ENS 48676: Difference between revisions
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| event date = 01/15/2013 21:12 EST | | event date = 01/15/2013 21:12 EST | ||
| last update date = 01/16/2013 | | last update date = 01/16/2013 | ||
| title = Loss | | title = Loss of a 4160 Volt Bus While Performing Testing | ||
| event text = On January 15, 2013 at 2112 EST while performing testing associated with the remote shutdown system at the James A. FitzPatrick Nuclear Power Plant, an unexpected loss of the 10600 bus 'B' division AC vital power system occurred. This loss of power to the 10600 bus resulted in an automatic actuation of the 'B' and 'D' Emergency Diesel Generators. The diesel generators started as expected, but did not close in to energize the 10600 Bus due to the configuration at the time of the event. As a result of the loss of the 10600 bus, the 'B' Reactor Protection System (RPS) lost power resulting in a half scram signal and a Group II Primary Containment Isolation System (PCIS) actuation. This actuation resulted in closing containment isolation valves in multiple systems and isolating Reactor Water Clean-Up (RWCU). Based on these system actuations, the event is reportable under criterion 10 CFR 50.72(b)(3)(iv). | | event text = On January 15, 2013 at 2112 EST while performing testing associated with the remote shutdown system at the James A. FitzPatrick Nuclear Power Plant, an unexpected loss of the 10600 bus 'B' division AC vital power system occurred. This loss of power to the 10600 bus resulted in an automatic actuation of the 'B' and 'D' Emergency Diesel Generators. The diesel generators started as expected, but did not close in to energize the 10600 Bus due to the configuration at the time of the event. As a result of the loss of the 10600 bus, the 'B' Reactor Protection System (RPS) lost power resulting in a half scram signal and a Group II Primary Containment Isolation System (PCIS) actuation. This actuation resulted in closing containment isolation valves in multiple systems and isolating Reactor Water Clean-Up (RWCU). Based on these system actuations, the event is reportable under criterion 10 CFR 50.72(b)(3)(iv). | ||
Power to the 10600 Bus was restored January 16, 2013 at 0400 EST, and the half scram and isolation signals have been reset. Additional actions to restore systems to a normal operating line-up are on-going. Investigation into the cause of the unexpected power loss is on-going and will be addressed through the corrective action program. | Power to the 10600 Bus was restored January 16, 2013 at 0400 EST, and the half scram and isolation signals have been reset. Additional actions to restore systems to a normal operating line-up are on-going. Investigation into the cause of the unexpected power loss is on-going and will be addressed through the corrective action program. |
Latest revision as of 21:02, 1 March 2018
Where | |
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Fitzpatrick New York (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+2.52 h0.105 days <br />0.015 weeks <br />0.00345 months <br />) | |
Opened: | Steve Defillippo 04:43 Jan 16, 2013 |
NRC Officer: | Mark Abramovitz |
Last Updated: | Jan 16, 2013 |
48676 - NRC Website
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