ML18348A214: Difference between revisions

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{{#Wiki_filter:* * *
* consumers Power *Company ;-;-:--, , ..........
r 7--,7 L;ic...,p0**:.;kii.:.::zL General Offices: 212 West Michigan Avenue, .Jackson, Michigan-49201
* Area Code 517 788-0550 October 4, l977 Mr James G Keppler Office of Inspection and Inforcement Region III US Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60l37 DOCKET 50-255, LICENSE DPR-20 PALISADES PLANT .,.. CORRECTED ER.,-77-034 AND ER-77-041 Licensee Event Report 77-034 reported an apparent high level in safety injection tank SI-82C. In the "cause description" portion of the report, we stated that testing would be performed.to determine the path of apparent leakage. In August, we determined that the cause of the low level indication was not in leakage, but instead was faulty indication.
Inasmuch as the leakage testing initially*
proposed is no longer applicable, an updated LER is attached to clarify the* record. Licensee Event Report 77-041 did not present a clear sequence of events leading to the low fuel inventory.
A corrected LER is attached to identify the proper cause description.
David P Hoffman ( S.igned) David P Hoffman Assistant Nuclear Licensing Administrator CC: ASchwencer, USNRC ---------------
.. -* u:iarE -PREVIOUS REPOR'l' DATE 08-01-* . *LICENSEE EVENT
* REPORT CORRECTED Palisades eoNTROL BLOCK: I I I I I I I (PLEASE PRINT ALL REQUIRED INFORMATION]
NAME LICENSEE I MI I I Pl A I L I 1 I 7 8 9 14 REPORT TYPE. 1 6 LICENSE NUMBER I o I o 1-1 o I o I o I o I ol-1 o I o I 15 25 REPORT SOURCE DOCKl;T NUMBER LICENSE TYPE 14111111111 26 30 EVENT OATE EVENT TYPE I o I 3 I 31 32 REPORT DATE @TI]coN'T l *I *I 7 8 57 58 lLJ LrJ lolslol-lol2l sl sl I ol 11 ol s1 11 ] lol912l917171 59 so 68 69 74 75 80 EVENT DESCRIPTION
@:lfil I T-82C safety injectiqn tank level was found to be 1% above Technical Specifications 7 8 9 10131 I limits. 7 8 9 The tank was drained to bring indicated level back within Technical lol4l I Specifications limits. (ER-77-034) 7 8 9 I 80 I 80 I 80 7 8 9...._ ____________________________________________________________________________________
__,80 lolsl 7 8 9 SYSTEM CODE @El Isl Fl CAUSE CODE COMPONENT CODE l!J I Al c I cl d MI u I 7 8 s 10 11 12 17 CAUSE DESCRIPTION PRIME COMPONENT SUPPLIER w 43 COMPONENT MANUFACTURER I z I 9 I 9 I 9 I 44 47 80 VIOLATION L1LI 48 I investigation revealed that the cause of the event was faulty indication.
I 7 8 9 80 I The indication has been restored to normal and no further action is contemplated.
I 7 8 9 r. I (Reference LER 77-40) 8 9 FACILITY EE] 7 8 rn STATUS LI_] 9 FORM OF ACTIVITY RELEASED w % PO'NER OTHER STATUS I 1 I 0 I 0 I I N /A I 10 12 13 44 CONTENT OF RELEASE AMOUNT OF ACTIVITY w I N/A. l METHOD OF DISCOVERY 45 46 N/A 7 8 9 10 11 44 45 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION ITEi 10101.01 l.!J I N/A 7 8 9 11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTION tlO I 80 DISCOVERY DESCRIPTION llLA 80 LOCATION OF RELEASE 80 80 rn 1o1 o 1 01. N/A. 7 8 9 11 PROBABLE CONSEQUENCES lill] I N /A 7 8 9 80 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION
[]]]_ U_J 7 8 9 10 tlO PUBLICITY ITIZJ I N/A 7 8 9 BO A,..., ADDITIONAL FACTORS 7 8 9 80 GE 7 8 9 80 
-.. .LICENSEE EVENT REPORT
* CORRECTED Palisades
*
* caw AOL BLOCK: I 1 I I I I [PLEASE PRINT ALL REQUIRED INFORMATION]
6 LICENSE NUMBER lo lo 1-lol ol ol ol ol-lo lo I 15 25 REPORT REPORT TYPE SOURCE OOCKJ;T NUMBER LICENSE TYPE 14111111!11 26 30 EVENT DATE EVENT TYPE Io I 1 I 31 32 REPORT OATE @IT]coN'T r
* I
* I 7 8 57 58 L!J 1015 lo I-lo 1215151 I o I 8 I 21 3 I 11 11 lol2lol2l1l1I 59 60 . 61 68 69 74 75 80 EVENT DESCRIPTION
@lfil I At 1600 on 8/23/77, during routine start-up operations, the level in the diesel oil 7 8 9 @El I storage tank, T-10, had decreased to 53 percent. 80 This is the level that provides the I 7 8 9 . loj41 I minimum required volume of 16 ,000 gallons as specified in Technical Specifications 7 8 9 @Jfil I 3. 7 .1. i for heatup above 325°F. Plant cooldown commenced immediately.
At 1800 oil 7 8 9 . '
lfil§] I was delivered and heatup resumed. Problem is not repetit*ive. (ER-77-041) 7 8 9 SYSTEM CAUSE CODE COOE COMPONENT CODE @El I El E I LEJ I x Ix I x I xi xi zj 7 8 9 10 11 12 17 CAUSE DESCRIPTION PRIME COMPONENT SUPPLIER w 43 COMPONENT MANUFACTURER I z I 9 I 9 I 9 I 44 47 VIOLATION w 48 80 I 80 I 80 I 80 ._I _F_u_e_l_h_a_d_b_ee_n_o_r_d_e_r_e_d_o_n_th_e_m_o_r_n_i_n..:;;g'--o_f_8.:.../2_2...;/_7.:...7.:...'=--b_u_t_t_h_e_su
.... p=-p._l_i_*
e_r_f_a_i_l_e_d_t_o_d_e_l_i_* 7 8 9 80 lo191 I that day. Delivery was further delayed on 8/23/77 because of difficulty in obtaining I 7 8 9 80 .. I a delivery vehicle. Correspondence to the supplier stressing the need for (Contd) I 8 9 80 FACILITY METHOD OF STATUS % POWER OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION EEi W . lo I 0 I 0 I I Routine Start-Up I LJJ I N/A. 7 8 9 10 12 13 44 45 46 80 FORM OF ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY w ._I _...N""""/
A..._, ______ __...,. 9 10 11 44 rn 7 8 LOCATION OF RELEASE 45 N/A 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION lolol
________________________________________________
;......J 7 8 9 11 12 13 80 PERSONNEL INJURIES NUMBER DESCRIPTION rn 1 o , a 1 a 1 .__N __ /_A ___________________________
.....,...,..,. 7 8 9 11 12 . 80 PROBABLE CONSEQUENCES lIJfil None 7 8 9 80 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION IIfil 7 8 9 10 PUBLICITY
[ill} N/A 7 8 9 ADDITIONAL FACTORS I Cause Description (Contd) -urgency in making deliveries is expected to forestall 7 8 9 (Tifil I future delivery problems. 7 8 9 80 80 80 I 80}}

