ML18353B268: Difference between revisions

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* H 1 egulatory Dodtet File consumers Power company General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201
* Hegulatory Dodtet File 1
* Area Code 517 788-0550 Directorate of Licensing US Nuclear Regulatory Commission Washington, DC 20555 Gentlemen:
* consumers
Re: Docket License DPR-20 Palisades Plant -A0-11-75 Attached is Abnormal Occurrence Report A0-11-75 which volves a safety setting on the linear power channel of the reactor protective system. The analysis of the occurrence concluded that there was no significant effect on safety . DAB/ds CC: JGKeppler, USNRC Yours very truly, Ralph B. Sewell Nuclear Licensing Administrator   
* Power company General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201
* *
* Area Code 517 788-0550 Directorate of Licensing                               Re:    Docket US Nuclear Regulatory Commission                               License DPR-20 Washington, DC 20555                                           Palisades Plant - A0-11-75 Gentlemen:
* I . ** ABNORMAL OCCURRENCE REPORT Palisades Plant
Attached is Abnormal Occurrence Report A0-11-75 which in-volves a safety setting on the linear power channel of the reactor protective system. The analysis of the occurrence concluded that
* 1. Report No: A0-11-75, Docket 50-255 2a. Report Date: May 30, 1975 2b. Occurrence Date: May 29, 1975 3. Facility:
* there was no significant effect on safety .
Palisades Plant, Covert, Michigan 4. Identification of Occurrence:
Yours very truly, DAB/ds                                      Ralph B. Sewell Nuclear Licensing Administrator CC: JGKeppler, USNRC
Linear power channel reactor protective system setting above technical specifications set point. 5. Conditions Prior to Occurrence:
*
Plant operating at steady-state 80 percent thermal power. 6. 7. 8. 9. 10. Description of Occurrence:
 
While performing monthly surveillance cedure MD-1, it was found that Channel NI-005 trip point was above the Technical Specifications limit, Table 2.3.1, of less than or equal to 106.5 percent by 0.3 percent. The set point was corrected . The linear power channel drawer was replaced with a spare. Designation of Apparent Cause of Occurrence:
                        **                               *
Component Failure -Channel, Internal Positive 15-Volt Power Supply. Analysis of Occurrence:
* ABNORMAL OCCURRENCE REPORT Palisades Plant
The reactor protection system is a 2 out of 4 system. Inasmuch as only one channel was affected, the system remained functional.
: 1. Report No:   A0-11-75, Docket 50-255 2a. Report Date: May 30, 1975 2b. Occurrence Date:   May 29, 1975
In addition, the set point was at plus 106.8 percent whereas the safety analysis, FSAR Section 14.1, assumed a power level of 112 percent. We have concluded that this occurrence had no cant effect on plant safety. Corrective Action: Repair failed component.
: 3. Facility: Palisades Plant, Covert, Michigan
Our records indicate that this is only the second failure out of 13 units in 6 years; thus, we have concluded no further action is required.
: 4. Identification of Occurrence: Linear power channel reactor protective system setting above technical specifications set point.
Failure Data: a. Previous Failure -Similiar Unit 10/5/72. b. Equipment Identification  
: 5. Conditions Prior to Occurrence:   Plant operating at steady-state 80 percent thermal power.
-Technipower Power Supply Model 227-4170 .}}
: 6. Description of Occurrence: While performing monthly surveillance Pro-cedure MD-1, it was found that Channel NI-005 trip point was above the Technical Specifications limit, Table 2.3.1, of less than or equal to 106.5 percent by 0.3 percent.
* The set point was corrected .
The linear power channel drawer was replaced with a spare.
: 7. Designation of Apparent Cause of Occurrence: Component Failure -
Channel, Internal Positive 15-Volt Power Supply.
: 8. Analysis of Occurrence: The reactor protection system is a 2 out of 4 system. Inasmuch as only one channel was affected, the system remained functional. In addition, the set point was at plus 106.8 percent whereas the safety analysis, FSAR Section 14.1, assumed a power level of 112 percent. We have concluded that this occurrence had no signifi-cant effect on plant safety.
: 9. Corrective Action: Repair failed component. Our records indicate that this is only the second failure out of 13 units in 6 years; thus, we have concluded no further action is required.
: 10. Failure Data:
: a. Previous Failure - Similiar Unit 10/5/72.
: b. Equipment Identification - Technipower Power Supply Model 227-4170 .
I .
    *}}

Revision as of 08:57, 20 October 2019

06/09/1975 Letter Submitting Abnormal Occurrence Report AO-11-75 Which Involves Safety Setting on Linear Power Channel of Reactor Protective System
ML18353B268
Person / Time
Site: Palisades Entergy icon.png
Issue date: 06/09/1975
From: Sewell R
Consumers Power Co
To:
Office of Nuclear Reactor Regulation
References
LER 1975-011-00
Download: ML18353B268 (2)


Text

,.

  • Hegulatory Dodtet File 1
  • consumers
  • Power company General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201
  • Area Code 517 788-0550 Directorate of Licensing Re: Docket US Nuclear Regulatory Commission License DPR-20 Washington, DC 20555 Palisades Plant - A0-11-75 Gentlemen:

Attached is Abnormal Occurrence Report A0-11-75 which in-volves a safety setting on the linear power channel of the reactor protective system. The analysis of the occurrence concluded that

  • there was no significant effect on safety .

Yours very truly, DAB/ds Ralph B. Sewell Nuclear Licensing Administrator CC: JGKeppler, USNRC

    • *
  • ABNORMAL OCCURRENCE REPORT Palisades Plant
1. Report No: A0-11-75, Docket 50-255 2a. Report Date: May 30, 1975 2b. Occurrence Date: May 29, 1975
3. Facility: Palisades Plant, Covert, Michigan
4. Identification of Occurrence: Linear power channel reactor protective system setting above technical specifications set point.
5. Conditions Prior to Occurrence: Plant operating at steady-state 80 percent thermal power.
6. Description of Occurrence: While performing monthly surveillance Pro-cedure MD-1, it was found that Channel NI-005 trip point was above the Technical Specifications limit, Table 2.3.1, of less than or equal to 106.5 percent by 0.3 percent.
  • The set point was corrected .

The linear power channel drawer was replaced with a spare.

7. Designation of Apparent Cause of Occurrence: Component Failure -

Channel, Internal Positive 15-Volt Power Supply.

8. Analysis of Occurrence: The reactor protection system is a 2 out of 4 system. Inasmuch as only one channel was affected, the system remained functional. In addition, the set point was at plus 106.8 percent whereas the safety analysis, FSAR Section 14.1, assumed a power level of 112 percent. We have concluded that this occurrence had no signifi-cant effect on plant safety.
9. Corrective Action: Repair failed component. Our records indicate that this is only the second failure out of 13 units in 6 years; thus, we have concluded no further action is required.
10. Failure Data:
a. Previous Failure - Similiar Unit 10/5/72.
b. Equipment Identification - Technipower Power Supply Model 227-4170 .

I .