTING~FME/HOUSEKEEPING
10                                                                                         .
~PROCEDURES
 
*o MATERIAL CONTROL TITLE OF ISSUES e e SIGNIFICANCE OF QUALITY ISSUES 2520 21 0)~<5 0)0)kL 0 10 14 SlGN(FlCANT VERY SlGNtFlCANT EXTREMELY SlGNlFlCANT
                                                                                                ~Vnit2 Target g   s r
~NPWO CLOSEOUTIREVIEWS
C 6
~JWR'WORK PRACTICES'POOR PROCESSES~Hl-LITERS ON PAPER~EXISTING CONDITIONS
0 0
'LOST PAPER'TESTING'CHEMICAL CONTROL PROGRAM'DEFECTIVE EQUIPMENT/MATERIAL
R   4 Target = 0 Sep     Oct   Nov   Dec   Jan Feb Mar   Apr     May Jun Jul Aug Sep . Oct   Nov . Dec
~MATERIAL CONTROL~WORK PRACTICES~REWORK~INADEQUATE PROCEDURES
              '95                          '96 Date Data Source: R.J. Davis (OM)
;,FME.+PROCEDURE NON-COMPLIANCE
Unit 1 = Outage Unit2 =3     614/16Aux Feed Pum 2C, LPM age 10
'PERSONAL ERRORS'CONFIGURATION ISSUES SEVERITY OF ISSUES  
 
~.-  
QUALITYFEEDBACK BY CREWS 10 GRAPH REFLECTS 41 CR'S INITIATEDBY QAIQC CONTAINING 43 ISSUES I-   8 K
.IMPROVEMENTS/ACTIONS r vement Improve Configuration Management Controls: Reduce Open TSAs Reduce Age of Oldest PCMs SLl-14 Outl~Scope PCMs CR&#xb9;CRs PMAI's 81 311 3SO 74 Nuclear Instrumentation S/G Tube Plugging License Amendment and Operating Evaluations enforcement Conference issues TEMPORARY SYSTEM ALTERATlONS TSA Kris Mohindroo-Engineering 50 45 40 35 30 v-25 I-0 20 15 10 Good Legend~unit 1~unlt2-X-Total---Target-Target tg"-.-..~Oct Dec Feb Apr Jun Date Aug Oct Dec Data Source: Kris hlohlndroo
0Q.
K   6 R
0 l-Cl 4 R
0O 0   2 0
VALVES WELDING     I&C   PROJECTS VENDOR     OST 'OTATING     EM       QC       HP     OTHER (FULFORD) (ENGLISH) (KORTE) (BLADOW)(McCULLERS) ~ NMM (MOTLEY) (JACOBS) (OLSON) (FRECHETTE)
                                                                                                    ~ ISI
                                                                                                    ~ JPN
                                                                                                    ~ SCE CREWS
 
~ .
0-
 
I DISTRIBUTION OF QUALITYISSUES 13 12
~ 10 Q
R
~ s K
D Q
Q 6 0
0 4 0                                                               CONFIGURATION EQUIPMENT DEFECTS  OTHER PROCEDURE     WORK PRACTICES PAPER PROBLEMS PERSONAL ERRORS
                                                                                                    ~ CHEMICALCONTROL NON-COMPLIANCE               (NPWO/JWR)
                                                                                                    ~ TESTING
                                                                                                    ~ FME/HOUSEKEEPING
                                                                                                    ~ PROCEDURES
* o MATERIALCONTROL TITLE OF ISSUES
 
e e
 
SIGNIFICANCE OF QUALITYISSUES 25 21 20 0)
~ <5                                     14 0) 0)
kL 0 10 SlGN(FlCANT         VERY SlGNtFlCANT   EXTREMELY SlGNlFlCANT
      ~ NPWO CLOSEOUTIREVIEWS 'LOST PAPER               'TESTING
      ~ JWR                    'CHEMICALCONTROL PROGRAM   'DEFECTIVE EQUIPMENT/MATERIAL
      'WORK PRACTICES          ~ MATERIALCONTROL          ~ WORK PRACTICES
      'POOR PROCESSES          ~ REWORK
      ~ Hl-LITERS ON PAPER    ~ INADEQUATE PROCEDURES
      ~ EXISTING CONDITIONS    ;,FME
                              .+PROCEDURE NON-COMPLIANCE
                              'PERSONAL ERRORS
                              'CONFIGURATION ISSUES SEVERITY OF ISSUES
 
~ .
-
 
IMPROVEMENTS/ACTIONS
.
r     vement Improve Configuration Management Controls:
Reduce Open TSAs Reduce Age of Oldest PCMs SLl-14 Outl~ Scope PCMs         81 CR&#xb9;           311 CRs           3SO PMAI's       74 Nuclear Instrumentation S/G Tube Plugging License Amendment and Operating Evaluations enforcement Conference issues
 
TEMPORARY SYSTEM ALTERATlONS TSA Kris Mohindroo - Engineering 50                                                                           Good           Legend 45                                                                                      ~unit         1
                                                                                              ~unlt2 40                                                                                      X 35                                                                                      ---     Total Target 30 I-v- 25 0
20                                                                                - Target   tg" -. - .. ~
15 10 Oct         Dec Feb       Apr     Jun       Aug   Oct   Dec Date Data Source: Kris hlohlndroo


==SUMMARY==
==SUMMARY==
STATUS Dlscl line Mechanical Electrical ILC En lneerln 0 eratlons Health Ph slcs Construction Preventive Malnt SCE Total Unit 1 Unit 2 Total 14 Oldest TSA Disci line 11/17/95 1&C&C~~
STATUS Dlscl line     Unit 1          Unit 2        Total Mechanical Electrical ILC                                                   14 En lneerln 0 eratlons Health Ph slcs Construction Preventive Malnt SCE Total Oldest TSA           11/17/95 Disci line              1&C               &C                                           ~ ~
PLANT CHANGE/MODIFICATIONS Kris Mohindroo-Engineering 150 Good Legend 125~100 75 0 50~~~~~~Open PCIM Target"-80~untt1~unit2~Common-X-Total---Target 25 Oct Dec Feb Apr Jun Date Aug Oct Dec Data Source: Kris Mohlndroo SUNIMARY STATIjS-WORKING Disci line 0 enPCIM PC/Ms)24 Mo.Unit 1 109 Unit 2 18 Common Total 132 12 ST.LUCIE PLANT-10 OLDEST OPEN PC/M's-PC/M NUMBER 193-189 042-289 335-190 097-191 171-191 186-191 295-191 086-292 203-192 DESCRIPTION I Open Blowdown Cooling Water Heat Exchanger Vacuum Breaker Valve Changeout Instrument u de installation of Conduit Seals Check Valve Hinge Pin and Bonnet Modifications on CCW pump discharge check valves V14143, V14147 and V14151 FOP 55GL1154 Power Supply Repl Resizing and replacement of MOV Thermal Overload Devices on 137 MOV's Intake Cooling Water Support Modifications RCP Vibration Probes Relocation Radiation Monitoring Computer Replaccmcnt Replacement of 95 Sigma Meters in the Control Room and Hot Shutdown Panel do to obsolesence issues.3/21/89 3/23/89 7/18/91-4/13/93-Siip 0 Sup 0 3/25/93-4/13/93-Sup I Sup I 7/19/91 8/9/94 7/17/91 9/19/91 7/I/92-Su I Not FRG'd 10/18/91 4/27/93 4/22/92 5/7/92 12/21/92 4/6/93 DATE DATE ISSUED FRG'D 2/I I/89 12/I I/89 SCH CLOSE DATE UNIT I OUTAGE UNIT I OUTAGE UNIT I OUTAGE UNIT I OUTAGE STATUS AND ACTIONS REQUIRED TO CLOSE PC/M implemented.
 
Action plan to resolve slight periodic leakage problems with permanent drain catcher.Engr CRN issued for implementation.
PLANT CHANGE/MODIFICATIONS Kris Mohindroo - Engineering 150 Good           Legend
PC/M implemented on valves V14147 and V14151.Modifications to V14143 planned for next refueling outage.Will close PC/M upon'ompletion of the work activity PC/M implemented on 122 valves.15 valves remaining to be modified.EM needs to schedule remaining work.Will close PC/M upon completion of the work activity Sup 0 Complete.Sup.I was budget approved at the MRB I/30/96 for im lementationduringthe 1996Unit I outa e.PC/M implemented.
                                                                                                      ~untt1 125
ICM has one PWO associated with two remaining CRN's which is required to be worked to close the PC/M.Will close PC/M upon completion of the work activity.PC/M partially implemented with 15 instruments installed.
  ~ 100
Recommend as-building what work has been completed and close PC/M.New PC/M's can then be generated based on planned work activities.
                                                                                                      ~
282-192 Anchor Darling Replacement 3/25/93-Supp 0 10/8/93-Supp I 2/9/95-Supp 2 4/I/93-Supp 0 10/26/93 Supp I 2/23/95-Supp 2 PC/M issued as an As-Required (ARP)CRN's are being issue as needed.
                                                                                                      ~unit2 X
I1MPROVEMXNTS/ACTIONS Ma or Im rovements Areas'utage Material Performance Amount of outage material ordered but not used Reduce on Site Inventory-a)38 million by year end, b)review and remove 1995 already written off DME material on site (See next page)Increase Spare Parts Availability:
Common Total Target 75                                    ~    ~  ~ ~ ~ ~
~Maintain non-outage restocks to less than 500 (1%)~Maintain non-outage AWP PWO's to less than 70~Maintain the number of 30 day old PO's to less than 20 Address Equipment Differences Between Units and its Effect on Inventory stat719 48 Reduce on Site Inventory:
Open PCIM 0                                                                                        "
a)38 million by year end, b)review and remove 1995 already written off DME material on site.QTATQ$: 19 million of DME was on site January 1, 1996 14.5 million was sold at auction Approximately 4 million leA.of 1995 DME to review and return to inventory, or remove&om site (only PC 1 and 2 items)LA/HED Finish review of remaining 1995 DME by November 30th.In coincidence with above, remove material not to be returned to inventory December 15th (options;auction, consignment, FPL resources, commission contractor)
Target -80 50 25 Oct      Dec  Feb      Apr        Jun      Aug    Oct         Dec Date Data Source: Kris Mohlndroo SUNIMARY STATIjS-WORKING Disci line     Unit 1            Unit 2          Common            Total 0 enPCIM           109                18                                  132 PC/Ms )24 Mo.                                                               12
Potentjta 1996 DME funding shortage (current inventory 41.2 million, DME available 2.2 million, 1 million delta to get to 38 million)a)ICW pump rebuilds'b)RCP seals-N9000 design c)Capitalize turbine valves like PTN Overmax currently at 4.4 million a)Numerous small examples Budget for 1997 DME (2 million needed to go&om 38 to 36 million)Establish 1997 outage"contingency fund" by and implement"you order it you pay for it" policy by September 1, 1996.LAR/aa019a 49
 
~'NVENTORY VALUE Dan Quilty-Nuclear Materials Management 60 Good 50 ro r 0>~0 L 0$0 O 30 41.3 Target=38 20 Oct Dec Feb Apr Jun Date Aug Oct Dec Data Source: Norman Quesada Nuclear Materials Management WAREHOUSE RESTOCKS 3000 2500 N 2000 1500 3 1000 500 0 1066~Aalaal-----Target Jan Feb Mar Apr May June July Aug Sept Oct Nov Dec Date OVERMAX INVENTORY VALUE 5 C7 o 4 CI I 3 CO 1 r~..r.,~r~..-~4.4 W%%%H u%R aa--5-Actual" Target Jan Feb Mar Apr May June July Aug Sept Oct Nov Dec Date Nuclear Materials nagementOPEN REQUISITIONS OVER 30 DAYS 250 200 c 0 N 150 100 C 50 0 aa H w H aa 0%aa w p aa w w 12 aa%%aa%H%H H W W W aa H aa H%W%H a H H W W H~Aclual Target Jan Feb Mar Apr May June Date July Aug Sept Oct Ncv Dec NON-OUTAGE AWP (STATUS 46&48)200 180 160 140 e 120 100 80 60 40 20 0 4 C'a aa aa aa aa aa a aa aa aa aa aa aa aa aa aa aa aa e aa aa aa aa aa w aa aa aa aa aa a aa w aa w a aa a a aa aa aa aa~Aclual" Target Good Jan Feb Mar Apr May June July Aug Sept Date Oct Ncv Dec
ST. LUCIE PLANT - 10 OLDEST OPEN PC/M's SCH
~~e 0 0-
 
