ENS 44419
ENS Event | |
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07:12 Aug 17, 2008 | |
Title | Unusual Event Declared Due to Fire in Main Bank Tranformer |
Event Description | At 0012 the licensee declared a Notice of Unusual Event due to a fire in Main Bank Transformer. The licensee is fighting the fire along with offsite assistance from CAL FIRE. The unit is shutdown and stable in mode 3. All control rods fully inserted on the trip. Decay heat is being removed via auxiliary feedwater to the steam generators steaming to the main condenser via the main condenser steam dumps. Emergency buses remain powered via offsite power with emergency diesel generators available if required.
The licensee will notify the NRC Resident Inspector. Notified DHS (Barnes), FEMA (Blankenship).
The fire is out. Plant personnel are assessing the damage in the main transformer area. The plant is stable in mode 3. The licensee will notify the NRC Resident Inspector.
The licensee has terminated the Notice of Unusual Event at 0231 PDT due to the fact that the fire was out and no reflash occurred. The plant remains stable in mode 3. The licensee will notify the NRC Resident Inspector. Notified R4DO (Lantz), IRD (McMurtray), NRR EO (Wermiel), R4 (Collins), NRR (Grobe), DHS (Wallace), FEMA (Biscoe).
This is an update of the Notification of Unusual Event due to Fire in the 'C' phase of the main bank transformer, and Automatic Reactor Trip. This update is to report automatic actuation of the auxiliary feedwater system (AFW) and is being reported as an 8-hour non-emergency event in accordance with 10 CFR 50.72(b)(3)(iv)(A) 'System Actuation.' The unit is stable in mode 3 (Hot Standby) with offsite power being supplied to all buses via the 230 Kv startup circuit. All rods fully inserted on the reactor trip. All systems performed as designed. Operators are preparing to place the unit in Mode 5, while preparing to assess the damage to the 500 Kv transformer. All emergency diesel generators remain operable in standby. Unit 1 was unaffected by this event and remains at 100% power. This notification also constitutes a late 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> notification for the RPS actuation. To summarize, on August 16, 2008, at 2356 PDT, the 'C' phase 500 Kv transformer failed resulting in a fire and an automatic reactor trip, and automatic actuation of AFW. An unusual event was declared on August 17, 2008, at 0012 PDT due to the fire. Cal Fire was called to assist and support the on-site fire brigade. The fire was extinguished and the NUE was downgraded at 0231 PDT. The NRC Resident Inspector has been notified as well as State and local government agencies. The licensee intends to issue a press release. R4DO (Lantz) notified. |
Where | |
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Diablo Canyon California (NRC Region 4) | |
Reporting | |
Emergency class: | Unusual Event |
10 CFR 50.72(a) (1) (i), Emergency Class Declaration 10 CFR 50.72(b)(3)(iv)(A), System Actuation 10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
LER: | 05000323/LER-2008-001 |
Time - Person (Reporting Time:+-3.58 h-0.149 days <br />-0.0213 weeks <br />-0.0049 months <br />) | |
Opened: | James Dillis 03:37 Aug 17, 2008 |
NRC Officer: | Pete Snyder |
Last Updated: | Aug 17, 2008 |
44419 - NRC Website
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Unit 2 | |
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Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Standby (0 %) |
Diablo Canyon with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 567692023-10-01T03:14:0001 October 2023 03:14:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip ENS 555262021-10-16T00:49:00016 October 2021 00:49:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip and Automatic Auxiliary Feedwater Actuation ENS 547892020-07-17T20:46:00017 July 2020 20:46:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram Due to Increased Hydrogen Usage ENS 537642018-12-01T08:00:0001 December 2018 08:00:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip of Unit 2 Due to a Load Rejection ENS 528762017-07-28T19:06:00028 July 2017 19:06:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Alert Declared Due to Low Oxygen Levels Inside Containment ENS 519652016-05-30T16:30:00030 May 2016 16:30:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Opening of Reactor Trip Breakers Due to Rod Position Error Greater than 12 Steps ENS 516552016-01-14T22:43:00014 January 2016 22:43:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Notification of Unusual Event - Security Condition That Does Not Involve Hostile Action ENS 505862014-11-01T00:40:0001 November 2014 00:40:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Emergency Diesel Generator Start Due to Loss of Offsite 230Kv Startup Power Supply ENS 497862014-02-02T19:29:0002 February 2014 