ML18348A277: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
 
(Created page by program invented by StriderTol)
 
(One intermediate revision by the same user not shown)
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:} .*..; * *
{{#Wiki_filter:} .*..;
* consumers Power company General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201
consumers
* Area Code 517 788-0550 November 11, 1976 Mr James G Keppler Office of Inspection and Enforcement Region III US Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 DOCKET 50-255 -LICENSE DPR-20 -PALISADES PLANT -ER-76-34 AND 35 DISCHARGE ABOVE 5°F LIMIT Attached are two reportable occurrences which related to the Palisades Plant. These occurrences involve the discharge of cooling water above the 5°F limit. However, the plant NPDES limits were not exceeded.
* Power company General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201
David A Bixel Assistant Nuclear Licensing Administrator NOV 151976
* Area Code 517 788-0550 November 11, 1976 Mr James G Keppler Office of Inspection and Enforcement Region III US Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 DOCKET 50-255 - LICENSE DPR         PALISADES PLANT - ER-76-34 AND 35 ~
.ICENSEE EVENT REPORT
DISCHARGE ABOVE 5°F LIMIT Attached are two reportable occurrences which related to the Palisades Plant.
* CONTROL BLOCK: I . I [PLEASE ALL REQUIRED INFORMATION] . 1..._ _____ .._...._ __ .....,.6 ' LICENSEE NAME 1 IM I I Ip IA IL I 1 I 7 8 9 . 14 LICENSE NUMBER lolo 1--lololololol-lolol 15 25 LICENSE TYPE l411l1l1l1I 26 . 30 EVENT CATE EVENT TYPE 1-0 I 3 I 31 32 REPORT CATE @IT] CON'T ..... I __ _,I 78 57 58 REPORT TYPE w REPORT SOURCE w DOCKl;T NUMBER I ols lol-lo 121515 I l1lol2 lol1l6I I 1 I 1 I. i I 1 I 1 I 6 I 59 60 61 . 68 69 74 75 . 80 EVENT DESCRIPTION 10'21 I Plant operational problems resulted in tripping of the cooling tower pumps. Re-7 8 9 . . lol3I I establishment of water box vacuum and pump starting lead to a discharge tempera-7 8 9 lol41 I ture above the 5°F limit. The maximum temperature was 0.4°F over the limit and 7 8 9 . . 10151 I the total time over the limit was 8 minutes. 7 8 9 lolsl 7 8 9 SYSTEM CAUSE COOE CODE @0 IHJFI l!J 7 8 9 10 11 CAUSE DESCRIPTION COMPONENT COOE lzlzlzlzlzlzl 12 17 PRIME COMPONENT SUPPl..IER w 43 CEJMPONENT MANUFACTURER I z I ZI z I z I 44 . 47 (ER-76-34)
These occurrences involve the discharge of cooling water above the 5°F limit.
VIOLATION w 48 I 80 I 80 I 80 I 80 80 lol0I I To reestablish a vacuum in the condenser water box and permit restart of 7 8 9 . . . the pumps I BO I some coolant flow was required.
However, the plant NPDES limits were not exceeded.
This flow caused the discharge limit to be ex-7 B 9 I ceeded for a short period of time. NPDES limits were not exceeded.
David A Bixel Assistant Nuclear Licensing Administrator NOV 151976
WBs FACILITY . METHOO OF STATUS % POWER OTHER STATUS DISCOVERY EE1 L£J I 0 I 0 I 0 I -----* N_A __ __.I w 7 8 9 10 12 13 44 45 FORM OF ACTIVITY CONTENT rn OF l._ ___ AM_o_u_N_T
 