~~, IMPROVEMENTS/ACTIONS r vement: Improve Procedure Quality and Revision Process: Temporary Change Reduction Convert Non-safety Procedures to Guidelines
PC/M                                                       DATE    DATE DESCRIPTION                                          CLOSE          STATUS AND ACTIONS REQUIRED TO CLOSE NUMBER                                                     ISSUED    FRG'D I                                        DATE 193-189 Open Blowdown Cooling Water Heat Exchanger        2/I I/89 12/I I/89        PC/M implemented. Action plan to resolve slight periodic leakage Vacuum Breaker Valve Changeout                                               problems with permanent drain catcher. Engr CRN issued for implementation.
~Monitor Quality of Upgmded OPS/Maintenance Procedures Improve the Safety Focus of the FRG:~Improve consistency and membership
042-289 Instrument u     de installation of Conduit Seals 3/21/89  3/23/89 335-190 Check Valve Hinge Pin and Bonnet Modifications     7/18/91- 4/13/93-  UNIT I PC/M implemented on valves V14147 and V14151. Modifications to on CCW pump discharge check valves V14143,          Siip 0  Sup 0  OUTAGE V14143 planned for next refueling outage. Willclose PC/M upon V14147 and V14151                                  3/25/93- 4/13/93-                      of the work activity                                'ompletion Sup I    Sup I 097-191 FOP 55GL1154 Power Supply Repl                    7/19/91    8/9/94  UNIT I OUTAGE 171-191 Resizing and replacement of MOV Thermal            7/17/91   9/19/91  UNIT I PC/M implemented on 122 valves. 15 valves remaining to be modified.
~.Reduce Volume Tech Spec Admin Section Change Improve Plant's ability to Implement E-Plan~Upgmde/Revs the ERO~Implement more&xpent;limited scope drills~Enhance EP Training Implement Revised Configuration Control Process~Configuration Management Enforcement Conference Preps~Establish Configuration Control Group/mission/process
Overload Devices on 137 MOV's                                        OUTAGE EM needs to schedule remaining work. Willclose PC/M upon completion of the work activity 186-191 Intake Cooling Water Support Modifications        7/I/92-     Not    UNIT I Sup 0 Complete. Sup. I was budget approved at the MRB I/30/96 for Su I   FRG'd   OUTAGE im lementationduringthe 1996Unit I outa e.
~Revise design control procedures
295-191 RCP Vibration Probes Relocation                    10/18/91 4/27/93 086-292 Radiation Monitoring Computer Replaccmcnt          4/22/92   5/7/92         PC/M implemented. ICM has one PWO associated with two remaining CRN's which is required to be worked to close the PC/M. Willclose PC/M upon completion of the work activity.
~-Initiate RTSI.for minor mods~Identify Unit 2 Outage Top 20%ork Items Improve Site Training Integrate outside perspective into organization 1'levate Training Standards/Reinforcement Establish Method to determine Training Effectiveness Complete Corrrplete Complete Complete On-gong 12/31/96 8/30/96 9/30/96 12/1/96 7/26/96 Complete 8/15/96 Complete Complete Complete'n-gourg 7/31/96 53 TEMPORARY CHANGES TO PROCEDURES Jim Holt-Information Services 350 300 250 O~200 0 0 150 X 100 Good Legend~Untt 1~Unit 2~common-X-Total---Target 50 Oct Dec Feb Apr Jun Date Aug Oct Dec Data Source: Jtm Holt  
203-192 Replacement of 95 Sigma Meters in the Control      12/21/92  4/6/93          PC/M partially implemented with 15 instruments installed. Recommend Room and Hot Shutdown Panel do to obsolesence                                as-building what work has been completed and close PC/M. New issues.                                                                      PC/M's can then be generated based on planned work activities.
282-192 Anchor Darling Replacement                        3/25/93-  4/I/93-          PC/M issued as an As - Required (ARP) CRN's are being issue as Supp 0  Supp 0           needed.
10/8/93-  10/26/93 Supp I   Supp I 2/9/95- 2/23/95-Supp 2  Supp 2
 
I1MPROVEMXNTS/ACTIONS Ma or Im rovements Areas
'utage    Material Performance Amount of outage material ordered but not used Reduce on Site Inventory - a)38 million by year end, b)review and remove 1995 already written offDME material on site (See next page)
Increase Spare Parts Availability:
  ~      Maintain non-outage restocks to less than 500 (1%)
  ~      Maintain non-outage AWP PWO's to less than 70
  ~      Maintain the number of 30 day old PO's to less than 20 Address Equipment Differences Between Units and its Effect on Inventory stat719 48
 
Reduce on Site Inventory: a) 38 million by year end, b)review and remove 1995 already written offDME material on site.
QTATQ$ :
19  million of DME was on site January    1, 1996 14.5  million was sold at auction Approximately 4 million leA. of 1995 DME to review and return to inventory, or remove &om site (only PC 1 and 2 items)
LA /      HED Finish review of remaining 1995 DME by November 30th.
In coincidence with above, remove material not to be returned to inventory December 15th (options; auction, consignment, FPL resources, commission contractor)
Potentjta 1996 DME funding shortage (current inventory 41.2 million, DME available 2.2 million, 1 million delta to get to 38 million) a)ICW pump rebuilds
                'b)RCP seals - N9000 design c)Capitalize turbine valves like PTN Overmax currently at 4.4 million a)Numerous small examples Budget for 1997 DME (2 million needed to go &om 38 to 36 million)
Establish 1997 outage "contingency fund" by and implement "you order      it you pay for it" policy by September 1, 1996.
LAR/aa019a 49
 
~
            'NVENTORYVALUE Dan Quilty - Nuclear Materials Management 60 Good 50 ro                                                            41.3 r
0
>~0 L
0$                                                                          Target = 38 0
O 30 20 Oct    Dec    Feb        Apr        Jun      Aug  Oct            Dec Date Data Source: Norman Quesada
 
Nuclear Materials Management WAREHOUSE RESTOCKS 3000 2500 N  2000
                                                                                                ~Aalaal
                                                                                                ----- Target 1500 1066 3    1000 500 0
Jan    Feb    Mar      Apr        May    June          July  Aug  Sept Oct Nov Dec Date OVERMAX INVENTORYVALUE 5
                                            ..r.,
                              ..- ~ ~ r
                                        ~
C7                                                        4.4 o
CI 4                                                                                            - Actual I                                                                                                    " Target 3
r ~
W  %  %  %  H  u %  R aa CO 1
Jan      Feb    Mar      Apr        May    June          July  Aug  Sept  Oct Nov Dec Date
 
Nuclear Materials                                         nagement OPEN REQUISITIONS OVER 30 DAYS 250 c  200 0
N  150                                                                                                                                                                            ~Aclual Target 100 C
12 50 aa  H w      H  aa  0      %  aa  w  p  aa  w w          aa  %  %    aa    %  H %    H  H  W  W  W  aa  H  aa  H %  W  %  H  a H H W W      H 0
Jan             Feb             Mar             Apr             May           June               July         Aug             Sept         Oct         Ncv        Dec Date NON-OUTAGE AWP (STATUS 46 & 48) 200 180 160 e
140 120 4 C'a                                                                                ~Aclual
                                                                                                                                                                                      " Target 100 80                                                                            e                                                a                a      a a aa  aa  aa  aa  aa  a  aa  aa  aa  aa aa  aa  aa  aa aa  aa aa      aa  aa    aa  aa  aa  w  aa  aa  aa  aa aa     aa   w aa w     aa      aa aa aa aa 60 Good 40 20 0
Jan              Feb              Mar             Apr           May           June               July           Aug             Sept         Oct       Ncv           Dec Date
 
~ ~
e 0
0-
 
  ~ ~
IMPROVEMENTS/ACTIONS
,
r      vement Improve Procedure Quality and Revision Process:
Temporary Change Reduction                              Complete Convert Non-safety Procedures to Guidelines            Corrrplete
            ~      Monitor Quality of Upgmded OPS/Maintenance Procedures  Complete Improve the Safety Focus    of the FRG:
            ~      Improve consistency and membership                      Complete
            ~. Reduce Volume                                          On-gong Tech Spec Admin Section Change                          12/31/96 Improve Plant's ability to Implement E-Plan
            ~     Upgmde/Revs the ERO                                      8/30/96
            ~       Implement more &xpent; limited scope drills            9/30/96
            ~       Enhance EP Training                                    12/1/96 Implement Revised Configuration Control Process
              ~
Configuration Management Enforcement Conference Preps  7/26/96
              ~       Establish Configuration Control Group/mission/process Complete
              ~       Revise design control procedures                      8/15/96
              ~   - Initiate RTSI. for minor mods                          Complete
              ~       Identify Unit 2 Outage Top 20 %ork Items              Complete Improve Site Training Integrate outside perspective into organization      Complete 1
                  'levate
:                              Training Standards/Reinforcement                        'n-gourg Establish Method to determine Training Effectiveness  7/31/96 53
 
TEMPORARY CHANGES TO PROCEDURES Jim Holt - Information Services 350 Legend Good
                                                                                                  ~Untt        1
                                                                                                  ~Unit2
 
300
                                                                                                  ~common 250                                                                                        X    Total Target O~  200 0
0 150 X
100 50 Oct        Dec      Feb        Apr          Jun      Aug  Oct       Dec Date Data Source: Jtm Holt


==SUMMARY==
==SUMMARY==
STATUS Oldest TC (days)27 26 26 27 0 0.Discipline 0 erations Mechanical Electrical I&C Reactor En.SCE HP Unit 1 0 0 0 Unit 2 0 0 0 0 0 0 Common 0 0 0 0 0 Total 0 0 0 PSL TRAINING OBSERVATIONS 100%%d 904%%d80/o 70%%d g 60%%d g So%%d 4o%%d 30%~Actual 20/a 10%%d 0%%d g~~i P19S1V+992; QS93;@99~4 51995,i 5~%R2/963~~Q/96K g$96T-6/96~;7/966~~q xhl96~rio/96',81/96-f52/96-OA~WctM~Data Source: M.Allen 100%85%0%2%S5%100%100%91%55 t~O.0 0-s~~~.CO CTIVE ACTION PROG  
STATUS Oldest TC                                               Unit 1            Unit 2    Common                Total Discipline (days) 27             0  erations 26             Mechanical                                            0            0 26             Electrical                                            0             0 27            I&C                                                   0 0            Reactor En   .                     0                 0             0                   0 SCE                                  0                 0             0                   0
, CONDITION REPORT PROCESS STATUS*VOLUME CONTINUES TO BE HIGH CR's GENERATED BY QUARTER 1500 1000 O o 50%h 1ST QTR 95 2nd QTR 3'TR 401 QTR 1st QTR 96 2nd QTR TOP SOURCES FOR 2ND QUARTER OPERATIONS QUALITY ASSURANCE ENGINEERING IC" SIGNIFICANT CRs REVIEWED AT 0730 MANAGEMENT MEETING, ALL CRs APPROVED BY PGM*2ND QUARTER TREND REPORT DRAFT ISSUE JULY 26 MANAGEMENT REVIEW-AUGUST 7 PRESENT TO NRC AUGUST 29*AREAS FOR IMPROVEMENT
: 0.          HP                                  0                 0             0                   0
-CORRECTIVE ACTION PROGRAM:-REVIEW OF COMPLETED CRs SHOW INCONSISTENT LEVEL OF ROOT CAUSE-BETTER TIE WITH ROOT CAUSE PROCEDURE (LEVELS Of ROOT CAUSE TIED TO SIGNIFICANCE OF PROBLEM)-MORE WIDESPREAD TRAINING NEEDED ON PROCEDURE/PIC HANDBOOK-PROBLEM REPORT TIMELINESS 56  
 