19:29:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Automatic Reactor Trip ENS 492872013-08-16T01:24:00016 August 2013 01:24:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Startup Power Results in Valid Starts of All Three Emergency Diesel Generators ENS 491842013-07-10T16:50:00010 July 2013 16:50:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Automatic Reactor Trip ENS 491432013-06-24T04:20:00024 June 2013 04:20:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of 230 Kv Offsite Power Results in the Automatic Start of Emergency Diesel Generators ENS 487962013-03-01T05:54:0001 March 2013 05:54:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Bus Inadvertently De-Energized with Unit Defueled ENS 484272012-10-21T07:09:00021 October 2012 07:09:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Unusual Event Declared Due to Seismic Event ENS 484002012-10-11T19:08:00011 October 2012 19:08:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Experienced an Automatic Reactor Trip on a 500Kv Line Differential Relay Actuation ENS 469002011-05-27T19:12:00027 May 2011 19:12:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Unit 1 Startup Power Results in Starting All Emergency Diesel Generators ENS 468942011-05-26T09:26:00026 May 2011 09:26:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Startup Power Due to Fault in Switchyard Causes All Edgs to Start ENS 468562011-05-17T16:54:00017 May 2011 16:54:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generators Start Due to Maintenance Activities ENS 467012011-03-26T21:49:00026 March 2011 21:49:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip When a Loss of the 2-1 Main Feedwater Pump Occurred ENS 466682011-03-11T09:23:00011 March 2011 09:23:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Notice of Unusual Event as a Result of a Tsunami Warning in the Area ENS 465092010-12-26T00:25:00026 December 2010 00:25:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Notification of Unusual Event Declared Due to High Winds ENS 460362010-06-23T17:48:00023 June 2010 17:48:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Alert Declared for a Cardox Discharge in the Turbine Building ENS 459922010-06-09T18:12:0009 June 2010 18:12:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Unusual Event Declared Due to Toxic Gas/Chemical Spill in the Protected Area ENS 451122009-06-02T08:22:0002 June 2009 08:22:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Unusual Event - Smoke Alarm in Protected Area Lasting Greater than 15 Minutes ENS 445882008-10-22T03:51:00022 October 2008 03:51:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 2 Manual Reactor Trip Due to Jellyfish Intrusion ENS 444192008-08-17T07:12:00017 August 2008 07:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Fire in Main Bank Tranformer ENS 443572008-07-21T16:08:00021 July 2008 16:08:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Unusual Event Declared - Unable to Validate a Fire Alarm within 15 Minutes ENS 433932007-05-29T05:50:00029 May 2007 05:50:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator Actuation Due to Momentary Undervoltage Condition ENS 433912007-05-27T18:17:00027 May 2007 18:17:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip in Mode 3 During Control Rod Testing ENS 433602007-05-12T17:25:00012 May 2007 17:25:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generators Start Due to Loss of Off Site Start Up Power ENS 430472006-12-12T21:22:00012 December 2006 21:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Circulating Water Pump Failure Causes Explosion in Intake Structure ENS 430422006-12-11T00:08:00011 December 2006 00:08:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Rapid Shutdown and Manual Reactor Trip Due to High Reactor Coolant Pump Stator Temperature ENS 421572005-11-19T23:51:00019 November 2005 23:51:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Diesel Generator Starts on a Vaild Bus Undervoltage Signal ENS 417742005-06-15T03:50:00015 June 2005 03:50:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Notification of Unusual Event Due to Tsunami Warning ENS 412502004-12-09T10:04:0009 December 2004 10:04:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Rps Actuation While Shutdown Due to Failed Fuse ENS 411682004-11-02T19:05:0002 November 2004 19:05:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Diesel Generator Start on a Valid Bus Undervoltage Signal ENS 410762004-09-28T17:30:00028 September 2004 17:30:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Unusual Event Declared Due to Seismic Activity ENS 404082003-12-22T19:22:00022 December 2003 19:22:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Notification of Unusual Event - Earthquake ENS 402582003-10-18T07:52:00018 October 2003 07:52:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Earthquake Felt on Site. Entered Emergency Action Level (Eal) 18 2023-10-01T03:14:00 | |