ML19320A072: Difference between revisions
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,h. UCENSEE EVENT REPOR m CONTROL BLCCK:l l l l l l l [Pt. EASE PRINT ALL REOlJIMED INPomatATIO98) | ,h. UCENSEE EVENT REPOR m CONTROL BLCCK:l l l l l l l [Pt. EASE PRINT ALL REOlJIMED INPomatATIO98) | ||
(0 \ | (0 \ | ||
| Line 25: | Line 24: | ||
_ .. _ E. w = | _ .. _ E. w = | ||
@E) I AIR , A IRIK I U 101o1-1o1010101o1-10101 14 I I I il I I I i lol31 32 7 89 14 15 25 26 30 3e CATEGORY Type s DOCKET NUM8EA EVENT DATE AEPORT CAff 0 CON'Tl l I W M 1015101-101311131 1110101317161 lll11o1117161 7 8 57 58 59 60 61 68 69 74 75 80 EVENT DESCRIPTON | @E) I AIR , A IRIK I U 101o1-1o1010101o1-10101 14 I I I il I I I i lol31 32 7 89 14 15 25 26 30 3e CATEGORY Type s DOCKET NUM8EA EVENT DATE AEPORT CAff 0 CON'Tl l I W M 1015101-101311131 1110101317161 lll11o1117161 7 8 57 58 59 60 61 68 69 74 75 80 EVENT DESCRIPTON | ||
!!E lbi . steadv state .oceah . at IM5 . 10 3 % a leak was discovered at a | !!E lbi . steadv state .oceah . at IM5 . 10 3 % a leak was discovered at a 80 l | ||
80 l | |||
7 89 ' | 7 89 ' | ||
0 15ecke{inald,e;,,(3 C)O' elbow u,e11. *,n we 'Pv; ..,' Mali. . P m p ?%c. eu.4;.. re) e c 1 7 89 ' ' ' ' | 0 15ecke{inald,e;,,(3 C)O' elbow u,e11. *,n we 'Pv; ..,' Mali. . P m p ?%c. eu.4;.. re) e c 1 7 89 ' ' ' ' | ||
80' 30 l IIwe . bb b t4sM olkced in sevve'te and the Ne ld on Oe Ph( Such reliN lIwe Wu 80 | 80' 30 l IIwe . bb b t4sM olkced in sevve'te and the Ne ld on Oe Ph( Such reliN lIwe Wu 80 7 89 8 HE Iveca,;rea. %it well failure was re ported previously t w RoR 50-Sit / M-12,.(*>o Bi31%-In l 7 89 80 I | ||
7 89 8 HE Iveca,;rea. %it well failure was re ported previously t w RoR 50-Sit / M-12,.(*>o Bi31%-In l 7 89 80 I | |||
@B L 80 7 89 m, Yes CCOE CCMpONENT CODE VAPM V10uTCN u Icl41 LB] lP lI l P lG lx ix i LAJ IZl919191 11] | @B L 80 7 89 m, Yes CCOE CCMpONENT CODE VAPM V10uTCN u Icl41 LB] lP lI l P lG lx ix i LAJ IZl919191 11] | ||
7 89 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION U lDe b'ilure veaw be cowtWhAfed to Oc & art Ekd khe Y4" FelieE line is NeidIv supo.rked ~ | 7 89 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION U lDe b'ilure veaw be cowtWhAfed to Oc & art Ekd khe Y4" FelieE line is NeidIv supo.rked ~ | ||
7 89 ' | 7 89 ' | ||
80 HE lt.> Lite the 6" sutw. i ce is not ava is muede4 h vibrati.w . A. .w ;tecerroevousw.ars | 80 HE lt.> Lite the 6" sutw. i ce is not ava is muede4 h vibrati.w . A. .w ;tecerroevousw.ars | ||
| Line 47: | Line 41: | ||
LOSS OR DAMAGE TO FAC:UTY fvpf OESCAWTCN Emi NA I-7 89 10 80 PUBUCITY I NA I 7 89 80 A00lTONAL FACTCAS I NA I 89 80 mg I a 0 0 4140 b bE i NAME; CCck N ONE(5 00 M l. 4 199 kEacpp,y "o "b u7 n,...w. i . t o-r s. . _ _ ._. NSP-III-2. Rev. 5 | LOSS OR DAMAGE TO FAC:UTY fvpf OESCAWTCN Emi NA I-7 89 10 80 PUBUCITY I NA I 7 89 80 A00lTONAL FACTCAS I NA I 89 80 mg I a 0 0 4140 b bE i NAME; CCck N ONE(5 00 M l. 4 199 kEacpp,y "o "b u7 n,...w. i . t o-r s. . _ _ ._. NSP-III-2. Rev. 5 | ||
m | m | ||
: 1. Reportable Occurrence Report No. 50-313/76-29 4 | : 1. Reportable Occurrence Report No. 50-313/76-29 4 | ||
