ENS 44588: Difference between revisions

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| event date = 10/21/2008 20:51 PDT
| event date = 10/21/2008 20:51 PDT
| last update date = 10/22/2008
| last update date = 10/22/2008
| title = Unit 2 Manual Reactor Trip Due To Jellyfish Intrusion
| title = Unit 2 Manual Reactor Trip Due to Jellyfish Intrusion
| event text = On October 21, 2008, with both units operating at 100% power, Operators manually actuated the Unit 2 reactor protection system (RPS/reactor trip) due to high differential pressure (DP) across the circulating water pumps' intake traveling screens. The high DP resulted from a rapid influx of jellyfish.  All systems responded as designed. All control rods fully inserted. Auxiliary feedwater actuated as designed. The grid is stable with power being supplied by 230 Kv startup power. Diesel generator (DG) 2-2 and 2-3 are operable in standby. DG 2-1 is inoperable due to scheduled maintenance. The traveling screens for the safety-related auxiliary saltwater system (ASW) are not degraded and are managing the influx of jellyfish with no significantly elevated DP. Unit 2 is stable in Mode 3 at normal operating temperature and pressure.  
| event text = On October 21, 2008, with both units operating at 100% power, Operators manually actuated the Unit 2 reactor protection system (RPS/reactor trip) due to high differential pressure (DP) across the circulating water pumps' intake traveling screens. The high DP resulted from a rapid influx of jellyfish.  All systems responded as designed. All control rods fully inserted. Auxiliary feedwater actuated as designed. The grid is stable with power being supplied by 230 Kv startup power. Diesel generator (DG) 2-2 and 2-3 are operable in standby. DG 2-1 is inoperable due to scheduled maintenance. The traveling screens for the safety-related auxiliary saltwater system (ASW) are not degraded and are managing the influx of jellyfish with no significantly elevated DP. Unit 2 is stable in Mode 3 at normal operating temperature and pressure.  
This event is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(B), 'RPS actuation,' and 50.72(b)(3)(iv)(A), 'Specified System Actuation.'
This event is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(B), 'RPS actuation,' and 50.72(b)(3)(iv)(A), 'Specified System Actuation.'

Latest revision as of 21:13, 1 March 2018

ENS 44588 +/-
Where
Diablo Canyon Pacific Gas & Electric icon.png
California (NRC Region 4)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(iv)(A), System Actuation

10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
LER: 05000323/LER-2008-002
Time - Person (Reporting Time:+-2.12 h-0.0883 days <br />-0.0126 weeks <br />-0.0029 months <br />)
Opened: John Whetsler
01:44 Oct 22, 2008
NRC Officer: Jason Kozal
Last Updated: Oct 22, 2008
44588 - NRC Website
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