ENS 44588: Difference between revisions
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| event date = 10/21/2008 20:51 PDT | | event date = 10/21/2008 20:51 PDT | ||
| last update date = 10/22/2008 | | last update date = 10/22/2008 | ||
| title = Unit 2 Manual Reactor Trip Due | | title = Unit 2 Manual Reactor Trip Due to Jellyfish Intrusion | ||
| event text = On October 21, 2008, with both units operating at 100% power, Operators manually actuated the Unit 2 reactor protection system (RPS/reactor trip) due to high differential pressure (DP) across the circulating water pumps' intake traveling screens. The high DP resulted from a rapid influx of jellyfish. All systems responded as designed. All control rods fully inserted. Auxiliary feedwater actuated as designed. The grid is stable with power being supplied by 230 Kv startup power. Diesel generator (DG) 2-2 and 2-3 are operable in standby. DG 2-1 is inoperable due to scheduled maintenance. The traveling screens for the safety-related auxiliary saltwater system (ASW) are not degraded and are managing the influx of jellyfish with no significantly elevated DP. Unit 2 is stable in Mode 3 at normal operating temperature and pressure. | | event text = On October 21, 2008, with both units operating at 100% power, Operators manually actuated the Unit 2 reactor protection system (RPS/reactor trip) due to high differential pressure (DP) across the circulating water pumps' intake traveling screens. The high DP resulted from a rapid influx of jellyfish. All systems responded as designed. All control rods fully inserted. Auxiliary feedwater actuated as designed. The grid is stable with power being supplied by 230 Kv startup power. Diesel generator (DG) 2-2 and 2-3 are operable in standby. DG 2-1 is inoperable due to scheduled maintenance. The traveling screens for the safety-related auxiliary saltwater system (ASW) are not degraded and are managing the influx of jellyfish with no significantly elevated DP. Unit 2 is stable in Mode 3 at normal operating temperature and pressure. | ||
This event is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(B), 'RPS actuation,' and 50.72(b)(3)(iv)(A), 'Specified System Actuation.' | This event is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(B), 'RPS actuation,' and 50.72(b)(3)(iv)(A), 'Specified System Actuation.' |
Latest revision as of 21:13, 1 March 2018
Where | |
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Diablo Canyon California (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release | |
LER: | 05000323/LER-2008-002 |
Time - Person (Reporting Time:+-2.12 h-0.0883 days <br />-0.0126 weeks <br />-0.0029 months <br />) | |
Opened: | John Whetsler 01:44 Oct 22, 2008 |
NRC Officer: | Jason Kozal |
Last Updated: | Oct 22, 2008 |
44588 - NRC Website
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