Revision as of 17:35, 12 September 2019

Corrected LER 1977-034-00 to Clarify Leakage Testing & LER 1977-041-00 to Identify Proper Cause Description of Low Fuel Inventory
ML18348A214
Person / Time
Site: Palisades Entergy icon.png
Issue date: 10/04/1977
From: Hoffman D
Consumers Power Co
To: James Keppler
NRC/RGN-III
References
LER 1977-034-00, LER 1977-041-00
Download: ML18348A214 (3)


Text

  • * *
  • consumers Power *Company ;-;-:--, , ..........

r 7--,7 L;ic...,p0**:.;kii.:.::zL General Offices: 212 West Michigan Avenue, .Jackson, Michigan-49201

  • Area Code 517 788-0550 October 4, l977 Mr James G Keppler Office of Inspection and Inforcement Region III US Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60l37 DOCKET 50-255, LICENSE DPR-20 PALISADES PLANT .,.. CORRECTED ER.,-77-034 AND ER-77-041 Licensee Event Report 77-034 reported an apparent high level in safety injection tank SI-82C. In the "cause description" portion of the report, we stated that testing would be performed.to determine the path of apparent leakage. In August, we determined that the cause of the low level indication was not in leakage, but instead was faulty indication.

Inasmuch as the leakage testing initially*

proposed is no longer applicable, an updated LER is attached to clarify the* record. Licensee Event Report 77-041 did not present a clear sequence of events leading to the low fuel inventory.

A corrected LER is attached to identify the proper cause description.

David P Hoffman ( S.igned) David P Hoffman Assistant Nuclear Licensing Administrator CC: ASchwencer, USNRC ---------------

.. -* u:iarE -PREVIOUS REPOR'l' DATE 08-01-* . *LICENSEE EVENT

  • REPORT CORRECTED Palisades eoNTROL BLOCK: I I I I I I I (PLEASE PRINT ALL REQUIRED INFORMATION]

NAME LICENSEE I MI I I Pl A I L I 1 I 7 8 9 14 REPORT TYPE. 1 6 LICENSE NUMBER I o I o 1-1 o I o I o I o I ol-1 o I o I 15 25 REPORT SOURCE DOCKl;T NUMBER LICENSE TYPE 14111111111 26 30 EVENT OATE EVENT TYPE I o I 3 I 31 32 REPORT DATE @TI]coN'T l *I *I 7 8 57 58 lLJ LrJ lolslol-lol2l sl sl I ol 11 ol s1 11 ] lol912l917171 59 so 68 69 74 75 80 EVENT DESCRIPTION

@:lfil I T-82C safety injectiqn tank level was found to be 1% above Technical Specifications 7 8 9 10131 I limits. 7 8 9 The tank was drained to bring indicated level back within Technical lol4l I Specifications limits. (ER-77-034) 7 8 9 I 80 I 80 I 80 7 8 9...._ ____________________________________________________________________________________

__,80 lolsl 7 8 9 SYSTEM CODE @El Isl Fl CAUSE CODE COMPONENT CODE l!J I Al c I cl d MI u I 7 8 s 10 11 12 17 CAUSE DESCRIPTION PRIME COMPONENT SUPPLIER w 43 COMPONENT MANUFACTURER I z I 9 I 9 I 9 I 44 47 80 VIOLATION L1LI 48 I investigation revealed that the cause of the event was faulty indication.

