ENS 43360
ENS Event | |
---|---|
17:25 May 12, 2007 | |
Title | Emergency Diesel Generators Start Due to Loss of Off Site Start Up Power |
Event Description | On May 12, 2007, at 10:25 am PST, offsite startup power was lost to Diablo Canyon Units 1 and 2. This is the 8-hour non-emergency event notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) for a valid actuation of five emergency diesel generators (EDGs) due to the loss of startup power.
Unit 1 is in a refueling outage in No Mode, with all fuel offloaded to the spent fuel pool (SFP). Auxiliary power is cleared for maintenance and offsite power was being provided by startup power. EDG 1-3 was also cleared for maintenance. On the loss of startup power, EDGs 1-1 and 1-2 auto-started and powered their loads. Since SFP cooling is not automatically loaded on the EDGs, Operators re-started a SFP Cooling pump. This re-established decay heat removal via component cooling water (CCW) (two of three pumps remained operable) and auxiliary saltwater pump 1-2. SFP temperature remained at approximately 105 degrees F. Unit 2 remained in Mode 1 at 100 percent power with auxiliary power supplying Unit 2 equipment. The loss of startup power caused all three EDGs to auto-start but they did not load. At approximately 11:30am PDT, startup power was restored to the site via the Mesa substation. Operators completed restoration of startup power to plant equipment by approximately 14:30 PDT. The cause of the loss of startup power was reported as a failed Morro Bay - Diablo transmission line. The licensee notified the NRC Resident Inspector. |
Where | |
---|---|
Diablo Canyon California (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
LER: | 05000275/LER-2007-001 |
Time - Person (Reporting Time:+0.73 h0.0304 days <br />0.00435 weeks <br />9.99954e-4 months <br />) | |
Opened: | Jan Nimick 18:09 May 12, 2007 |
NRC Officer: | Jason Kozal |
Last Updated: | May 12, 2007 |
43360 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 43360\u003C/a\u003E - \u003Ca href=\"/Diablo_Canyon\" title=\"Diablo Canyon\"\u003EDiablo Canyon\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003EEmergency Diesel Generators Start Due to Loss of Off Site Start Up Power\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 43360 - Diablo Canyon\n","link":"","lat":35.21169166666667,"lon":-120.85504166666666,"icon":"/w/images/f/ff/Pacific_Gas_%26_Electric_icon.png"}],"imageoverlays":null} | |
Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 567692023-10-01T03:14:0001 October 2023 03:14:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip ENS 555262021-10-16T00:49:00016 October 2021 00:49:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip and Automatic Auxiliary Feedwater Actuation ENS 537642018-12-01T08:00:0001 December 2018 08:00:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip of Unit 2 Due to a Load Rejection ENS 519652016-05-30T16:30:00030 May 2016 16:30:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Opening of Reactor Trip Breakers Due to Rod Position Error Greater than 12 Steps ENS 505862014-11-01T00:40:0001 November 2014 00:40:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Emergency Diesel Generator Start Due to Loss of Offsite 230Kv Startup Power Supply ENS 497862014-02-02T19:29:0002 February 2014 19:29:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Automatic Reactor Trip ENS 492872013-08-16T01:24:00016 August 2013 01:24:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Startup Power Results in Valid Starts of All Three Emergency Diesel Generators ENS 491842013-07-10T16:50:00010 July 2013 16:50:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Automatic Reactor Trip ENS 491432013-06-24T04:20:00024 June 2013 04:20:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of 230 Kv Offsite Power Results in the Automatic Start of Emergency Diesel Generators ENS 487962013-03-01T05:54:0001 March 2013 05:54:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Bus Inadvertently De-Energized with Unit Defueled ENS 484002012-10-11T19:08:00011 October 2012 19:08:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Experienced an Automatic Reactor Trip on a 500Kv Line Differential Relay Actuation ENS 469002011-05-27T19:12:00027 May 2011 19:12:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Unit 1 Startup Power Results in Starting All Emergency Diesel Generators ENS 468942011-05-26T09:26:00026 May 2011 09:26:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Startup Power Due to Fault in Switchyard Causes All Edgs to Start ENS 468562011-05-17T16:54:00017 May 2011 16:54:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generators Start Due to Maintenance Activities ENS 467012011-03-26T21:49:00026 March 2011 21:49:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip When a Loss of the 2-1 Main Feedwater Pump Occurred ENS 445882008-10-22T03:51:00022 October 2008 03:51:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Manual Reactor Trip Due to Jellyfish Intrusion ENS 444192008-08-17T07:12:00017 August 2008 07:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Fire in Main Bank Tranformer ENS 433932007-05-29T05:50:00029 May 2007 05:50:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator Actuation Due to Momentary Undervoltage Condition ENS 433912007-05-27T18:17:00027 May 2007 18:17:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip in Mode 3 During Control Rod Testing ENS 433602007-05-12T17:25:00012 May 2007 17:25:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generators Start Due to Loss of Off Site Start Up Power ENS 430472006-12-12T21:22:00012 December 2006 21:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Circulating Water Pump Failure Causes Explosion in Intake Structure ENS 430422006-12-11T00:08:00011 December 2006 00:08:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Rapid Shutdown and Manual Reactor Trip Due to High Reactor Coolant Pump Stator Temperature ENS 421572005-11-19T23:51:00019 November 2005 23:51:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Diesel Generator Starts on a Vaild Bus Undervoltage Signal ENS 412502004-12-09T10:04:0009 December 2004 10:04:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Rps Actuation While Shutdown Due to Failed Fuse ENS 411682004-11-02T19:05:0002 November 2004 19:05:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Diesel Generator Start on a Valid Bus Undervoltage Signal 2023-10-01T03:14:00 | |