~J.:  
PSL TRAINING OBSERVATIONS 100%%d 904%%d 80/o
~OVERALL ASSESSMENT Corrective actions is considered a limiting weakness and rcxruires increased management attention Personnel errors, attention to detail and procedural adherence are continuing problems'Ihe operating expeoence feedback program (OEF)and the foreign material exclusion program (FME)are unsatisfactory
                                                                                              ~Actual 70%%d g   60%%d g   So%%d 4o%%d 30%
.Our inability to curb the trend of recurring problems is indicative of ineffective correchve actions and less than adequate when determining underlying causal factors QA AUDITS/PERFORMANCE MONITORING (AUGMENTED BY IB/PSL QA/QC PERSONNEL)
20/a 10%%d 0%%d g~~i P19S1V+992; QS93; @99~4 51995,i 5~% R2/963 ~~ Q/96K g$ 96T -6/96~; 7/966 ~~q xhl96~ rio/96',81/96- f52/96-OA~WctM~                       100% 85%     0% 2%     S5% 100% 100%   91%
Second quarter 96: 7 Audits, 25 Finding, 80 Condition Reports Programs and Procedures are not sufEcient to preclude problems fern occurring (Procedure Quality)Procedures are not being followed with rigor (Human Performance) 13 Finding Responses late to QA.Process change with VP sign off Rejected-by Site VP due to shallowness of response~INDEPENDENT TECHNICAL REVIEWS Second quarter'96: 7 ITRs, 38 Recommendations, 11 Condition Reports-Conduct of Operations acceptable, however, inconsistencies exist between crews 57 QUAIXIY ASSURANCE (continued)
Data Source: M. Allen 55
O.OEF program is not effective in reducing severity and renurence of events PME programmatic controls have improved, however, cultural and personnel behavior changes are requned to achieve desired results QC INSPECIIONS/SURVEKLANCES Second quarter deficiencies rate 7.5%down Rom 8%1st quarter'96 1363 surveillance/inspections with 102 deficiencies (most outage related), 71 Condition Reports Use of template and underwater repair methodologies for Rx vessel Qange resulted in major man-rem and budget savings0-58  
 
.\l r.zcmsING C:
t ~
n ,~O.0-REGULATORY COMPLIANCE STATUS and AGENDA Recent NIRC lns ections as of June 30$996 RESIDENTS'ERIODIC:
O.
3-30-96 through 5-11-96 and 5-12-96 through 6-8-96 (5 inspectors per report)EMPLOYEE CONCERNS PROGRAM: 4-29-96 through 5-3-96 (4 inspectors)
0 0-
 
s ~ ~ ~
.
CO CTIVE ACTION PROG
 
,                     CONDITION REPORT PROCESS STATUS
* VOLUME CONTINUES TO BE HIGH CR's GENERATED BY QUARTER 1500 1000 O
o   50
        %h 1ST   2nd                401  1st  2nd 3'TR QTR   QTR              QTR  QTR  QTR 95                            96 TOP SOURCES FOR 2ND QUARTER OPERATIONS QUALITYASSURANCE ENGINEERING IC
  " SIGNIFICANT CRs REVIEWED AT 0730 MANAGEMENTMEETING, ALLCRs APPROVED BY PGM
* 2ND QUARTER TREND REPORT DRAFT ISSUE MANAGEMENTREVIEW PRESENT TO NRC JULY 26 AUGUST 7 AUGUST 29
* AREAS FOR IMPROVEMENT- CORRECTIVE ACTION PROGRAM
          - REVIEW OF COMPLETED CRs SHOW INCONSISTENT LEVEL OF ROOT CAUSE
                  - BETTER TIE WITH ROOT CAUSE PROCEDURE (LEVELS Of ROOT CAUSE TIED TO SIGNIFICANCE OF PROBLEM)
                - MORE WIDESPREAD TRAINING NEEDED ON PROCEDURE/PIC HANDBOOK
:          - PROBLEM REPORT TIMELINESS 56
 
~ J
  .
:
 
  ~ OVERALLASSESSMENT Corrective actions is considered a limiting weakness and rcxruires increased management attention Personnel errors, attention to detail and procedural adherence are continuing problems
            'Ihe operating expeoence feedback program (OEF) and the foreign material exclusion program (FME) are unsatisfactory Our inability to curb the trend of recurring problems is indicative of ineffective correchve actions and less than adequate when determining
.          underlying causal factors QA AUDITS/PERFORMANCE MONITORING (AUGMENTED BY IB/PSL QA/QC PERSONNEL)
Second quarter 96: 7 Audits, 25 Finding, 80 Condition Reports Programs and Procedures are not sufEcient to preclude problems     fern occurring (Procedure Quality)
Procedures are not being followed with rigor (Human Performance) 13 Finding Responses late to QA. Process change with VP sign     off Rejected
          - by Site VP due to shallowness of response
    ~ INDEPENDENT TECHNICALREVIEWS Second quarter '96: 7 ITRs, 38 Recommendations,     11 Condition Reports
-             Conduct crews of Operations acceptable, however, inconsistencies exist between 57
 
QUAIXIYASSURANCE (continued)
O.
OEF program is not effective in reducing severity and renurence   of events PME programmatic controls have improved, however, cultural and personnel behavior changes are requned to achieve desired results QC INSPECIIONS/SURVEKLANCES Second quarter deficiencies rate 7.5% down Rom 8% 1st quarter '96 1363 surveillance/inspections with 102 deficiencies (most outage related), 71 Condition Reports Use of template and underwater repair methodologies for Rx vessel Qange resulted in major man-rem and budget savings 0-58
 
    \ l
.
r.zcmsING C
:
 
n
,~
O.
0-
 
REGULATORYCOMPLIANCE STATUS and AGENDA Recent NIRC lns ections as of June 30                   $ 996 RESIDENTS'ERIODIC: 3-30-96 through 5-11-96 and 5-12-96 through 6-8-96 (5 inspectors per report)
EMPLOYEE CONCERNS PROGRAM: 4-29-96 through 5-3-96 (4 inspectors)
PHYSICAL SECURITY PROGRAM FOR POWER REACTORS: 4-30-96 through 5-3-96 (1 inspector)
PHYSICAL SECURITY PROGRAM FOR POWER REACTORS: 4-30-96 through 5-3-96 (1 inspector)
Estimated NRC ins ector man-hours as of March 31 1996: 3978 Violations Sfafus as of June 30 1996 Nine Cited Violations Ten Non-Cited Violations Potential.
Estimated NRC ins ector man-hours as of March 31 1996: 3978 Violations Sfafus as of June 30 1996 Nine Cited Violations Ten Non-Cited Violations Potential. Violations Pending
Violations Pending 1)Configuration Control InadequaciesNiolations Potential Nonited Violations Pending 1)Licensee made a change to the facility without a 10 CFR 50.59 evaluation 2)Wide Range Nls inoperable for surveillance during Core Alterations (LER 335/96-05) 3)Maintenance performed without a stamped controlled version of a procedure 4)A temporary modiTication to an EDG was made and independently verNed incorrectly U comin Ins ecfions fhrou h Se fember f996:0 CEDMCS PROBLEMS: One Week-7/8/96 (Two Inspectors)
: 1) Configuration Control InadequaciesNiolations Potential Nonited     Violations Pending
ENGINEERING (FSAR CORRECTIVE ACTIONS): One Week-7/22/96 NRC REGION II SECTION CHIEF SITE VISIT: Two Days-Week of 7/29/96 SENIOR RESIDENT INSPECTOR OBJECTIVITY VISIT: One Week-8/5/96 RADIOLOGICAL PROGRAM: One Week-8/5/96 MAINTENANCE IMPLEMENTATION:
: 1) Licensee made a change to the facility without a 10 CFR 50.59 evaluation
One Week-8/19/96 LICENSED OPERATOR REQUALIFICATION PROGRAM EVALUATION:
: 2) Wide Range Nls inoperable for surveillance during Core Alterations (LER 335/96-05)
PHYSICAL SECURITY PROGRAM: One Week-9/9/96 One Week-9/9/96 OCCUPATIONAL RADIATION EXPOSURE: One Week-9/9/96 MAINTENANCE RULE INSPECTION PROCEDURE:
: 3) Maintenance performed without a stamped controlled version of a procedure
One Week-9/16/96 (Five Inspectors) 59 NRC VIOLATIONS
: 4) A temporary modiTication to an EDG was made and independently verNed incorrectly U comin Ins ecfions fhrou h Se fember f996 CEDMCS PROBLEMS: One Week - 7/8/96 (Two Inspectors)
+10 0 0 O 2 5 10 I 1 5 0 0 0~~0 0 0 0~~0~~14 Legend~Aclual Violaltons Actual NCV's 0 Jan Feb Mar-Apr May Jun Jul Aug Sep Oct Nov Dec'86 Date-Date Source: E.Weinkarn r~~1 l l~~
ENGINEERING (FSAR CORRECTIVE ACTIONS):                   One Week -7/22/96 NRC REGION II SECTION CHIEF SITE VISIT: Two Days - Week of 7/29/96 SENIOR RESIDENT INSPECTOR OBJECTIVITY VISIT: One Week- 8/5/96 RADIOLOGICALPROGRAM:           One Week - 8/5/96 MAINTENANCEIMPLEMENTATION: One Week- 8/19/96 LICENSED OPERATOR REQUALIFICATIONPROGRAM EVALUATION:                           One Week - 9/9/96
LICENSEE EYENT REPORTS20 15 15 Legend~10 CFR 6073 LER 10 CFR 50.72 Good ul~IO cr 0 z C.S.0 Jan Feb Mar Apr May Jun Jul Aug Sep Oct Nov Dec'S6 Date Data Source: Ed Weinkam Operating Experience Feedback FOP's TO BE PROCESSED 30 25 20 23 Good o 15 10~Actual Jan Feb Mar Apr May Jun Jul Aug Sept Oct Nov Dec Time (Month)FOP's TO BE CLOSED (CLOSE OUT SUNIMARY)35 30 25 Good 20 0 15 10 12~Actual Jan Feb Mar Apr May Jun Jul Aug Sept Oct Nov Dec Time (Month)~~y 1}}
:0  PHYSICAL SECURITY PROGRAM:
OCCUPATIONAL RADIATIONEXPOSURE:
One Week - 9/9/96 One Week - 9/9/96 MAINTENANCERULE INSPECTION PROCEDURE:                   One Week - 9/16/96 (Five Inspectors) 59
 
NRC VIOLATIONS I
0 0   0 ~     ~ 0 0 0 0 ~     ~ 0 ~       ~
15 14                                   Legend
                                                                                              ~Aclual Violaltons Actual NCV's 10
  +10 0
0 O
2    5 0
Jan     Feb   Mar- Apr         May       Jun     Jul     Aug Sep Oct Nov Dec
                '86 Date-Date Source: E. Weinkarn l  l  ~ ~
r   ~ ~ 1
 
LICENSEE EYENT REPORTS 20 Legend 15
                                                                              ~10   CFR 6073 LER 10 CFR 50.72 15 Good ul                                     C.
~IO                                 S.
cr z0 0
Jan     Feb Mar Apr May Jun   Jul     Aug Sep Oct Nov Dec
                'S6 Date Data Source: Ed Weinkam
 
Operating Experience Feedback FOP's TO BE PROCESSED 30 Good 25 23 20 15                                                               ~Actual o
10 Jan Feb Mar Apr   May   Jun     Jul Aug   Sept Oct Nov Dec Time (Month)
FOP's TO BE CLOSED (CLOSE OUT SUNIMARY) 35 30 Good 25 20 0                                                                 ~Actual 15 12 10 Jan Feb Mar Apr   May   Jun     Jul Aug   Sept Oct Nov Dec Time (Month)
~ ~ y 1}}

Revision as of 08:38, 29 October 2019

Forwards Matls Reviewed During 960719 FPL St. Lucie Status Meeting Including Key Performance Indicators for Plant
ML17309A848
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 07/24/1996
From: Stall J
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
L-96-193, NUDOCS 9608020352
Download: ML17309A848 (84)


Text

CATEGORY 1 REGULATORY INFORMATION DISTRIBUTION SYSTEM

~ (RIDE)

ACCESSTON NBR:9608020352 DOC.DATE: 96/07/24 NOTARIZED: NO DOCKET FACI.: .-50-335 St. Luci,e Plant, Unit 1, Florida Power & Light Co. 05000335 50-389 St. Lupie P3;ant, Unit 2, Florida Power 6 Light Co. 05000389 AUTH. NAME AUTHOR AFFILIATION STALL,J.A. Florida Power s Light Co.

