ENS 46900
From kanterella
Jump to navigation
Jump to search
ENS Event | |
---|---|
19:12 May 27, 2011 | |
Title | Loss of Unit 1 Startup Power Results in Starting All Emergency Diesel Generators |
Event Description | On May 27, 2011, at 1212 PDT, Unit 1 startup power was lost due to actuation of startup transformer 1-1 overcurrent/differential relay 51-87UT11-1, which isolated the 12 kV feeder to startup bus. The loss of offsite startup power caused all Unit 1 emergency diesel generators (EDGs) to start in the standby mode. The EDGs started as designed with no issues observed. No vital loads were affected as a result of the 12 kV bus loss. On May 27, 2011, at 1241 PDT, all Unit 1 EDGs were shut down and returned to auto. Subsequently, startup transformers 1-1 and 1-2 were energized, followed by the 12 kV underground loop, and on May 27, 2011, at 1337 PDT, Unit 1 startup power was declared operable.
The cause of the event was a human performance error while attempting to test the startup transformer 2-1 overcurrent/differential relay. The maintenance electrical worker inadvertently installed a jumper on the overcurrent/differential relay for startup transformer 1-1. Unit 2 startup power was cleared at this time and there was no effect on Unit 2. The NRC Resident Inspector was notified. |
Where | |
---|---|
Diablo Canyon California (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+1 h0.0417 days <br />0.00595 weeks <br />0.00137 months <br />) | |
Opened: | Anthony Chitwood 20:12 May 27, 2011 |
NRC Officer: | Howie Crouch |
Last Updated: | May 27, 2011 |
46900 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 46900\u003C/a\u003E - \u003Ca href=\"/Diablo_Canyon\" title=\"Diablo Canyon\"\u003EDiablo Canyon\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003ELoss of Unit 1 Startup Power Results in Starting All Emergency Diesel Generators\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 46900 - Diablo Canyon\n","link":"","lat":35.21169166666667,"lon":-120.85504166666666,"icon":"/w/images/f/ff/Pacific_Gas_%26_Electric_icon.png"}],"imageoverlays":null} | |
Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 567692023-10-01T03:14:0001 October 2023 03:14:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip ENS 555262021-10-16T00:49:00016 October 2021 00:49:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip and Automatic Auxiliary Feedwater Actuation ENS 537642018-12-01T08:00:0001 December 2018 08:00:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip of Unit 2 Due to a Load Rejection ENS 519652016-05-30T16:30:00030 May 2016 16:30:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Opening of Reactor Trip Breakers Due to Rod Position Error Greater than 12 Steps ENS 505862014-11-01T00:40:0001 November 2014 00:40:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Emergency Diesel Generator Start Due to Loss of Offsite 230Kv Startup Power Supply ENS 497862014-02-02T19:29:0002 February 2014 19:29:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Automatic Reactor Trip ENS 492872013-08-16T01:24:00016 August 2013 01:24:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Startup Power Results in Valid Starts of All Three Emergency Diesel Generators ENS 491842013-07-10T16:50:00010 July 2013 16:50:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Automatic Reactor Trip ENS 491432013-06-24T04:20:00024 June 2013 04:20:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of 230 Kv Offsite Power Results in the Automatic Start of Emergency Diesel Generators ENS 487962013-03-01T05:54:0001 March 2013 05:54:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Bus Inadvertently De-Energized with Unit Defueled ENS 484002012-10-11T19:08:00011 October 2012 19:08:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Experienced an Automatic Reactor Trip on a 500Kv Line Differential Relay Actuation ENS 469002011-05-27T19:12:00027 May 2011 19:12:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Unit 1 Startup Power Results in Starting All Emergency Diesel Generators ENS 468942011-05-26T09:26:00026 May 2011 09:26:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Startup Power Due to Fault in Switchyard Causes All Edgs to Start ENS 468562011-05-17T16:54:00017 May 2011 16:54:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generators Start Due to Maintenance Activities ENS 467012011-03-26T21:49:00026 March 2011 21:49:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip When a Loss of the 2-1 Main Feedwater Pump Occurred ENS 445882008-10-22T03:51:00022 October 2008 03:51:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Manual Reactor Trip Due to Jellyfish Intrusion ENS 444192008-08-17T07:12:00017 August 2008 07:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Fire in Main Bank Tranformer ENS 433932007-05-29T05:50:00029 May 2007 05:50:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator Actuation Due to Momentary Undervoltage Condition ENS 433912007-05-27T18:17:00027 May 2007 18:17:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip in Mode 3 During Control Rod Testing ENS 433602007-05-12T17:25:00012 May 2007 17:25:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generators Start Due to Loss of Off Site Start Up Power ENS 430472006-12-12T21:22:00012 December 2006 21:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Circulating Water Pump Failure Causes Explosion in Intake Structure ENS 430422006-12-11T00:08:00011 December 2006 00:08:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Rapid Shutdown and Manual Reactor Trip Due to High Reactor Coolant Pump Stator Temperature ENS 421572005-11-19T23:51:00019 November 2005 23:51:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Diesel Generator Starts on a Vaild Bus Undervoltage Signal ENS 412502004-12-09T10:04:0009 December 2004 10:04:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Rps Actuation While Shutdown Due to Failed Fuse ENS 411682004-11-02T19:05:0002 November 2004 19:05:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Diesel Generator Start on a Valid Bus Undervoltage Signal 2023-10-01T03:14:00 | |
Retrieved from "https://kanterella.com/w/index.php?title=ENS_46900&oldid=424620"