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| document type = OPERATING LICENSES-APPLIATION TO AMEND-RENEW EXISTING, TEXT-LICENSE APPLICATIONS & PERMITS
| document type = OPERATING LICENSES-APPLIATION TO AMEND-RENEW EXISTING, TEXT-LICENSE APPLICATIONS & PERMITS
| page count = 14
| page count = 14
| project =
| stage = Request
}}
}}


=Text=
=Text=
{{#Wiki_filter:P R.ICDR.IMY'
{{#Wiki_filter:R.ICDR.IMY' P'CELERATED   RIDS PROCESSING)
'CELERATED RIDS PROCESSING)
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9504060198 DOC.DATE: 95/03/31 NOTARIZED:
ACCESSION NBR:9504060198                         DOC.DATE: 95/03/31 NOTARIZED: YES       DOCKET FACIL:50-315 Donald C. Cook Nuclear Power Plant, Unit 1, Indiana M                       05000315 50-316 Donald C. Cook Nuclear Power Plant, Unit 2, Indiana M 05000316 AUTH. NAME             AUTHOR AFFILIATION FITZPATRICK,E.       Indiana Michigan Power Co. (formerly Indiana & Michigan Ele RECIP.NAME             RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
YES DOCKET FACIL:50-315 Donald C.Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 50-316 Donald C.Cook Nuclear Power Plant, Unit 2, Indiana M 05000316 AUTH.NAME AUTHOR AFFILIATION FITZPATRICK,E.
SUBZECT:   Application for amends to licenses DPR-58 & DPR-74.Amends
Indiana Michigan Power Co.(formerly Indiana&Michigan Ele RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)SUBZECT: Application for amends to licenses DPR-58&DPR-74.Amends
          . would modify TS 3/4.6.1.7 to allow limited purge operation in modes 1,2,3 & 4 for pressure control,ALARA & respirable air quality considerations.
.would modify TS 3/4.6.1.7 to allow limited purge operation in modes 1,2,3&4 for pressure control,ALARA
DISTRIBUTION CODE: A001D                       COPIES RECEIVED:LTR       ENCL SIZE:
&respirable air quality considerations.
TITLE: OR   Submittal: General Distribution NOTES:
DISTRIBUTION CODE: A001D COPIES RECEIVED:LTR ENCL SIZE: TITLE: OR Submittal:
RECIPIENT                          COPIES          RECIPIENT     COPIES ID CODE/NAME                       LTTR ENCL      ID  CODE/NAME LTTR ENCL PD3-1 LA                               1    1    PD3-1 PD          1    1 HICKMAN,Z                             1    1 INTERNAL~FILE CENTER                               1    1    NMS S/DWM/LLDP    2    2
General Distribution NOTES: RECIPIENT ID CODE/NAME PD3-1 LA HICKMAN,Z INTERNAL~FILE CENTER~01'RR/DRCH/HICB NRR/DSSA/SRXB OGC/HDS2 EXTERNAL: NOAC COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 0 RECIPIENT ID CODE/NAME PD3-1 PD NMS S/DWM/LLDP NRR/DSSA/SPLB NUDOCS-ABSTRACT NRC PDR COPIES LTTR ENCL 1 1 2 2 1 1 1 1 1 1 NOTE TO ALL"RIDS'ECIPIENTS:
                              ~01'RR/DRCH/HICB 1    1    NRR/DSSA/SPLB    1    1 NRR/DSSA/SRXB                         1    1    NUDOCS-ABSTRACT  1    1 OGC/HDS2                               1    0 EXTERNAL: NOAC                                                 NRC PDR          1   1 NOTE TO ALL"RIDS'ECIPIENTS:
PLEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM PI-37 (EXT.504-2083)TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEEDl TOTAL NUMBER OF COPIES REQUIRED: LTTR 13 ENCL 12 fl l indiana Michigan Power Company P.O.Box 16631 Columbus, OH 43216 i4arch 31, 1995 AEP:NRC:1185 Docket Nos.: 50-315 50-316 U.S.Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C.20555 Gentlemen:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM PI-37 (EXT. 504-2083 ) TO ELIMINATEYOUR NAME FROM DISTRIBUTIONLISTS FOR DOCUMENTS YOU DON'T NEEDl TOTAL NUMBER OF COPIES REQUIRED: LTTR                         13  ENCL   12
Donald C.Cook Nuclear Plant Units 1 and 2 PROPOSED AMENDMENT TO TECHNICAL SPECIFICATION SECTION 3/4.6.1.7 FOR CONTAINMENT PURGE REQUIREMENTS and This letter and its attachments constitute an application for amendment to the Technical Specifications (T/Ss)for Donald C.Cook Nuclear Plant Units 1 and 2.Specifically, we are proposing to modify T/Ss 3/4.6.1.7, Containment Ventilation System, and its associated Bases, to allow limited (240 hours annually)purge operation in MODES 1, 2, 3, and 4 for pressure control, ALARA and respirable air quality considerations.
 
The proposed changes will enhance our ability to use the containment purge system to reduce unnecessaiy hardships on plant personnel performing activities in containment.
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Additionally, an increase in allowable purge time is being requested to address improvements in plant operations and capacity factors.Attachment 1 provides a detailed description of the proposed changes, the justification for the changes, and ou'r determination of no significant hazards consideration performed pursuant to 10 CFR 50.92.Attachment 2 contains the existing T/S pages marked to reflect the proposed changes.Attachment 3 contains the revised T/S pages.We believe the proposed changes will not result in (1)a significant increase in.the amounts, and no significant change in the types of any effluent that may be released offsite, or (2)a significant increase in individual or cumulative occupational radiation exposure.These proposed changes have been reviewed by the Plant Nuclear Safety Review Committee and the Nuclear Safety and Design Review Committee.
 