RECIP.NAME REC1'PIENT AFFILIAT10N Document Control Branch (Document Control Desk)

SUBJECT:

Transmits copy of matls reviewed during 960719 FPL St. Lucie Status Meeting including key performance indicators for St.

Lucie Plant.

DISTRIBUTION CODE: A001D COPIES RECEIVED:LTR ENCL SIZE:

TITLE: OR Submittal: General Distribution NOTES:

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-3 LA 1 1 PD2-3 PD 1 1 WIENSFL. 1 1 INTERNAL: ACRS 1 1 FILE CENTER 01 1 1 NRR/DE/EMCB 1 1 NR ICB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 NUDOCS-ABSTRACT 1 1 OGC/HDS3 1 0 NOAC 'XTERNAL:

1 1 NRC PDR 1 1 D

N NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP UP TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN 5D-5(EXT. 415-2083) TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

TOTAL NUMBER OF COPIES REQUIRED: LTTR 13 ENCI 12

i+

0 f v-~

l]f (4

Florida Power 5 Light Company, P.O. Box 128, Fort Pierce, FL 34954-0128 July 24, 1996 L-96-193 10 CFR 50.4 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 RE: St. Lucie Units 1 and 2 Docket Nos. 50-335 and 50-389 St. Lucie Status Meetin Jul 1996 During a November 1995 meeting with the NRC, Florida Power and Light Company (FPL) reviewed the progress made in completing activities outlined in the St. Lucie Plan to Improve Operational Performance. FPL stated that meetings to review performance would be held monthly and would include a detailed review of the plant's key performance indicators. In the November meeting, FPL committed to provide the monthly review materials to the NRC.

Attached is a copy of the materials reviewed during the July 19, 1996, FPL St. Lucie Status Meeting including the key performance indicators for St. Lucie Plant.

We look forward to NRC presence and feedback at these monthly meetings. If you have any questions on this material, please contact us.

Very truly yours, J. A. Stall Vice President St. Lucie Plant JAS/EJW Attachment c c: Stewart D. Ebneter, Regional Administrator, USNRC, Region Ellis W. Merschoff, Director, DRP, USNRC, Region II II Kerry D. Landis, Branch Chief, USNRC, Region II Senior Resident Inspector, USNRC, St. Lucie Plant L. A. Wiens, Senior Project Manager, USNRC, NRR 9608020352 960724 PDQ(l'ADOCK 05000335

'

P PDR an FPL Group company

ST. LUCIE STATUS MEETING AGENDA JULY 19, 1996 9:30 AM SSB ROOM 2200 J. Scarola A. Pell GOALS vs. PERFORMANCE SCOPE COMPLETED EQUIPMENT UPGRADES NEAR MISS ENERGIZING 1B2 4160v BUS B. Korte UNIT 2 MANUALTRIP ON 6/6 DUE TO GENERATOR TEMPERATURE J. Price INADVERTENT SIAS ACTUATION ON 6/8 R. Filipek STEAM GENERATOR G. Boissy ~

LOSS OF BUDGET CONTROL R. Heroux RAYTHEON CONTRACT MISMANAGMENT J. Marchese OPERATIONS H. Johnson MAINTENANCE J. Marchese ENGINEERING/TECHNICAL D. Denver MATERIALS MANAGEMENT G. Boissy SERVICES C. Burton CORRECTIVE ACTIONS B. Dawson QUALITYASSURANCE W. Bladow LICENSING E. Weinkam

'...960802Q35$

0 e

ox zmTIzg azvoav e

Unit1 Equivalent Availability

'%~V' 1 II j, 4 "r'.,4+I/ u 4 DAILYEQUIVALENTAVAILABIUTY nrul 2&if'+%0 ~,~sf ii<<sl 4'I/ 0 t +t ri/'ut /lith/o >6 5 IT 'l /lit, "9 a , I 0 Days orartne as of 7/I5/96.

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0/10/QO 0/la/90 0/20IQO OI22/90 0/24/90 0/20/90 0/24/90 0/Xrte 7/2/90 7/4/90 7/tvas 7/0/te 7/10/90 7/12/te 7/14/90 7/10/90 Monthly Average EAFaOOAXN Lost Generation Date MWH Loss Reason 0/1000/te 4020% tech/44/o Oi/faye 1$ dare Besot ea a Mtaaiae/a e/ttdatse capassy of 029 Mw EQUIVALENTAVAILABILITY FACTOR - UNIT 1

~Ate/at 949 QSA Tan/ct e705 --4--- Ta/Qet Bett Aaa'etta/e a 740 Best ttaeatse 75 704 aa Ie 50 0

Fat/ Mar Apr May tun Jul Aug Sep Oct Nov Dec Date

Unit 2 Equivalent Availability DAILYEQUIVALENTAVAILABILITY 32 Days on4ne Bs of 7/I5/96.

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$ 20/IO 5/2?/90 5/24/90 5/25/90 5/25/te Shoss 7/2/90 7/4/90 7/5/90 7/5/90 Tha/90 Th2/90 Tlin/90 7h5/95 Date Monthly At/erage EAF&5.9250 Lost Generation Date MWH Loss Reason 5/1025he 2B IlFWito0. V/na 5/2405/90 Hi Vhr.yo/ona SP.

5/2740/90 -747 Hi BP/rn/S.V/r/5/m.t/t Bnsce on 5 54annun opnnsoon eooncar or 059 Mw EQUIVALENTAVAILABILITY FACTOR - UNIT 2 Tor9et ~ 95.0 75 .Good .

47 a

50

~O Feb Mar Apr May tun Date

AUTOMATICREAGTOR TRIPS Legend 5- ~Actual 4

.Good .-..

rn CL l

03 0

R 2

0-Oct Dec Jan 'SS Mar May Jul Sep Nov Date Data Source: Hugh Johnson

-

ST. LUGI ANT Equipment Causes Operations to Maneuver Plant 20 15.

10 0

'u 0

0.

1 QTR 2 QTR 3 QTR 4 QTR 1 QTR 2 QTR Date 96 95

T 1 ovrAGE 8

1996 SPRING OUTAGE GOALS gNIT 1 I Goal Actual Personnel Safety - Lost Time Injuries ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ 0 0

2. Doctor Case Injuries ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ ~ . <6 12
3. NRC Violations...................................... 0 0
4. Outage Duration ~.............. ~ . ~................ ~ 49 85
5. Personnel Radiation Exposure........-...., .... ~ 310Mrem 366
6. Personnel Contaminations (any Contamination Resulting in a Skin Dose)...............-.. ~ ~ ~ ~ ~ ~ ~ ~ ~ o 5 1 0 Contaminated Floor Space within 14 Days PostOutage.................,.............,. <1,500ft'BD 7.
8. Cubic Feet of Radiological Waste Gen............. < 6,300 ft3 11,935 ft3
9. Outage Budget........,.......... .:.... ~ $ 25 Million 31.6 Million
10. Unit Performance

- 60 days Post Outage Availability... > 93 TBD outgoal.wpd July 17, 1996

Original Actual Difference Schedule Duration 46 85 39 Plant Modifications* 72 81 NPWOs 1769 2556 787 Activities 5243 9170 3927 CRs N/A 978 N/A OWAs 17 17 0 S/G Tubes P.lugged 50 2081 2031 S/G Tubes Staked 163 156 S/6 PAPs 500 500 0

  • 12 Major 8 69 Minor

10 Year Reactor Vessel Exam & Core Barrel Inspections Main Generator End Winding Module & Through Bolt Repairs Incore Instrument Assembly Replacement Polar Crane Load Test Diesel Generator Governor & Radiator Replacements RCP Seal Replaced Westinghouse S/G Tube Plug Repair (PAPs) & S/G Tube Plugs Pressurizer Code Safety Valve Replacements

.

HP Turbine Seal Ring Replacement Condenser Tube Cleaning System RPS NIS Upgrade V071 61 & Bypass Replacement RCGVS Valve Replacements & Piping Mod Rx Head 0-ring Upgrade

Outage Progress Chart St. Lucie Unit 1 Cycle 14 Refueling 100 Cunent Outage Dunttion 85 Days 3 Koum 0

.,Expanded MRPC

-1 00

~ ~ ~~

~~

-200

'. Free Span Added MRPC

-300

~~ ~ ~ g~

g -400

-500 ~Kours Ahead or Behind 1pp% MRPC

-600

-700 ~ t~

-800 ~

0 S/8 Rework ';

-900

Outage Progress Chart Legend Gains 8 Losses (Hours)

Date Day Hours Discription 4/29 1 6 Loss Delayed Shutdown CEA ¹1 4/30 2 8 Gain Beaming Metal Temperature Satisfactory 5/1 3 3 Loss Generator Disassembly 5/2 4' 8 Loss Blower Gas Baffle Removal 5/3 Blower Gas Baffle Removal 5/4 6 14 Gain Generator Blower Disassembly 5/5 7 26 Gain Rotor Removal 5/6 8 14 Loss Asbestos Abatement 5n 9 34 Gain Wedge Replacement 5/8 10 41 Loss Scope Expansion: Low Torque on Through Bolts 5/9 11 3 Loss Generator Disassembly 5/10 12 5 Loss Generator Disassembly 5/11 13 8 Gain Support Ring Removal 5/12 14 Support Ring Removal 5/13 15 Support Ring Removal 5/14 16 Support Ring Removal 5/15 17 189 Loss Expanded MRPC Thru 5/26 27 5/2? 28 148 Loss Free Span Added MRPC Thru 6/3 35 6I4 36 480 Loss 100% MRPC Thru 7/5 68 r 7/6 69 130 Loss S/G Rework Thru 7/12 74 7/13 75 6 Loss CEDM Venting 7/14 76 13 Loss RCP 1A2 Seal Leakoff Flange Leak 7/15 77 20 Loss Valve Ql-II's 8 Retesting 7/16 78 11 Loss HVS-1B Cooler Leak 7/17 79 11 Loss HVS-1B Cooler Repair

Total Duration: 85 Days (Projected)

Hours Lost From Original 46 Day Outage Original Schedule: . 46 Days Hours Days System Description

-793 -33 Steam Generators Expansion of MRPC 8 Tube Plugging Scope Steam Generators Rework-Missing "8" S/G H/L Plug 8 2 "A" S/G H/L