__ _,I I 7 8 9 10 11 44 45 PERSONNEL EXPOSURES NUMBER TYPE OESCRIP.TION W NA 7 B 9 11 12 13 PERSnNNEL INJURIES NUMBER DESCRIPTION ololol NA 7 8 9 11 12 PROBABLE CONSEQUENCES None 7 B 9 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION ITifil liJ NA 7 8 9 10 PUBLICITY
                                                              .ICENSEE EVENT REPORT
[ill] NA 7 8 9
* I CONTROL BLOCK: 1...______.._....___.....,.6         .I                            [PLEASE P~INT ALL REQUIRED INFORMATION] .
* ADDITIONAL FACTORS 7 8 9 l1lfil 7 8 9 46 DISCOVERY DESCRIPTION NA LOCATION OF RELEASE NA I 80 I 80 80 80 80 80 80 80 BO BO BO 
LICENSEE                                                                                     LICENSE              EVENT NAME                                     LICENSE NUMBER                                      TYPE                TYPE 1   IM I I Ip IA IL I 1 I lolo 1--lololololol-lolol l411l1l1l1I                                                                 1-0 I 3 I 7    8 9                            . 14    15                                                  25    26                . 30  31     32
-* _Iii' 9.1cENSEE EVENT REPORT
'                                    REPORT     REPORT DOCKl;T NUMBER                            EVENT CATE                     REPORT CATE
* CONTROL BLOCK: .._I ___.__._I
      @IT] CON'T I.....___,I 78             57       58 w w TYPE 59 SOURCE 60 I61ols lol-lo 12151568I l1lol2 lol1l6I I751 I 1 I. i I.1 I 1 I 680I 69                         74 EVENT DESCRIPTION 10'21 I Plant         operational problems resulted in tripping of the cooling tower pumps.                                                     Re-   I 7     8 9                 .                                 .                                                                                         80 lol3I I establishment of water box vacuum and pump starting lead to a discharge tempera-                                                                 I 7     8 9                                                                                                                                               80 lol41 7 8 9 I ture above     . .
the 5°F limit. The maximum temperature was 0.4°F over the limit and                                                     I 80 10151 I the total time over the limit was 8 minutes.                                                             (ER-76-34)                            I 7 8 9                                                                                                                                                   80 lolsl                                                                                                                                                 80 7     8 9                                                                     PRIME SYSTEM       CAUSE                                             COMPONENT              CEJMPONENT COMPONENT COOE                SUPPl..IER          MANUFACTURER            VIOLATION w
COOE         CODE 7
    @0 IHJFI 8 9 10 l!J 11 lzlzlzlzlzlzl 12                           17 w43 Iz I ZI z. I z47I 44                           48 CAUSE DESCRIPTION lol0I I To reestablish a vacuum in the condenser water box and permit restart                                                           of the pumps    I 7 8 9 .                     .       .                                                                                                                   BO
    ~ I some coolant flow was required. This flow caused the discharge limit                                                               to be ex-       I 7     B 9                                                                                                                                               80
  ~          I ceeded for a short period of time.                                 NPDES limits were not exceeded.                                           I WBs           FACILITY                                                           . METHOO OF 80 w
STATUS               % POWER                   OTHER STATUS               DISCOVERY                      DISCOVERY DESCRIPTION EE18 7
L£J 9
I 0 I 0 I 0 I -----*N_A_ ___.I 10             12 13                             44       45     46 NA 80 FORM OF rn ACTIVITY         CONTENT Rl~SiD            r~LiSE l.____AM_o_u_N_T_~-~-A-CT,...IV_IT_Y_ __,I LOCATION OF RELEASE OF I                   NA 7     8       9                 10       11                                       44         45                                                         80 PERSONNEL EXPOSURES NUMBER           TYPE       OESCRIP.TION 7
    ~lololol B 9               11 W12      13 NA 80 PERSnNNEL INJURIES NUMBER             DESCRIPTION
    ~I        ololol                                                                           NA 7   8 9               11   12                                                                                                                       80 PROBABLE CONSEQUENCES
    ~                        None 7   B 9                                                                                                                                               80 LOSS OR DAMAGE TO FACILITY TYPE       DESCRIPTION ITifil8 9liJ 7                 10 NA 80 PUBLICITY
[ill]                                                                     NA 7   8 9                                                                                                                                               BO
* ADDITIONAL FACTORS 7   8 9                                                                                                                                               BO l1lfil8 9 7                                                                                                                                                       BO
 