: 2. Report Date: November 1, 1976 3. Occurrence Date: October 3, 1976 | : 2. Report Date: November 1, 1976 3. Occurrence Date: October 3, 1976 | ||
: 4. Facility: Arkansas Nuclear One-Unit 1 Russellville, Arkansas | : 4. Facility: Arkansas Nuclear One-Unit 1 Russellville, Arkansas | ||
: 5. Identification 6f Occurrence: | : 5. Identification 6f Occurrence: | ||
Leak in Primary Makeup Pump P36C suction relief line , | Leak in Primary Makeup Pump P36C suction relief line , | ||
4 | 4 | ||
: 6. Conditions Prior to Occurrence: | : 6. Conditions Prior to Occurrence: | ||
3 Steady-State Power X Reactor Power 2542 MWth | 3 Steady-State Power X Reactor Power 2542 MWth Hot Standby Net Output 824 MWe Cold Shutdown Percent of Full Power 99 % | ||
Hot Standby Net Output 824 MWe Cold Shutdown Percent of Full Power 99 % | |||
Refueling Shutdown Load Changes During Routine Power Operation _. | Refueling Shutdown Load Changes During Routine Power Operation _. | ||
Routine Startup.. | Routine Startup.. | ||
| Line 80: | Line 57: | ||
, i | , i | ||
: 7. Description of Occurrence: ~2 At 165S hrs. on 10.3/76, a leak was discovered at a socket weld, pipe to 900 elbow weld, in the primary makeup pump P36C suction relief line. P36C was removed from service and P36B was placed in service. . | : 7. Description of Occurrence: ~2 At 165S hrs. on 10.3/76, a leak was discovered at a socket weld, pipe to 900 elbow weld, in the primary makeup pump P36C suction relief line. P36C was removed from service and P36B was placed in service. . | ||
NSP-III-2, Rev. 5 Attachment "D" S _ | |||
NSP-III-2, Rev. 5 | October 1, 1976 Page 2 of 4 l | ||
Attachment "D" S _ | |||
October 1, 1976 Page 2 of 4 | |||
l | |||
] ., % ) | ] ., % ) | ||
Reportable Occurrence Report No. 50-313/76-29 4 | Reportable Occurrence Report No. 50-313/76-29 4 | ||
: 8. Designation of Apparent Cause of Occurrence: | : 8. Designation of Apparent Cause of Occurrence: | ||
Design x Procedure | Design x Procedure | ||
| Line 103: | Line 67: | ||
; | ; | ||
Construction Component Failure. | Construction Component Failure. | ||
(See Failure D tta) 5 Operator | (See Failure D tta) 5 Operator Other' (specify) | ||
Other' (specify) | |||
This failure could be contributed to the fact that the 3/4" relief line is rigidly supported witile the 6" suction line is subjected to vibration. | This failure could be contributed to the fact that the 3/4" relief line is rigidly supported witile the 6" suction line is subjected to vibration. | ||
i | i | ||
: 9. Analysis of Occurrence: | : 9. Analysis of Occurrence: | ||
Even though only one pump was operable during the time repairs were made, which is allowable by Tech. Spec., there was no ha:ard to the health and safety of the public. | Even though only one pump was operable during the time repairs were made, which is allowable by Tech. Spec., there was no ha:ard to the health and safety of the public. | ||
t | t | ||
. ~; | . ~; | ||
1 October 1, 1976 NSP-III-2, Rev. 5 Attachment "D" 5 Page 3 Of 4 ym . . - . - +- -3.- +- ayy. .,- *.--w-. ,---a- ,------ -- e- e, | |||