-96 Stakes Component HVS-1B Cooler Leak

-22 -0.92 Cooling Water Sy'tem

-20 -0.83 ECCS 8 RCS Valve Ql-II's 8 Retesting

-13 -.0.64 Rx Coolant System RCP 1A2 Seal Leakoff Flange Leak

-6 -0.25 Rx Coolant System CEDM Venting 960 39.5 TOTAL

The Major Schedule Impact Behind The Steam Generators Hours Days System Description Nuclear Wide Range Nl's 8 RPS Nl Upgrade Project 912 38 Instrumentation Resources Reduced Primary & Secondary Resources Behind 456 Steam Generators 72 Fuel Pool System Fuel Transfer Gate Valve V-4111 Process Clearances, Housekeeping, Paperwork, Procedures 64 3 Delays/Problems

0 c ILGZL8

~ Pre-outage Planning & Preparations Pre-outage Milestones Must be Met for Upcoming Outages Earlier Delivery of NPWO's, PCM's 8 Procedures Continue to Improve Organization's Schedule Adherence Freeze Organizational & Process Changes Earlier (Pre-outage)

~ Scope Control

~ 20/30 MRB

~ Budget Controls

~ Manpower Schedule Set Earlier

~ 13 Week Rolling Schedule

~ Scheduled CMMs, Perform Daily Work Out of Outage

~ Improve Organization's Schedule Adherence

~ Eliminate Periods of Inactivity

~ Improve Communications 8 Handoffs

~ Ensure Procedures are Ready

~ Continue to Improve Contingency Planning

~ ~

~ ~

azC ~

~y~ ACTIONS

. NEAR MISS ENERGIXING 1B2 4160V BUS On June 1, 1996, the Electrical Maintenance outage shift supervisor (peakshift) released the 1B2 4160V bus clearance with a grounding breaker installed in the Auxiliary Transformer feeder breaker cubicle. During the bus restoration by Operations, the peakshift Chief Electrician discovered the grounding breaker and alerted operations to stop the restoration.

CA E (ERT TEAM FINDINGS)

Bi Failure of the Supervisor to ensure the equipment was ready for service:

Unaware of the configuration of the feeder stabs and the bus stabs Did nof read the caution tag installed on the grounding breaker indicating the bus was grounded Did not review all work orders associated with the work on the bus or related equipment The clearance order did not have the work order number associated with the bus work on the clearance N

AllElectrical Maintenance Shift Supervisors are not required to be trained in the high voltage grounding training Clearance orders do not list work orders against the clearance Clearance orders do not list grounds on the clearance order There is no labeling at the bus cubicles that identify that grounds are installed 13

NEAR MISS ENERGIZING IB2 4160V BUS

.

RRECT A COML. DAYK DISCIPLINARYACTION TO THE SUPERVISOR 6/3/96 SAFETY MEETING REVIEW 6/20/96 REVISE THE CLEARANCE PROCEDURE TO TRACK 6/30/96 GROUNDS AS PART OF THE CLEARANCE ORDER ISSUE NEW CLEARANCE PROCEDURE (F.R.G.) 7/30/96 UPDATE DRAWINGS TO NOTE BUS 7/30/96 CONFIGURATIONS ANNUALHIGH VOLTAGE GROUNDING TRAINING 8/2/96 FOR SUPERVISORS ADD PLACARDS/VISUALAIDS TO BREAKER 8/30/96 CUBICLE WHEN GROUNDED REVISE THE CAUTION TAG PROCEDURE TO 7/15/96 REFLECT SPECIFIC LOCATIONOF GROUNDS 14

MANUALREACTOR TRIP DUE TO HIGH COLD GAS TEMPERATURE At 1209 on June 6, 1996 the GENERATOR TEMPERATURE MONITOR annunciator (N49) alarm was received. The Kaye computer, which records main generator temperature showed that average cold gas temperature was above normal at 48.8 degrees but was decreasing. The annunciator cleared one minute later and all temperatures returned to normal and were stable. TCV-13-15 (hydrogen cooler outlet temperature control valve) was in automatic and appeared to be controlling at setpoint.

At 1232, the control room noted average cold gas temperature rising as displayed on the Kaye computer. Within seconds the temperature reached 53 degrees, which is above the procedurally required reactor trip level of 52 degrees. The Operators tripped the reactor and turbine.

Initial investigation indicated that TCV-13-15 had failed closed, and that the positioner feedback arm had vibrated loose and fell off.

This is the second event in 1996 in which closure of TCV-13-15 had caused a

~

Manual trip. This issue was addressed in PR-96-001 and was attributed to

~ ~

~

~

improper setting of the derivation setting.

~

ROOT CAUSE (ERT FINDINGS)

TCV-13-15 has high level of system induced vibration.

Positioner linkage fasteners are below level of design. DevCon material was used as locking mechanism and periodically inspected.

This particular failure was not precluded using this practice of fastener retention.

Fail close mechanism under current design does not allow sufficient time for operator intervention. Operation in bypass will provide adequate control under varying system dynamic changes with some operator action.

MANUALREACTOR TRIP DUE TO HIGH COLD GAS TEMPERATURE CORRECTIVE ACTIONS Isolate TCV-13-15 and operate in manual bypass. Complete Modify positioner to a direct mounted device Complete eliminating linkage failure mechanisms.

Four valves per unit affected.

Review system and component requirements for PMAI Due 8/31/96 optimizing TCW control under v'arying load conditions. PM 96-06~7 Provide design changes as necessary to eliminate Working TCV failures as plant trip initiators while in automatic, or continue manual operation.

16

. INADVERTENTSIAS ACTUATIONON 6/8/96 EVENT SEQUENCE a6/8/96 - INADVERTENTACTUATION OF 'B'HANNEL SIAS AND CIAS RECEIVED WHEN IBC MAINTENANCE REPLACED POWER SUPPLY REGULATING CARD.

ERT TEAM ESTABLISHED.

~ SENSITIVE SYSTEMS PROCEDURES INVOKED FOR TROUBLESHOOTING. IDENTIFIED POTENTIAL FOR CSAS 8 RAS ACTUATION DURING TROUBLESHOOTING BUT THAT WAS INADVERTENTLYCOMMUNICATED TO THE OPERATING CREW ON 7/3/96.

~ 7/3/96- INADVERTENTACTUATION OF 'B'HANNELCSAS & RAS RECEIVED WHILE TROUBLESHOOTING PREVIOUS ACTUATION.-

ROOT CAUSE INVESTIGATION RESULTS 6/8/96 ACTUATION aAUCTIONEERED POWER SUPPLIES BOTH FAILED CAUSING INITIALACTUATION. S3 SUPPLY HAD CROWBARED DURING ADJUSTMENTS OR INSTALLATIONOF REGULATING CARD. M3 SUPPLY FUSE BLEW WHILE INSERTING REGULATING CARD. LOSS OF BOTH POWER SUPPLIES CAUSED ACTUATION RELAYS TO DE-ENERG IZE.

~ ESFAS ACTUATION MODULE POWER SUPPLIES NOT WIRED PER

- DRAWINGS. BY DESIGN SIAS & CIAS ARE POWERED FROM POWER SUPPLIES INDEPENDENT FROM THOSE THAT FAILED.

17

ROOT CAUSE /NVEST/GAT/ON RESUl TS 7/3/98 ACTUATION

+MISCOMMUNICATIONOF SENSITIVE SYSTEMS TO THE OPERATING CREW.

aMISUNDERSTANDING OF WHAT "ENERGIZE TO ACTUATE" MEANS IN REGARDS TO CSAS AND RAS. DUE TO ACTUATION MODULE DESIGN, THE ACTUATION RELAYS WILL ENERGIZE IF+ 15V POWER IS LOST BUT+24V REMAINS. WHEN +15V POWER WAS REMOVED DURING TROUBLESHOOTING, CSAS AND RAS ACTUATED. WHILE THIS IS AN ACCEPTABLE DESIGN, THE MISUNDERSTANDING WAS THAT IT WAS ASSUMED THAT "ANY" LOSS OF VOLTA'GE WOULD NOT CAUSE AN "ENERGIZE TO ACTUATE" SYSTEM TO ACTUATE.

CORRECTIVE ACTIONS

+READJUSTED POWER SUPPLIES REWIRED ESFAS SA AND SB CABINETS PER DESIGN DOCUMENTATION

'LTHOUGH IT WAS DETERMINED THAT ESFAS WOULD PROPERLY FUNCTION IN THE AS FOUND CONFIGURATION.

~ PROVIDE GUIDANCE ON WHAT "ENERGIZE TO ACTUATE" MEANS.

m 18

~ C I P

RR ~ C

~ ~ P

~ C

~ P ~ C

~ 0 ~

~ ~

C PJ C ~

team Generator P ugging Operation

+ 157 Short Tube Stabilizers

+ 4 Long Tube Stabilizers

+ 1021 Tubes Plugged in Steam Generator "A"

+ 1060 Tubes Plugged in Steam Generator "B"

+ 2 Welded Plug Repairs

+ Corner Cover Plates Modifications for Plugging

+ Scheduled Finnish of Plugging Operations - 7/12/96

+ Finished Plugging Operation on 7/5/96 0

Original Base Scope of Work

+3 Plenum Effort Dual Guide Tube during PAP Installation, than 4 Plenum Operation

+ 100%0 Bobbin Coil Testing

+ 100'/o Hot Leg MRPC

+ 20'lo Cold Leg MRPC

+ Inspection Schedule k PAP Installation - 15 Days

+ Steam Generator Work Started - 5/7/96

+ Completed Original Base Scope of Work - 5/18/96

+ Completed 3 Days Ahead of Schedule.

+ Includes 1 Day Delay for PAP Installation

Revise Scope of Wor

+ 100/0 Cold Leg MRPC

+ Diagnostic Testing Program

+ Limited Free Span Testing

+ 100/0 of P9 k 010 Support Plates

+ 100'/0 Free Span Testing

+ Extended Outage Duration from 5/19/96 - 6/26/96

+ Combinations of Inspection and Plugging Operations in progress. during this period.

+ Equipment Expansion - Platforms Modifications, dditional Genesis Equip:nt Added (10 Stations)-

I

team Generator C oseout Process

+ Missing (2) Short Stabilizers in Steam Generator "A" Transcription Error

+ Missing Hot Leg Plug in Steam Generator "B" Shift Supervisor Interpretation Error

LOSS OF BUDGET CONTROL Problems Encountered Poor contract administration practices Budget inadequate O.

Budget does not mirror site organization Budget disconnected from tracking Departments not familiar with approved budget Resource Controls Staff not independent Expectations not clear Enhanced Controls Contract Administration Enforcement of NP 1100 Authorization Matrix Discipline for Violations Eliminate "covenience contractors" Full time Phone Tech and Plumber Service agreements Good Practice - NC performed by PSL Maintenance Reduce Overtime Eliminate Exempt Overtime Confine Non Exempt overtime to LCO and,Techspec Eliminate Discretionary Spending Subscriptions, Painting, Tool Purchases Office Supplies, Luncheons, Consummables Budget Reconstitute 1996 08 M Budget

$ 24 Million in budgeted funds for the balance of 1996 Must reduce to 'bare bones'otal recovery is not possible New Process for 1997 MRB to determine Project Scope during budget cycle Resource Controls will issue department targets Departments may challenge assumptions Departments may submit additions for consideration Budget will be signed by Cognizant Owners 24

I. dentification of vent/Current ituation Raytheon contract P.O. B92914-20017 is out of funds on 5/19/96 and expires 6/30/96.

A contract amendment to extend the contract expiration date to 8/30/96 was authorized, however, additional funding was not authorized on the amendment. Woik is currently being performed without authorized funds to cover the subject work.