~
  -* _Iii' CONTROL BLOCK:
LICENSEE NAME 9.1cENSEE EVENT REPORT
                                                        . _I___.__._I__,___.._.,.j~'
1                          5*
LICENSE NUMBER
[PLEASE PRINT ALL REQUIRED INFORMATION]
[PLEASE PRINT ALL REQUIRED INFORMATION]
LICENSEE NAME 7 8 9 14 REPORT TYPE. 1 5* LICENSE NUMBER ol-lolol 15 25 REPORT SOURCE OOCKE;T NUMBER LICENSE TYPE 14111111111
LICENSE TYPE EVENT TYPE
: 26. 30 EVENT DATE EVENT TYPE I o I 3 I 31 32 REPORT DATE @IT] CON'T 7 8 57 58 w L1J lol 51ol-101215151 1110121617161 1111111111161 . 59 60 61 68 69 74 75 . 80 EVENT DESCRIPTION 10121 I During plant start-up on October 26 and 27, 1976 three events occurred which re-I 7 8 9 . 80 lol3l I sulted in discharge water al)ove the5°F limit. The disi;harges averaged about 3°F I 7 8 9 80 lol41 I over the limit. The total time over the limit f'or all three events was 88 minutes . I 7 8 9 . lol51 I and the maximum temperature was 11°F over the limit. 7 8 9 lol61 7 8 9 SYSTEM CAUSE CODE CODE . COMPONENT CODE @El I HI F I L!.J lz I z I z I z I z I z I 7 8 9 10 11 12 17 CAUSE DESCRIPTION PANE COMPONENT SUPPlER w 43 COMPONENT MANUFACTURER 1z1z1z1z1 44 47 80 (ER-76-35)
~IMlrlPIAILl1I                                          lolol~lolololol ol-lolol                              14111111111                  I oI 3 I 7     8 9                                 14       15                                              25    26.                    30    31    32 REPORT      REPORT TYPE.                                                                                                 REPORT DATE w          SOURCE               OOCKE;T NUMBER                         EVENT DATE
I 80 80 VIOLATION w 48 Iola! I The three events are. related to placing the cooling towers in service in I 7 8 9 80 lolsl I preparation f'or plant start-up.
    @IT] CON'T         ~I,.........,~I                L1J       lol 51ol-101215151                     1110121617161                   1111111111161 7      8          57 58              . 59         60       61                               68   69                         74   75                 . 80 EVENT DESCRIPTION 10121       I During           plant start-up on October 26 and 27, 1976 three events occurred which re-                                                       I 7     8 9                       .                                                                                                                             80 lol3l     I sulted           in discharge water al)ove the5°F limit.                                 The disi;harges averaged about 3°F                     I 7     8 9                                                                                                                                                     80 lol41 I over the limit. The total time over the limit f'or all three events was 88 minutes . I 7 8 9                             .                                                                                                                         80 lol51 I and the maximum temperature was 11°F over the limit.                                                           (ER-76-35)                              I 7 8 9                                                                                                                                                         80 lol61 7 8 9                                                                             PANE                                                                        80 SYSTEM         CAUSE                                             COMPONENT            COMPONENT CODE           CODE               . COMPONENT CODE               SUPPlER            MANUFACTURER          VIOLATION
NPDES limits were not exceeded.
  @El I HI 7    8 9      10 F   I L!.J 11 lz I z I zI z I z I z I 12                             17 w43 1z1z1z1z1 44                 47 w48 CAUSE DESCRIPTION Iola!     I The       three events are. related to placing the cooling towers in service in                                                                   I 7 89                                                                                                                                                          80 lolsl I preparation f'or plant start-up.                                       NPDES limits were not exceeded.                                                 I 7     B 9                   .                                                                                                                                 80
I 7 B 9 . 80 FACILITY METHOD OF STATUS % POWER OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION fill] L£J I ol o Io I NA I w I NA 7 B 9 10 12 13 44 45 46 80 FORM OF ACTIVITY CONTENT RELEASED OF RELEASE E§1 W L!.J I.._ __
~9.!;----------~------------------------------------....,..-------------------------------------.180
AMOUNT OF ACTIVITY I LOCATION OF RELEASE NA NA 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION [olo I ol l1_J NA 7 8 9 . . 11 12 13 80 PERS.ONNEL INJURIES NUMBER DESCRIPTION EE] 1010101 NA 7 B 9 11 12 80 PROBABLE CONSEQUENCES None 7 8 9 80 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION (Ifil liJ NA 7 B 9 10 80 PUBLICITY 7 B 9 80 illfil 7 B 9 80}}
~E                FACILITY                                                               METHOD OF OTHER STATUS         DISCOVERY                       DISCOVERY DESCRIPTION w
STATUS                % POWER fill]
7    B L£J 9
I ol o Io I 10               12 13 NA              I 44     45 I
46 NA 80 FORM OF ACTIVITY           CONTENT RELEASED         OF RELEASE                AMOUNT OF ACTIVITY                                            LOCATION OF RELEASE E§1             W                   L!.J     I..__ _~---~    NA                    I                                       NA 7     8           9                   10     11                                     44       45                                                             80 PERSONNEL EXPOSURES NUMBER               TYPE       DESCRIPTION
  ~          [olo I ol l1_J                                                                         NA 7     8 9           . . 11         12     13                                                                                                               80 PERS.ONNEL INJURIES NUMBER               DESCRIPTION EE]       1010101                                                                             NA 7     B 9                   11     12                                                                                                                       80 PROBABLE CONSEQUENCES
  ~                      None 7     8 9                                                                                                                                                     80 LOSS OR DAMAGE TO FACILITY TYPE       DESCRIPTION (Ifil     liJ     10 NA 7     B 9                                                                                                                                                     80 PUBLICITY 7     B 9                                                                                                                                                     80 illfilB 9 7                                                                                                                                                             80}}