1 October 1, 1976 NSP-III-2, Rev. 5 Attachment "D" 5 Page 3 Of 4 | |||
ym . . - . - +- -3.- +- ayy. .,- *.--w-. ,---a- ,------ -- e- e, | |||
. , 7 A | |||
Reportable Occurrence Report No. 50-313/76-29 4 | |||
. , 7 | |||
1 | 1 | ||
: 10. Corrective Action: | : 10. Corrective Action: | ||
The defective weld was repaired. An engineering evaluation is being | The defective weld was repaired. An engineering evaluation is being | ||
,. made and if.necessary modifications will be made to prevent a ! | ,. made and if.necessary modifications will be made to prevent a ! | ||
reoccurrence. - ' | reoccurrence. - ' | ||
4 4 | 4 4 | ||
m. | m. | ||
l l | l l | ||
: 11. Failure' Data: , | : 11. Failure' Data: , | ||
This same weld failure was also reported in ROR #'/6-12. | This same weld failure was also reported in ROR #'/6-12. | ||
i ,I | i ,I | ||
] I i | ] I i | ||
~; | ~; | ||
l i | l i | ||
October 1, 1976 NSP-III-2, Rev. 5 Attachment "D" 5 Page 4 of 4 4 | October 1, 1976 NSP-III-2, Rev. 5 Attachment "D" 5 Page 4 of 4 4 | ||
-, . . . .}} | -, . . . .}} | ||
Revision as of 04:24, 1 February 2020
| ML19320A072 | |
| Person / Time | |
|---|---|
| Site: | Arkansas Nuclear |
| Issue date: | 11/01/1976 |
| From: | Cook R ARKANSAS POWER & LIGHT CO. |
| To: | |
| Shared Package | |
| ML19320A067 | List: |
| References | |
| NUDOCS 8004140685 | |
| Download: ML19320A072 (4) | |
Text
-
,h. UCENSEE EVENT REPOR m CONTROL BLCCK:l l l l l l l [Pt. EASE PRINT ALL REOlJIMED INPomatATIO98)
(0 \
=
, 8
_ .. _ E. w =
@E) I AIR , A IRIK I U 101o1-1o1010101o1-10101 14 I I I il I I I i lol31 32 7 89 14 15 25 26 30 3e CATEGORY Type s DOCKET NUM8EA EVENT DATE AEPORT CAff 0 CON'Tl l I W M 1015101-101311131 1110101317161 lll11o1117161 7 8 57 58 59 60 61 68 69 74 75 80 EVENT DESCRIPTON
!!E lbi . steadv state .oceah . at IM5 . 10 3 % a leak was discovered at a 80 l
7 89 '
0 15ecke{inald,e;,,(3 C)O' elbow u,e11. *,n we 'Pv; ..,' Mali. . P m p ?%c. eu.4;.. re) e c 1 7 89 ' ' ' '
80' 30 l IIwe . bb b t4sM olkced in sevve'te and the Ne ld on Oe Ph( Such reliN lIwe Wu 80 7 89 8 HE Iveca,;rea. %it well failure was re ported previously t w RoR 50-Sit / M-12,.(*>o Bi31%-In l 7 89 80 I
@B L 80 7 89 m, Yes CCOE CCMpONENT CODE VAPM V10uTCN u Icl41 LB] lP lI l P lG lx ix i LAJ IZl919191 11]
7 89 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION U lDe b'ilure veaw be cowtWhAfed to Oc & art Ekd khe Y4" FelieE line is NeidIv supo.rked ~
7 89 '
80 HE lt.> Lite the 6" sutw. i ce is not ava is muede4 h vibrati.w . A. .w ;tecerroevousw.ars
' " ~
1 89 80 I b.i.. ce< t. ea 4. 4.t. . ;c w.oa:t; aw.. s,e ne ..s av, . I
'st % POWEA QTHER STATUS OSCOVERY OISCOVERY DESCASTCN
- EB LEJ 1o1919I I N A I Lbj i MA l 7 8 9 10 12 13 44 45 48 80 AYtrIsED o $ASE AMOUNT or ACTmTv toCarCN or REttast 3E LIJ lIJ l NA I I NA I
- 7 8 9 10 11 44 45 80 PERSONNEL EXPOSUAES ,
NuMsEn tvet otsConvCN g DE 1010101 LIJ lNA I 7 89 11 12 13 80 PERSONNEL INJUAIES NUM8ER DE lololol ICESCA*T'O1 N 1 7 89 11 12 80 0FFSITE CONSEQUENCES i l MA 80 i
7 89 .