II. ack round 6/30/92 Contract issued for $ 57,000,000.00 to Raytheon Constructors, Inc.

4/11/96 Projects determined there was not suQicient authorized funding in the contract to cover the SLl-14 outage and a contract extension would also be required since the contract termination date was 6/30/96 and the SLl-14 outage could still be in progress or just completed. A Contract Change Order for $ 8,000,000.00 and contract extension to 9/30/96 was initiated.

4/18/96 CCO approved by the Site Services Manager. PSL Vice President identified need for cover letter and returned the CCO to the Site Services Manager.

Budgets analyzed available funds, projected outage work, and new fund requirements. Maintenance Manager reduced amount of new CCO to

$ 5,000,000. from $ 8,000,000., and shortened the contract extension date based on original scheduled outage scope and returned to Services Manager 5/19/96 Contract dollar limit reached on subject contract.

5/22/96 Projects re-identified inadequate funding and Maintenance Budget or Maintenance Projects Resource Control generated a new CCO with reduced dollar amount ($ 5,000,000.00) sinceprevious CCO had pen and ink changes.

DWA 0165340 R4 for $ 5,000,000.00 was initiated on 5/22/96 authorized by the Services Manager of 5/28/96. DWA also extended the expiration date to 8/30/96.

5/23/96 Contract Amendment No. 4 was initiated and approved by the Site Vice President to extend contract expiration date to 8/30/96.

25

5/27/96 New CCO which added $ 5,000,000.00 approved by the Maintenance Manager 5/31/96 Approved by Resource Control Supervisor. Rejected by Plant Manager because date on new CCO not correct in that it didn't show that the original CCO was initiated on 4/11/96.

6/6/96 CCO returned to Resource Control Supervisor for revision to reflect appropriate dates.

6/7/96 All PSI. Signatures obtained. Invoice for period 6/5 through 5/19 paid.

Insufficient contract funding remaining to pay for work completed since 5/19/96.

XQ. Xdentification of the Cau e s A. R C

~ Failure to follow procedure NP-1100 and established site policies regarding authorized contract funding.

Failure of site organizations to process CCO in a timely manner or provide timely feedback to appropriate groups.

B.'ntri uti actors

~ Failure of site to strictly enforce procedure NP1100 and established site requirements regarding authorized contract funding.

~ DWA on 5/22/96 applied to work already complete (through 5/19) and Rev 4 Amendment to contract without funding authorization.

V. Corrective Action

1. Review all other site contracts for similar occurrences, insufficient contract funding or contract authorization dates. Complete
2. Re-enforce NP-1100 policy/site requirements to ensure adequate control of contract authorization amounts. Complete
3. Due to increased outage and SG support, re-evaluate dollar amount to ensure adequate funding until new contract is awarded. Complete
4. Approve CCO for additional funding.
5. Strengthen cost tracking for contracted work.

0-26

OPERATXGNB fr r Annunciator response procedures Procedure upgrade prioritization Conf iguration management process changes EOOS procedure Surveillance tracking Equipment clearance Operations personnel performance 27

OPERATOR WORK AROUNDS Updated and Submitted by: OST - Fuiford MONTH Aug.95 Sep-95 Oct-95 Nov-95 Deo-95 Jan-98 Feb-96 Mar-98 APr-98 May-98 Jun.98 Jui.98 Aug.98 Sep.98 Oct-98 Nov-96 Dec-98 OPEN 79 96 103 101 96 41 55 47 43 37 38 32 TARGET 45 4e 48 43 40 38 30 20 18 17 18 15 120 operator ln performing duties within the approved procedures or In accordance with the Intended design.

100 Decrease due to separation of OWAs from Operator Inconveniences.

80

~OPEN 60 .. 0 ..TARGET 40 .-

Year End Target"-15 20 Aug-95 Oct-95 Dec-95 Feb-96 Apr-96 Jun-96, Aug-96 Oct-96 Dec-96 Time (Nlonth)

OPERATOR WORK AROUNDS WORKING LIST 0 pdated and Submitted by: OST Fuiford NPWOI SCHD SCHD CR NO. DESCRIPTION DEPT STATUS START COMPLETION UNIT - COMMON 96424111 Pull-to-lock PCM defeats SIAS on ICW/CCW kcally NEED PMT 3/1/96 7/11/96 9642<58 RCGVS leak- Replace Unit 1 (V1441~) MM NEED PMT '/30/96 0-960091 Lvl Cntrl Viva position iixficators destroyed during maint. PM SCHD '/30/98 UNIT 1 PCM 017-196 Lrg P p starts cause btry chrgr 8, instr buss to alarm NEED PMT 6/19/96 63-2868 Turbine latch pushbutton on RTGB is not operable IC'C NEED PMT 4/29/96 6/30/96

'/1 9&4817 Turbine turning gear anil not engage from control room NEED PMT 4/29/96 5/96 5/96

'0/1 9602-228 L/D pressure control viva are notable to control press IC SCHD 4/29/96 864356 Spurious RTGB gmds have caused many annundators IC SCHD 4/29/96 7/30/96 634559 GEARS indicating wrong positionduring dwnpwr causing airm IC NEED PMT 5/1 5/96 6/31/96 96-5386 Rad mon pwr failure alarms frequently IC SCHD '/31/96 9642-403 1B fire Pp start causes battery chrgr to alarm IC NEED PMT 6/15/96 96434I68 SB 13306 is vibrating, this will enlarge keyway again ~ JPN NEED PMT 4/1 5/96 '/6/96 9641718 HP stub shaft has a bow, causing eccen to be beyond design MM NEED PMT 4/29/96 6/1/96 9643448 Pressurizer code salties have leaked frequenfiy NEED PMT 4/29/96 '/30/96 9643-256 DEH filters do not remain full during normal ops. Vented 1/shit NEED PMT 4/29/96 '/30/96 964 34I68 PCV-12-50 does not work according to procedure NEED PMT 4/29/96 '/1/96 9643443 Auto-sync feature of DEH is Inadequate SCE NEED PMT 4/29/96 6/30/96 '

9642C00 CST kep seal gets pushed out w/no fitl in progress. Alarms SCE SCHD 4/1/97 9&03-255 Annun "gland seal stm press hillo" comes in frequently SCE NEED PMT 4/29/96 6/30/96 9603477 Root cause of gas surge tk moisture trap failure SCE NEED PMT 4/29/96 '/30/96 9&0~14 Main generator vibration is approx 17 mila SCE NEED PMT 4/29/96 6/15/96 UNIT 2

~23 2A 8 2B D/G tachometer provide unreliable readings NEED MRB 960~64 D/G pyrometers 8 thermocoupies have chronic loose conn. SCHD 9/30/97 PCM 086-292 PC-11 kep 3 comm failure causes failure of audible alanna SCHD 8/31/96 9&03-702 PCV4kh879 gland seal reg does control pressure SCHD 11/30/96 PCM 251-295 SR-14350 lifted while testing CCW N hdr isolation vlvs Mh~ NONE 96-1880 V4111, iso fuel transfer tube, leaks by seat Restore PIA-1140 to original ccnfiguraticn when RCGVS is fixd

'C MM SCHD NONE 10/30/96 9602-287 V4217 Ls leaking by the seat causing the 2A2 Sl hdr to press. SCE SCHD 9/30/97 9642'1 MFW Pp sucfion relief viva fail repeatedly SCE SCHD 9/30/97 9643413 Extraction stm trap bypass viva wig not dose e 100% pwr SCE SCHD 9/30/97 9643459 TIC-2223, UD TCV Is swinging causing L/D temp to be unstable SCE SCHD 9/30/97 Work complete, waiting PMT 29

Man Rem 400 Unit 1 Refueling Outage 335.

I Outage Budget= 310 a+ r ~ ~ ~ ~~ 0 Pi A 300 1 =

E Target 200

~Aalual 100-0 Mar - Jun Jul Sept Oct Nov Dec Jan Feb Apr May Aug Time (Month)

Personnel Contamlnatlons 100 Unit 1 Refueling Outage 92 90 80 eC 70. ~..ge.g A 60 Target E

50 e'er e e e

~Aalual 40 ~ ~

o 30 r fe 20

.10 r ~ ~ rr 0

Jan Feb Mar Apr May Jun Jul Aug Sept Oct Nov Dec Time (Month)

ST. LUCIE PLANT CONTAMINATEOFLOOR SPACE 4500 4000 Post outage recovery of contaminated floor space.

~Aclual

- - - - - -Target 3500 3000 a 2500 Unit 1 Refueling Outage ro 2000 lnrrcceeek48 elec 8 fottowtng 1500 . Benchmertdng with Turkey Poktl end 1000 keeping wkh industry precgcee.

500 Sep- Oct Nov Dec Jan- Feb Mar Apr May June Jul Aug Sept Oct Nov Dec 95 95 Time (month)

Unit 1 CPI (Chemistry Performance Index)

Unit Shutdown For Refueling Outage INPO GOAL ~

125 120 K

EJ 1.10

"""DAILYCPI QTR AVG CPI I5I5mII5I5I/5flml151I5I5q<5555/55m Unit 2 CPI (Chemistry Performance Index) 1.50 INPO GOAL <

1.25

~

1.10 ~

~ ~ . ~ DAILYCPI

~OTR AVG CPI I 5 I 5 5 I I 5 I I I 5 5 I 5 I ( 511m < f 5 5 5 I I f5 5 32

IMPROVEMENTS/ACTIONS r vement Pro Status Update:

~ Maintenance Procedure Upgrade Pmj ect Plant Material Condition (Key Performance Indicator):

~

PWO Backlog (Power Block/Total)

~ Control Room Green Tags (C-Tags)

~

Aged PWOs (>12 months - Golden Oldies)

~ Leaks (Primary/Secondary)

~

Temporary Leak Repairs Quarterly Quality Report

~

Quality by Crews 33

0-ST. LUCI T MAINTENANCE PROCEDU GRADE PROJECT TASK N; DEVELOP PROCEDURES/GUIDELINES FOR FREQUENTLY PERFORMED MAINTENANCEACTIVITIESWHICH CURRENTLY EMPLOY THE USE OF VENDOR TECHNICAL MANUALS gG vis<2<<'.',j 1$ ,:y U<<t<AFAS ~ 4 I&C I&C Rosemounl Bench t'oyYi&<i',-"y Transmktcrs Ca'ibra6on 98080 IIO080 I&C 1&C I&C i&C I/,C I&C "t3doiiiti,L'tuel?'o;c Spcrl Fuel Pit Vers ega Cht Setup Rod Drop Ult U2Rcbuikln CEDM CaMe I 40006$ : Add

,,d.kfb';<~/ ., ttc/l$

0 <::N4

.40021.: Levd Swyches Sdl<<fcators C<<itrut<< FCV-12 1 Rcpdr /few E<sfpment t80504A'j.'4",8 181/90 681/90 98080 1081/90 1 IO080 681/90 I&C I&C I&C 'l&C MECH MECH Mayeetrd V2 Gcn Alomtc Ut Cot Coe Atoo/e Urft 2 LPM C<<6 Comp. Teiyd Rock Levd Swychcs GMMorftor Ooi. Iha SI.W&0M Letdown Vhis Valves 68180 98080 108 1I98 1 IO080 /Ol/90 /O1/96 I&C I&C I&C I&C I&C I&C I&C MECH Ash</oR V2 Gen Atordo U2 GenAIonfc Ut Roil!ore OP Soli Ut t 2 Correl of Tcc lsohlcrs OP-2 I 600029 Hcreypran Press Benches SSO Proc Monk<< SSL Proc Monil Alom Proc Mon Pros Mani Rdny Calbreyon I&C Procedure Valves

/8 f80 6OMS 9808$ 108180 118088 f28 f80 IOIRF 68 18S

<fSCH~~>r~<N. I&C I&C MECH MECH MECH I&C I&C MECH Mo>:ro i'o~%:t Ul leldown U2GenAt<<dc WesSnghouse eaton Hyrseutc /arne sbuy U2 Safcyuards IT'f Barton Sory Warner Process Me<<tore PIG Proc Meri otrcs Valves Valves Mdcrs Cel. Hyd. Ash<slots Valves

~~4ywg."; /OI80 tOI80 98080 108180 1IO080 128180 tOll97 68180 Ecg~<<'~>'g MECH MECH MECH MECH MECH MECH Oraycn Valves Ye<way Valves Dresser akor Eny Vetch tnc 0 bp cmdl/ny PSL.2 Pte d Sp ed5e Procedures

.'I'Il'hts'FW',..>'. (Consofdctcdt Vdves elves 500I'u~~i~4 IOI/98 honyeNbe>:>

aWi N.,"'dN'LLIS

'i g Fsb

<9!i%4,4

%>+) g@Mttlcg4%c @wg'

/OI80 I2FA (Weft/I @IN '@JtlIIlfl<<9UII agley<<jtt '@g <<@AII +~1 98080 8 'tttt2/StÃ<<

1001/90 NOSI0I00f-'.sn I IO080 rtshttt&~

1281/90 j'g)SSItlItITS@ g<<'tdy'futt'8 'f%'SFGb'

e POWER BLOCK PWO BACKLOG Joe Marchese - Maintenance PWO Backlo

- PWO backlog are non-outage corrective work orders (Work Type 5 status 22-48) on components/equipment in the power block. Total includes all Work Type 1, Work Type 3 8 Work Type 5.

all hold codes 900 600 700 TOTAL=" 2056 Good ~ t.