Latest revision as of 15:17, 2 February 2020

License Event Reports 1976-034-00 & 1976-035-00 Re Discharge Cooling Water Above 5oF Limit
ML18348A277
Person / Time
Site: Palisades Entergy icon.png
Issue date: 11/11/1976
From: Bixel D
Consumers Power Co
To: James Keppler
NRC/RGN-III
References
LER 1976-034-00, LER 1976-035-00
Download: ML18348A277 (3)


Text

} .*..;

consumers

  • Power company General Offices: 212 West Michigan Avenue, Jackson, Michigan 49201
  • Area Code 517 788-0550 November 11, 1976 Mr James G Keppler Office of Inspection and Enforcement Region III US Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 DOCKET 50-255 - LICENSE DPR PALISADES PLANT - ER-76-34 AND 35 ~

DISCHARGE ABOVE 5°F LIMIT Attached are two reportable occurrences which related to the Palisades Plant.

These occurrences involve the discharge of cooling water above the 5°F limit.

However, the plant NPDES limits were not exceeded.

David A Bixel Assistant Nuclear Licensing Administrator NOV 151976

.ICENSEE EVENT REPORT

  • I CONTROL BLOCK: 1...______.._....___.....,.6 .I [PLEASE P~INT ALL REQUIRED INFORMATION] .

LICENSEE LICENSE EVENT NAME LICENSE NUMBER TYPE TYPE 1 IM I I Ip IA IL I 1 I lolo 1--lololololol-lolol l411l1l1l1I 1-0 I 3 I 7 8 9 . 14 15 25 26 . 30 31 32

' REPORT REPORT DOCKl;T NUMBER EVENT CATE REPORT CATE

@IT] CON'T I.....___,I 78 57 58 w w TYPE 59 SOURCE 60 I61ols lol-lo 12151568I l1lol2 lol1l6I I751 I 1 I. i I.1 I 1 I 680I 69 74 EVENT DESCRIPTION 10'21 I Plant operational problems resulted in tripping of the cooling tower pumps. Re- I 7 8 9 . . 80 lol3I I establishment of water box vacuum and pump starting lead to a discharge tempera- I 7 8 9 80 lol41 7 8 9 I ture above . .

the 5°F limit. The maximum temperature was 0.4°F over the limit and I 80 10151 I the total time over the limit was 8 minutes. (ER-76-34) I 7 8 9 80 lolsl 80 7 8 9 PRIME SYSTEM CAUSE COMPONENT CEJMPONENT COMPONENT COOE SUPPl..IER MANUFACTURER VIOLATION w

