ENS 40250: Difference between revisions

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| event date = 10/15/2003 16:03 EDT
| event date = 10/15/2003 16:03 EDT
| last update date = 10/15/2003
| last update date = 10/15/2003
| title = Feedwater  Regulating Valve Issue Forces  Initiation Of Technical Specification  Shutdown
| title = Feedwater  Regulating Valve Issue Forces  Initiation of Technical Specification  Shutdown
| event text = At 1603 Salem Unit 1 commenced a down power to comply with Technical Specifications. Tech. Spec. 3.0.3.  was entered at 1505 when it was determined that the feed regulation valve for the 14 Steam generator (14BF19) was bound at approximately 71% open. This valve is required to close on a feedwater isolation signal. Currently the reactor is at 40% power and lowering with plans to stabilize at 25% prior to taking the unit off line (mode 3) by 2205 tonight.
| event text = At 1603 Salem Unit 1 commenced a down power to comply with Technical Specifications. Tech. Spec. 3.0.3.  was entered at 1505 when it was determined that the feed regulation valve for the 14 Steam generator (14BF19) was bound at approximately 71% open. This valve is required to close on a feedwater isolation signal. Currently the reactor is at 40% power and lowering with plans to stabilize at 25% prior to taking the unit off line (mode 3) by 2205 tonight.
Unit 1 has no other tech spec equipment out of service. Unit 1 is in two additional shutdown Technical Specifications, both are related to the control room ventilation system which is shared with Unit 2. Unit 2 is in a scheduled refueling outage and one of the Unit 2 emergency intake dampers is disabled (T.S. 3.7.6.1.a). This is a 7 day LCO that expires on 10/22/03.  Additionally Unit 2's emergency filtration system is out of service for planned maintenance (T.S 3.7.6.1.a). This is a 30 day LCO that expires on 11/13/03. All other systems on Unit 1 are operating as expected for current plant conditions.
Unit 1 has no other tech spec equipment out of service. Unit 1 is in two additional shutdown Technical Specifications, both are related to the control room ventilation system which is shared with Unit 2. Unit 2 is in a scheduled refueling outage and one of the Unit 2 emergency intake dampers is disabled (T.S. 3.7.6.1.a). This is a 7 day LCO that expires on 10/22/03.  Additionally Unit 2's emergency filtration system is out of service for planned maintenance (T.S 3.7.6.1.a). This is a 30 day LCO that expires on 11/13/03. All other systems on Unit 1 are operating as expected for current plant conditions.

Latest revision as of 22:25, 1 March 2018

ENS 40250 +/-
Where
Salem PSEG icon.png
New Jersey (NRC Region 1)
Reporting
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Time - Person (Reporting Time:+-0.55 h-0.0229 days <br />-0.00327 weeks <br />-7.5339e-4 months <br />)
Opened: Joe Sullivan
19:30 Oct 15, 2003
NRC Officer: Rich Laura
Last Updated: Oct 15, 2003
40250 - NRC Website
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