~una1

~commort X

end - tNT5 Vntt 2 Total 600 Terrret 0 500 400 a e s s s s s s ~ s a a a s a a a a s s s a a e e s a s a a as a s s s s s a Target e 350 Total 175 Mech 300 155 I&c 20 Hect 200 100 Sep Oct Nov Dec Jan Feb Mar Apr May Jun Jul Aug Sep Oct Nov Dec

'95 '96 Date Data Source Passport

SUMMARY

STATUS Discipline Unit 1. Unit 2 Common Total Mechanical 47 91 25 163 Electrical 10 22 I&C 93 95 13 201

. ProJects 0 Total 152 198 39 389

CONTROL ROOM DEFICIENCIES C-TAGS Randy Olson - l&C

~C.T8 S:

- The number of Control Room/Board Green Tags. It provides an indicalion of the I

attention given to maintaining control room instruments in an operable condition.

80 ~ " OU'fiGh-7 70 davit"" ~H~oso X Told

" Non Odoeo TNeel ol 80 I

80 l

c) 40 0

2o 30 20 ~

10 ~

Moo Odoeo Togd os Sep Oct Nov Dec Jan Feb Mar Apr May Jun Jut Aug Sep Oct Nov Dec

'95 '98 Date Data: M. Vitae

SUMMARY

STATUS Non-Outage Outage Total Ready to Work 12 18 or Workln Engineering/RTA AWP Other Holds Total 16 23 Unit 1 Unit 2 Oldest 10/17/94 PWO ¹ 0137 Discipline EM (OUTAGE) l&C ( AGE)

P e

AGED PWOs ) 12 M HS GOLDEN OLDIES Joe March Maintenance

~Aed PWoe:

- Non-outage corrective maintenance work type 1 and work type 5 PWOs older than 12 months.

80 Legend 70 Gbbtt ~una1

~unll2 60 ~Common O

350 Work Type 1 Included

-X-Torsi Te rect

>40 o 30 0

20 Target .0 10 Sep Oct Nov Dec Jan Feb Mar Apr May Jun Jul Aug Sep Oct Nov Dec

'95 '96 Date Osis Source: Psedrort SUMIIARYSTATUS Unlt1 Unit 2 Common Total Mechanical 20 26 Electrical 10 1&C 10 20 Construction Total 33 57 Oldest 10/5/94 5/12/95 4/17/95 PWO // 2546 4605 8676 Discipline ILC I&C I&C

LEAKS N. Motley Leaks:

~

- Active leaks (primary and secondary) 70 OUTAGE Legend 60 UNIT 1 OUTAGE UNIT 2 = 24

=

Good Non.outage 50 Non Outage Target J

40

's ~ ~ ~

30 R

20 10 Non.Outage Target ~ 10 0

Sep Oct Nov Dec Jan Feb Mar Apr May Jun Jul Aug Sep Oct Nov Dec

'95 '96 Date Data Source: Passport

SUMMARY

STATUS Unit 1 Unit 2 Total Non-Outage OUTAGE Oldest (Non-Outage) 2/13/95 3/17/95 PWO // 5224 2832 Status READY. ENG

LEAK REPAI FITTINGS Neal y Leak Re airs:

Leaks that have been temporarily repaired.

55 1.egend-50 G ood Le 45 40 I ~

~Unit1 Unit 2

n. 35

" 30 25 0 20 0

z 15 10 5

0 Sep Oct Nov Dec Jan Feb Mar Apr May Jun Jul Aug Sep Oct Nov Dec

'95 '96 Date Oata Sovrce: Nell Motley

SUMMARY

STATUS Unit 1 Unit 2 Total Total OUTAGE 10 10 Page 13

ANNUNCIATORS Randy Olson Annunciators:

- Annunciators in alarm state. PSL has a darkboard concept, which means any annunciator in the alarm state is unacceptable.

14 Legend 12 Good ~ Vnit 1 0

10 .

~Vnit2 Target g s r

C 6

0 0

R 4 Target = 0 Sep Oct Nov Dec Jan Feb Mar Apr May Jun Jul Aug Sep . Oct Nov . Dec

'95 '96 Date Data Source: R.J. Davis (OM)

Unit 1 = Outage Unit2 =3 614/16Aux Feed Pum 2C, LPM age 10

QUALITYFEEDBACK BY CREWS 10 GRAPH REFLECTS 41 CR'S INITIATEDBY QAIQC CONTAINING 43 ISSUES I- 8 K

0Q.

K 6 R

0 l-Cl 4 R

0O 0 2 0

VALVES WELDING I&C PROJECTS VENDOR OST 'OTATING EM QC HP OTHER (FULFORD) (ENGLISH) (KORTE) (BLADOW)(McCULLERS) ~ NMM (MOTLEY) (JACOBS) (OLSON) (FRECHETTE)

~ ISI

~ JPN

~ SCE CREWS

~ .

0-

I DISTRIBUTION OF QUALITYISSUES 13 12

~ 10 Q

R

~ s K

D Q

Q 6 0

0 4 0 CONFIGURATION EQUIPMENT DEFECTS OTHER PROCEDURE WORK PRACTICES PAPER PROBLEMS PERSONAL ERRORS

~ CHEMICALCONTROL NON-COMPLIANCE (NPWO/JWR)

~ TESTING

~ FME/HOUSEKEEPING

~ PROCEDURES

  • o MATERIALCONTROL TITLE OF ISSUES

e e

SIGNIFICANCE OF QUALITYISSUES 25 21 20 0)

~ <5 14 0) 0)

kL 0 10 SlGN(FlCANT VERY SlGNtFlCANT EXTREMELY SlGNlFlCANT

~ NPWO CLOSEOUTIREVIEWS 'LOST PAPER 'TESTING

~ JWR 'CHEMICALCONTROL PROGRAM 'DEFECTIVE EQUIPMENT/MATERIAL

'WORK PRACTICES ~ MATERIALCONTROL ~ WORK PRACTICES

'POOR PROCESSES ~ REWORK

~ Hl-LITERS ON PAPER ~ INADEQUATE PROCEDURES

~ EXISTING CONDITIONS  ;,FME

.+PROCEDURE NON-COMPLIANCE

'PERSONAL ERRORS

'CONFIGURATION ISSUES SEVERITY OF ISSUES

~ .

-

IMPROVEMENTS/ACTIONS

.

r vement Improve Configuration Management Controls:

Reduce Open TSAs Reduce Age of Oldest PCMs SLl-14 Outl~ Scope PCMs 81 CR¹ 311 CRs 3SO PMAI's 74 Nuclear Instrumentation S/G Tube Plugging License Amendment and Operating Evaluations enforcement Conference issues

TEMPORARY SYSTEM ALTERATlONS TSA Kris Mohindroo - Engineering 50 Good Legend 45 ~unit 1

~unlt2 40 X 35 --- Total Target 30 I-v- 25 0

20 - Target tg" -. - .. ~

15 10 Oct Dec Feb Apr Jun Aug Oct Dec Date Data Source: Kris hlohlndroo

SUMMARY

STATUS Dlscl line Unit 1 Unit 2 Total Mechanical Electrical ILC 14 En lneerln 0 eratlons Health Ph slcs Construction Preventive Malnt SCE Total Oldest TSA 11/17/95 Disci line 1&C &C ~ ~

PLANT CHANGE/MODIFICATIONS Kris Mohindroo - Engineering 150 Good Legend

~untt1 125

~ 100

~

~unit2 X

Common Total Target 75 ~ ~ ~ ~ ~ ~

Open PCIM 0 "

Target -80 50 25 Oct Dec Feb Apr Jun Aug Oct Dec Date Data Source: Kris Mohlndroo SUNIMARY STATIjS-WORKING Disci line Unit 1 Unit 2 Common Total 0 enPCIM 109 18 132 PC/Ms )24 Mo. 12

ST. LUCIE PLANT - 10 OLDEST OPEN PC/M's SCH

PC/M DATE DATE DESCRIPTION CLOSE STATUS AND ACTIONS REQUIRED TO CLOSE NUMBER ISSUED FRG'D I DATE 193-189 Open Blowdown Cooling Water Heat Exchanger 2/I I/89 12/I I/89 PC/M implemented. Action plan to resolve slight periodic leakage Vacuum Breaker Valve Changeout problems with permanent drain catcher. Engr CRN issued for implementation.

042-289 Instrument u de installation of Conduit Seals 3/21/89 3/23/89 335-190 Check Valve Hinge Pin and Bonnet Modifications 7/18/91- 4/13/93- UNIT I PC/M implemented on valves V14147 and V14151. Modifications to on CCW pump discharge check valves V14143, Siip 0 Sup 0 OUTAGE V14143 planned for next refueling outage. Willclose PC/M upon V14147 and V14151 3/25/93- 4/13/93- of the work activity 'ompletion Sup I Sup I 097-191 FOP 55GL1154 Power Supply Repl 7/19/91 8/9/94 UNIT I OUTAGE 171-191 Resizing and replacement of MOV Thermal 7/17/91 9/19/91 UNIT I PC/M implemented on 122 valves. 15 valves remaining to be modified.

Overload Devices on 137 MOV's OUTAGE EM needs to schedule remaining work. Willclose PC/M upon completion of the work activity 186-191 Intake Cooling Water Support Modifications 7/I/92- Not UNIT I Sup 0 Complete. Sup. I was budget approved at the MRB I/30/96 for Su I FRG'd OUTAGE im lementationduringthe 1996Unit I outa e.

295-191 RCP Vibration Probes Relocation 10/18/91 4/27/93 086-292 Radiation Monitoring Computer Replaccmcnt 4/22/92 5/7/92 PC/M implemented. ICM has one PWO associated with two remaining CRN's which is required to be worked to close the PC/M. Willclose PC/M upon completion of the work activity.

203-192 Replacement of 95 Sigma Meters in the Control 12/21/92 4/6/93 PC/M partially implemented with 15 instruments installed. Recommend Room and Hot Shutdown Panel do to obsolesence as-building what work has been completed and close PC/M. New issues. PC/M's can then be generated based on planned work activities.

282-192 Anchor Darling Replacement 3/25/93- 4/I/93- PC/M issued as an As - Required (ARP) CRN's are being issue as Supp 0 Supp 0 needed.