COOE CODE 7

@0 IHJFI 8 9 10 l!J 11 lzlzlzlzlzlzl 12 17 w43 Iz I ZI z. I z47I 44 48 CAUSE DESCRIPTION lol0I I To reestablish a vacuum in the condenser water box and permit restart of the pumps I 7 8 9 . . . BO

~ I some coolant flow was required. This flow caused the discharge limit to be ex- I 7 B 9 80

~ I ceeded for a short period of time. NPDES limits were not exceeded. I WBs FACILITY . METHOO OF 80 w

STATUS  % POWER OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION EE18 7

L£J 9

I 0 I 0 I 0 I -----*N_A_ ___.I 10 12 13 44 45 46 NA 80 FORM OF rn ACTIVITY CONTENT Rl~SiD r~LiSE l.____AM_o_u_N_T_~-~-A-CT,...IV_IT_Y_ __,I LOCATION OF RELEASE OF I NA 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE OESCRIP.TION 7

~lololol B 9 11 W12 13 NA 80 PERSnNNEL INJURIES NUMBER DESCRIPTION

~I ololol NA 7 8 9 11 12 80 PROBABLE CONSEQUENCES

~ None 7 B 9 80 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION ITifil8 9liJ 7 10 NA 80 PUBLICITY

[ill] NA 7 8 9 BO

  • ADDITIONAL FACTORS 7 8 9 BO l1lfil8 9 7 BO

~

-* _Iii' CONTROL BLOCK:

LICENSEE NAME 9.1cENSEE EVENT REPORT

. _I___.__._I__,___.._.,.j~'

1 5*

LICENSE NUMBER

[PLEASE PRINT ALL REQUIRED INFORMATION]

LICENSE TYPE EVENT TYPE

~IMlrlPIAILl1I lolol~lolololol ol-lolol 14111111111 I oI 3 I 7 8 9 14 15 25 26. 30 31 32 REPORT REPORT TYPE. REPORT DATE w SOURCE OOCKE;T NUMBER EVENT DATE

@IT] CON'T ~I,.........,~I L1J lol 51ol-101215151 1110121617161 1111111111161 7 8 57 58 . 59 60 61 68 69 74 75 . 80 EVENT DESCRIPTION 10121 I During plant start-up on October 26 and 27, 1976 three events occurred which re- I 7 8 9 . 80 lol3l I sulted in discharge water al)ove the5°F limit. The disi;harges averaged about 3°F I 7 8 9 80 lol41 I over the limit. The total time over the limit f'or all three events was 88 minutes . I 7 8 9 . 80 lol51 I and the maximum temperature was 11°F over the limit. (ER-76-35) I 7 8 9 80 lol61 7 8 9 PANE 80 SYSTEM CAUSE COMPONENT COMPONENT CODE CODE . COMPONENT CODE SUPPlER MANUFACTURER VIOLATION

@El I HI 7 8 9 10 F I L!.J 11 lz I z I zI z I z I z I 12 17 w43 1z1z1z1z1 44 47 w48 CAUSE DESCRIPTION Iola! I The three events are. related to placing the cooling towers in service in I 7 89 80 lolsl I preparation f'or plant start-up. NPDES limits were not exceeded. I 7 B 9 . 80

~9.!;----------~------------------------------------....,..-------------------------------------.180

~E FACILITY METHOD OF OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION w

STATUS  % POWER fill]

7 B L£J 9

I ol o Io I 10 12 13 NA I 44 45 I

46 NA 80 FORM OF ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE E§1 W L!.J I..__ _~---~ NA I NA 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION

~ [olo I ol l1_J NA 7 8 9 . . 11 12 13 80 PERS.ONNEL INJURIES NUMBER DESCRIPTION EE] 1010101 NA 7 B 9 11 12 80 PROBABLE CONSEQUENCES

~ None 7 8 9 80 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION (Ifil liJ 10 NA 7 B 9 80 PUBLICITY 7 B 9 80 illfilB 9 7 80