ENS 45434: Difference between revisions

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| event date = 10/15/2009 12:25 EDT
| event date = 10/15/2009 12:25 EDT
| last update date = 10/15/2009
| last update date = 10/15/2009
| title = Unit Commenced Shutdown Due To Inoperable Division 2 Emergency Service Water System
| title = Unit Commenced Shutdown Due to Inoperable Division 2 Emergency Service Water System
| event text = This event is being reported in accordance with 10CFR50.72(b)(2)(i).  On October 15, 2009, at approximately 1225 hours, the Perry Nuclear Power Plant commenced a Technical Specification required plant shutdown.
| event text = This event is being reported in accordance with 10CFR50.72(b)(2)(i).  On October 15, 2009, at approximately 1225 hours, the Perry Nuclear Power Plant commenced a Technical Specification required plant shutdown.
On October 14, 2009, At 1747 hours, the Division 2 Emergency Service Water (ESW) system was declared inoperable and unavailable for planned work. The plant entered Technical Specification (TS) 3.7.1 Action A for one inoperable ESW Division.  Other supported TSs were also entered (TS 3.8.1 for the Division 2 diesel generator, TS 3.6.1.7 for Containment Spray 'B', TS 3.6.2.3 for Suppression Pool Cooling 'B', TS 3.7.10 for Emergency Closed Cooling 'B', TS 3.5.1 for LPCI 'B' & 'C', among others).
On October 14, 2009, At 1747 hours, the Division 2 Emergency Service Water (ESW) system was declared inoperable and unavailable for planned work. The plant entered Technical Specification (TS) 3.7.1 Action A for one inoperable ESW Division.  Other supported TSs were also entered (TS 3.8.1 for the Division 2 diesel generator, TS 3.6.1.7 for Containment Spray 'B', TS 3.6.2.3 for Suppression Pool Cooling 'B', TS 3.7.10 for Emergency Closed Cooling 'B', TS 3.5.1 for LPCI 'B' & 'C', among others).

Latest revision as of 21:11, 1 March 2018

ENS 45434 +/-
Where
Perry FirstEnergy icon.png
Ohio (NRC Region 3)
Reporting
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
LER: 05000440/LER-2009-003
Time - Person (Reporting Time:+-1.63 h-0.0679 days <br />-0.0097 weeks <br />-0.00223 months <br />)
Opened: Michael Nemcek
14:47 Oct 15, 2009
NRC Officer: Steve Sandin
Last Updated: Oct 15, 2009
45434 - NRC Website
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