10/8/93- 10/26/93 Supp I Supp I 2/9/95- 2/23/95-Supp 2 Supp 2

I1MPROVEMXNTS/ACTIONS Ma or Im rovements Areas

'utage Material Performance Amount of outage material ordered but not used Reduce on Site Inventory - a)38 million by year end, b)review and remove 1995 already written offDME material on site (See next page)

Increase Spare Parts Availability:

~ Maintain non-outage restocks to less than 500 (1%)

~ Maintain non-outage AWP PWO's to less than 70

~ Maintain the number of 30 day old PO's to less than 20 Address Equipment Differences Between Units and its Effect on Inventory stat719 48

Reduce on Site Inventory: a) 38 million by year end, b)review and remove 1995 already written offDME material on site.

QTATQ$ :

19 million of DME was on site January 1, 1996 14.5 million was sold at auction Approximately 4 million leA. of 1995 DME to review and return to inventory, or remove &om site (only PC 1 and 2 items)

LA / HED Finish review of remaining 1995 DME by November 30th.

In coincidence with above, remove material not to be returned to inventory December 15th (options; auction, consignment, FPL resources, commission contractor)

Potentjta 1996 DME funding shortage (current inventory 41.2 million, DME available 2.2 million, 1 million delta to get to 38 million) a)ICW pump rebuilds

'b)RCP seals - N9000 design c)Capitalize turbine valves like PTN Overmax currently at 4.4 million a)Numerous small examples Budget for 1997 DME (2 million needed to go &om 38 to 36 million)

Establish 1997 outage "contingency fund" by and implement "you order it you pay for it" policy by September 1, 1996.

LAR/aa019a 49

~

'NVENTORYVALUE Dan Quilty - Nuclear Materials Management 60 Good 50 ro 41.3 r

0

>~0 L

0$ Target = 38 0

O 30 20 Oct Dec Feb Apr Jun Aug Oct Dec Date Data Source: Norman Quesada

Nuclear Materials Management WAREHOUSE RESTOCKS 3000 2500 N 2000

~Aalaal


Target 1500 1066 3 1000 500 0

Jan Feb Mar Apr May June July Aug Sept Oct Nov Dec Date OVERMAX INVENTORYVALUE 5

..r.,

..- ~ ~ r

~

C7 4.4 o

CI 4 - Actual I " Target 3

r ~

W  %  %  % H u % R aa CO 1

Jan Feb Mar Apr May June July Aug Sept Oct Nov Dec Date

Nuclear Materials nagement OPEN REQUISITIONS OVER 30 DAYS 250 c 200 0

N 150 ~Aclual Target 100 C

12 50 aa H w H aa 0  % aa w p aa w w aa  %  % aa  % H % H H W W W aa H aa H % W  % H a H H W W H 0

Jan Feb Mar Apr May June July Aug Sept Oct Ncv Dec Date NON-OUTAGE AWP (STATUS 46 & 48) 200 180 160 e

140 120 4 C'a ~Aclual

" Target 100 80 e a a a a aa aa aa aa aa a aa aa aa aa aa aa aa aa aa aa aa aa aa aa aa aa w aa aa aa aa aa aa w aa w aa aa aa aa aa 60 Good 40 20 0

Jan Feb Mar Apr May June July Aug Sept Oct Ncv Dec Date

~ ~

e 0

0-

~ ~

IMPROVEMENTS/ACTIONS

,

r vement Improve Procedure Quality and Revision Process:

Temporary Change Reduction Complete Convert Non-safety Procedures to Guidelines Corrrplete

~ Monitor Quality of Upgmded OPS/Maintenance Procedures Complete Improve the Safety Focus of the FRG:

~ Improve consistency and membership Complete

~. Reduce Volume On-gong Tech Spec Admin Section Change 12/31/96 Improve Plant's ability to Implement E-Plan

~ Upgmde/Revs the ERO 8/30/96

~ Implement more &xpent; limited scope drills 9/30/96

~ Enhance EP Training 12/1/96 Implement Revised Configuration Control Process

~

Configuration Management Enforcement Conference Preps 7/26/96

~ Establish Configuration Control Group/mission/process Complete

~ Revise design control procedures 8/15/96

~ - Initiate RTSI. for minor mods Complete

~ Identify Unit 2 Outage Top 20 %ork Items Complete Improve Site Training Integrate outside perspective into organization Complete 1

'levate

Training Standards/Reinforcement 'n-gourg Establish Method to determine Training Effectiveness 7/31/96 53

TEMPORARY CHANGES TO PROCEDURES Jim Holt - Information Services 350 Legend Good

~Untt 1

~Unit2

300

~common 250 X Total Target O~ 200 0

0 150 X

100 50 Oct Dec Feb Apr Jun Aug Oct Dec Date Data Source: Jtm Holt

SUMMARY

STATUS Oldest TC Unit 1 Unit 2 Common Total Discipline (days) 27 0 erations 26 Mechanical 0 0 26 Electrical 0 0 27 I&C 0 0 Reactor En . 0 0 0 0 SCE 0 0 0 0

0. HP 0 0 0 0

PSL TRAINING OBSERVATIONS 100%%d 904%%d 80/o

~Actual 70%%d g 60%%d g So%%d 4o%%d 30%

20/a 10%%d 0%%d g~~i P19S1V+992; QS93; @99~4 51995,i 5~% R2/963 ~~ Q/96K g$ 96T -6/96~; 7/966 ~~q xhl96~ rio/96',81/96- f52/96-OA~WctM~ 100% 85% 0% 2% S5% 100% 100% 91%

Data Source: M. Allen 55

t ~

O.

0 0-

s ~ ~ ~

.

CO CTIVE ACTION PROG

, CONDITION REPORT PROCESS STATUS

  • VOLUME CONTINUES TO BE HIGH CR's GENERATED BY QUARTER 1500 1000 O

o 50

%h 1ST 2nd 401 1st 2nd 3'TR QTR QTR QTR QTR QTR 95 96 TOP SOURCES FOR 2ND QUARTER OPERATIONS QUALITYASSURANCE ENGINEERING IC

" SIGNIFICANT CRs REVIEWED AT 0730 MANAGEMENTMEETING, ALLCRs APPROVED BY PGM

  • 2ND QUARTER TREND REPORT DRAFT ISSUE MANAGEMENTREVIEW PRESENT TO NRC JULY 26 AUGUST 7 AUGUST 29
  • AREAS FOR IMPROVEMENT- CORRECTIVE ACTION PROGRAM

- REVIEW OF COMPLETED CRs SHOW INCONSISTENT LEVEL OF ROOT CAUSE

- BETTER TIE WITH ROOT CAUSE PROCEDURE (LEVELS Of ROOT CAUSE TIED TO SIGNIFICANCE OF PROBLEM)

- MORE WIDESPREAD TRAINING NEEDED ON PROCEDURE/PIC HANDBOOK

- PROBLEM REPORT TIMELINESS 56

~ J

.

~ OVERALLASSESSMENT Corrective actions is considered a limiting weakness and rcxruires increased management attention Personnel errors, attention to detail and procedural adherence are continuing problems

'Ihe operating expeoence feedback program (OEF) and the foreign material exclusion program (FME) are unsatisfactory Our inability to curb the trend of recurring problems is indicative of ineffective correchve actions and less than adequate when determining

. underlying causal factors QA AUDITS/PERFORMANCE MONITORING (AUGMENTED BY IB/PSL QA/QC PERSONNEL)

Second quarter 96: 7 Audits, 25 Finding, 80 Condition Reports Programs and Procedures are not sufEcient to preclude problems fern occurring (Procedure Quality)

Procedures are not being followed with rigor (Human Performance) 13 Finding Responses late to QA. Process change with VP sign off Rejected

- by Site VP due to shallowness of response

~ INDEPENDENT TECHNICALREVIEWS Second quarter '96: 7 ITRs, 38 Recommendations, 11 Condition Reports

- Conduct crews of Operations acceptable, however, inconsistencies exist between 57

QUAIXIYASSURANCE (continued)

O.

OEF program is not effective in reducing severity and renurence of events PME programmatic controls have improved, however, cultural and personnel behavior changes are requned to achieve desired results QC INSPECIIONS/SURVEKLANCES Second quarter deficiencies rate 7.5% down Rom 8% 1st quarter '96 1363 surveillance/inspections with 102 deficiencies (most outage related), 71 Condition Reports Use of template and underwater repair methodologies for Rx vessel Qange resulted in major man-rem and budget savings 0-58

\ l

.

r.zcmsING C

n

,~

O.

0-

REGULATORYCOMPLIANCE STATUS and AGENDA Recent NIRC lns ections as of June 30 $ 996 RESIDENTS'ERIODIC: 3-30-96 through 5-11-96 and 5-12-96 through 6-8-96 (5 inspectors per report)

EMPLOYEE CONCERNS PROGRAM: 4-29-96 through 5-3-96 (4 inspectors)

PHYSICAL SECURITY PROGRAM FOR POWER REACTORS: 4-30-96 through 5-3-96 (1 inspector)

Estimated NRC ins ector man-hours as of March 31 1996: 3978 Violations Sfafus as of June 30 1996 Nine Cited Violations Ten Non-Cited Violations Potential. Violations Pending

1) Configuration Control InadequaciesNiolations Potential Nonited Violations Pending
1) Licensee made a change to the facility without a 10 CFR 50.59 evaluation
2) Wide Range Nls inoperable for surveillance during Core Alterations (LER 335/96-05)
3) Maintenance performed without a stamped controlled version of a procedure
4) A temporary modiTication to an EDG was made and independently verNed incorrectly U comin Ins ecfions fhrou h Se fember f996 CEDMCS PROBLEMS: One Week - 7/8/96 (Two Inspectors)

ENGINEERING (FSAR CORRECTIVE ACTIONS): One Week -7/22/96 NRC REGION II SECTION CHIEF SITE VISIT: Two Days - Week of 7/29/96 SENIOR RESIDENT INSPECTOR OBJECTIVITY VISIT: One Week- 8/5/96 RADIOLOGICALPROGRAM: One Week - 8/5/96 MAINTENANCEIMPLEMENTATION: One Week- 8/19/96 LICENSED OPERATOR REQUALIFICATIONPROGRAM EVALUATION: One Week - 9/9/96

0 PHYSICAL SECURITY PROGRAM:

OCCUPATIONAL RADIATIONEXPOSURE:

One Week - 9/9/96 One Week - 9/9/96 MAINTENANCERULE INSPECTION PROCEDURE: One Week - 9/16/96 (Five Inspectors) 59

NRC VIOLATIONS I

0 0 0 ~ ~ 0 0 0 0 ~ ~ 0 ~ ~

15 14 Legend

~Aclual Violaltons Actual NCV's 10

+10 0

0 O

2 5 0

Jan Feb Mar- Apr May Jun Jul Aug Sep Oct Nov Dec

'86 Date-Date Source: E. Weinkarn l l ~ ~

r ~ ~ 1

LICENSEE EYENT REPORTS 20 Legend 15

~10 CFR 6073 LER 10 CFR 50.72 15 Good ul C.

~IO S.

cr z0 0

Jan Feb Mar Apr May Jun Jul Aug Sep Oct Nov Dec

'S6 Date Data Source: Ed Weinkam

Operating Experience Feedback FOP's TO BE PROCESSED 30 Good 25 23 20 15 ~Actual o

10 Jan Feb Mar Apr May Jun Jul Aug Sept Oct Nov Dec Time (Month)

FOP's TO BE CLOSED (CLOSE OUT SUNIMARY) 35 30 Good 25 20 0 ~Actual 15 12 10 Jan Feb Mar Apr May Jun Jul Aug Sept Oct Nov Dec Time (Month)

~ ~ y 1