I 7 8 9 80 I The indication has been restored to normal and no further action is contemplated.

I 7 8 9 r. I (Reference LER 77-40) 8 9 FACILITY EE] 7 8 rn STATUS LI_] 9 FORM OF ACTIVITY RELEASED w % PO'NER OTHER STATUS I 1 I 0 I 0 I I N /A I 10 12 13 44 CONTENT OF RELEASE AMOUNT OF ACTIVITY w I N/A. l METHOD OF DISCOVERY 45 46 N/A 7 8 9 10 11 44 45 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION ITEi 10101.01 l.!J I N/A 7 8 9 11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTION tlO I 80 DISCOVERY DESCRIPTION llLA 80 LOCATION OF RELEASE 80 80 rn 1o1 o 1 01. N/A. 7 8 9 11 PROBABLE CONSEQUENCES lill] I N /A 7 8 9 80 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION

[]]]_ U_J 7 8 9 10 tlO PUBLICITY ITIZJ I N/A 7 8 9 BO A,..., ADDITIONAL FACTORS 7 8 9 80 GE 7 8 9 80

-.. .LICENSEE EVENT REPORT

  • CORRECTED Palisades
  • caw AOL BLOCK: I 1 I I I I [PLEASE PRINT ALL REQUIRED INFORMATION]

6 LICENSE NUMBER lo lo 1-lol ol ol ol ol-lo lo I 15 25 REPORT REPORT TYPE SOURCE OOCKJ;T NUMBER LICENSE TYPE 14111111!11 26 30 EVENT DATE EVENT TYPE Io I 1 I 31 32 REPORT OATE @IT]coN'T r

  • I
  • I 7 8 57 58 L!J 1015 lo I-lo 1215151 I o I 8 I 21 3 I 11 11 lol2lol2l1l1I 59 60 . 61 68 69 74 75 80 EVENT DESCRIPTION

@lfil I At 1600 on 8/23/77, during routine start-up operations, the level in the diesel oil 7 8 9 @El I storage tank, T-10, had decreased to 53 percent. 80 This is the level that provides the I 7 8 9 . loj41 I minimum required volume of 16 ,000 gallons as specified in Technical Specifications 7 8 9 @Jfil I 3. 7 .1. i for heatup above 325°F. Plant cooldown commenced immediately.

At 1800 oil 7 8 9 . '

lfil§] I was delivered and heatup resumed. Problem is not repetit*ive. (ER-77-041) 7 8 9 SYSTEM CAUSE CODE COOE COMPONENT CODE @El I El E I LEJ I x Ix I x I xi xi zj 7 8 9 10 11 12 17 CAUSE DESCRIPTION PRIME COMPONENT SUPPLIER w 43 COMPONENT MANUFACTURER I z I 9 I 9 I 9 I 44 47 VIOLATION w 48 80 I 80 I 80 I 80 ._I _F_u_e_l_h_a_d_b_ee_n_o_r_d_e_r_e_d_o_n_th_e_m_o_r_n_i_n..:;;g'--o_f_8.:.../2_2...;/_7.:...7.:...'=--b_u_t_t_h_e_su

.... p=-p._l_i_*

e_r_f_a_i_l_e_d_t_o_d_e_l_i_* 7 8 9 80 lo191 I that day. Delivery was further delayed on 8/23/77 because of difficulty in obtaining I 7 8 9 80 .. I a delivery vehicle. Correspondence to the supplier stressing the need for (Contd) I 8 9 80 FACILITY METHOD OF STATUS % POWER OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION EEi W . lo I 0 I 0 I I Routine Start-Up I LJJ I N/A. 7 8 9 10 12 13 44 45 46 80 FORM OF ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY w ._I _...N""""/

A..._, ______ __...,. 9 10 11 44 rn 7 8 LOCATION OF RELEASE 45 N/A 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION lolol

________________________________________________

......J 7 8 9 11 12 13 80 PERSONNEL INJURIES NUMBER DESCRIPTION rn 1 o , a 1 a 1 .__N __ /_A ___________________________

.....,...,..,. 7 8 9 11 12 . 80 PROBABLE CONSEQUENCES lIJfil None 7 8 9 80 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION IIfil 7 8 9 10 PUBLICITY

[ill} N/A 7 8 9 ADDITIONAL FACTORS I Cause Description (Contd) -urgency in making deliveries is expected to forestall 7 8 9 (Tifil I future delivery problems. 7 8 9 80 80 80 I 80