LOSS OR DAMAGE TO FAC:UTY fvpf OESCAWTCN Emi NA I-7 89 10 80 PUBUCITY I NA I 7 89 80 A00lTONAL FACTCAS I NA I 89 80 mg I a 0 0 4140 b bE i NAME; CCck N ONE(5 00 M l. 4 199 kEacpp,y "o "b u7 n,...w. i . t o-r s. . _ _ ._. NSP-III-2. Rev. 5
m
- 1. Reportable Occurrence Report No. 50-313/76-29 4
- 2. Report Date: November 1, 1976 3. Occurrence Date: October 3, 1976
- 5. Identification 6f Occurrence:
Leak in Primary Makeup Pump P36C suction relief line ,
4
- 6. Conditions Prior to Occurrence:
3 Steady-State Power X Reactor Power 2542 MWth Hot Standby Net Output 824 MWe Cold Shutdown Percent of Full Power 99 %
Refueling Shutdown Load Changes During Routine Power Operation _.
Routine Startup..
Operation
~
Routine Shutdown Operation Other (specify) s
, i
- 7. Description of Occurrence: ~2 At 165S hrs. on 10.3/76, a leak was discovered at a socket weld, pipe to 900 elbow weld, in the primary makeup pump P36C suction relief line. P36C was removed from service and P36B was placed in service. .
NSP-III-2, Rev. 5 Attachment "D" S _
October 1, 1976 Page 2 of 4 l
] ., % )
Reportable Occurrence Report No. 50-313/76-29 4
- 8. Designation of Apparent Cause of Occurrence:
Design x Procedure
, Manufacture Unusual Service Condition Including Environmental Installation / -
Construction Component Failure.
(See Failure D tta) 5 Operator Other' (specify)
This failure could be contributed to the fact that the 3/4" relief line is rigidly supported witile the 6" suction line is subjected to vibration.
i
- 9. Analysis of Occurrence:
Even though only one pump was operable during the time repairs were made, which is allowable by Tech. Spec., there was no ha:ard to the health and safety of the public.
t
. ~;
1 October 1, 1976 NSP-III-2, Rev. 5 Attachment "D" 5 Page 3 Of 4 ym . . - . - +- -3.- +- ayy. .,- *.--w-. ,---a- ,------ -- e- e,
. , 7 A
Reportable Occurrence Report No. 50-313/76-29 4
1
- 10. Corrective Action:
The defective weld was repaired. An engineering evaluation is being
,. made and if.necessary modifications will be made to prevent a !
reoccurrence. - '
4 4
m.
l l
- 11. Failure' Data: ,
This same weld failure was also reported in ROR #'/6-12.
i ,I
] I i
~;
l i
October 1, 1976 NSP-III-2, Rev. 5 Attachment "D" 5 Page 4 of 4 4
-, . . . .