',9504060198 950331 PDR ADDCK 05000315 P PDR'l)  
indiana Michigan Power Company P.O. Box 16631 Columbus, OH 43216 i4arch 31, 1995                                              AEP:NRC:1185 Docket Nos.: 50-315 50-316 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555 Gentlemen:
~, s)f 9 f U.S.Nuclear Regulatory Commission Page 2 AEP:NRC:1185 In compliance with the requirements of 10 CFR 50.91(b)(l), copies of this letter and its attachments have been transmitted to the Michigan Public Service Commission and to the Michigan Department of Public Health.Sincerely, E.E.Fit p trick Vice President SWORN TO AND SUBSCRIBED BEFORE ME THIS~4~~DAY OF QQ~~I~1995
Donald C. Cook Nuclear Plant Units   1 and 2 PROPOSED     AMENDMENT TO TECHNICAL SPECIFICATION SECTION 3/4.6.1.7   FOR CONTAINMENT PURGE REQUIREMENTS and This     letter     and its attachments constitute an application for amendment           to   the   Technical   Specifications     (T/Ss)   for Donald C. Cook Nuclear Plant Units 1 and 2. Specifically, we are proposing to modify T/Ss 3/4.6.1.7, Containment Ventilation System, and its associated Bases, to allow limited (240 hours annually) purge operation in MODES 1, 2, 3, and 4 for pressure control, ALARA and     respirable air quality considerations.         The proposed changes will enhance         our ability to use the containment purge system to reduce unnecessaiy             hardships on plant personnel performing activities in containment. Additionally, an increase in allowable purge time is being requested to address improvements in plant operations and capacity factors.
/0 Nota Public My Commission Expires:~P-$
Attachment 1 provides a detailed description of the proposed changes, the justification for the changes, and ou'r determination of no significant hazards consideration performed pursuant to 10 CFR 50.92. Attachment 2 contains the existing T/S pages marked to reflect the proposed changes. Attachment 3 contains the revised T/S pages.
'$'h Attachments CC: A.A.Blind G.Charnoff J.B.Martin NFEM Section Chief NRC Resident Inspector-Bridgman J.R.Padgett ATTACHMENT 1 TO AEP:NRC:1185 DESCRIPTION AND JUSTIFICATION OF CHANGES 10 CFR 50.92 ANALYSIS FOR CHANGES TO THE DONALD C.COOK NUCLEAR PLANT UNITS 1 AND 2 TECHNICAL SPECIFICATIONS C~w I~w~g~
We     believe the proposed changes will not result in (1) a significant increase in .the amounts, and no significant change in the types of any effluent that may be released offsite, or (2) a significant increase in individual or cumulative occupational radiation exposure.
Attachment 1 to AEP:NRC:1185 Page 1 I.ESCRIPTION OF CHANGES The proposed amendment to Technical Specifications (T/Ss)3/4.6.1.7 makes the following specific changes to the Cook Nuclear Plant Units 1 and 2 T/Ss: T/S 3/4.6.1.7 A.Revises the Limiting Condition for Operation for specification 3/4.6.1.7 (on page 3/4 6-9a)to redefine the conditions in which it is permissible to operate the containment purge system when in MODES 1, 2, 3, and 4.The proposed Limiting Condition for Operation would be modified to read: "The containment purge supply and exhaust isolation valves shall be closed except when operation of the containment purge system is required for;pressure control, ALARA, and respirable air quality considerations for personnel entry and for surveillance testing and maintenance activities." B.Revise the Bases for specification 3/4.6.1.7 (page B 3/4 6-2a)to reflect the activities which allow purging in MODES 1, 2, 3, and 4, as defined above.Additional changes to the bases will include, 1)increasing the allowable purge time from 200 to 240 hours, 2)adding a reference to the ability of the purge isolation valves to close against LOCA forces, thereby assuring 10 CFR 100 guidelines are maintained, and 3)deleting"**" notes corrected during previous amendments.
These     proposed changes have been reviewed by the Plant Nuclear Safety Review Committee and the Nuclear Safety and Design Review Committee.
IX.JUSTIFICATION FOR CHANGES T/S 3/4.6.1.7 We propose to change the wording in both the Limiting Condition For Operation and the Bases of T/S 3/4.6.1.7 to allow limited containment purging while in MODES 1, 2, 3, and 4 for reasons other than"safety related reasons." As currently written,.use of the containment purge system during MODES 1, 2, 3, and 4 is limited to"safety related reasons." These are defined as"the need to improve containment working conditions, e.g., reduce airborne activity, to perform surveillance and/or maintenance on a safety-related system or piece of equipment." Additionally, purge operation is limited to 200 hours, per the technical specification bases.The restrictiveness of this wording results in unnecessary hardship to operators, maintenance technicians, instrument technicians, and other plant workers performing routine tasks in containment.
', 9504060198 950331 PDR       ADDCK 05000315           'l )
For example, maintenance activities related to the upper containment  
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-a I n e Attachment 1 to AEP:NRC:1185 Page 2 ventilation systems and the glycol floor cooling system represent required activities on equipment which is not characterized as"safety related." A change to the specification would allow the limited use of containment purge to address adverse environmental conditions (i.e., temperature, humidity, and/or pressure), ALARA concerns, and to assure that respirable air quality is maintained.
 
It should be noted that the use of the purge system to support the above activities would be restricted to occasions when the existing air filtration and temperature control systems were not sufficient to provide a containment atmosphere supportive of working conditions.
~,
An additional change to T/S 3/4.6.1.7 is to increase the current purge limit of 200 hours per year to 240 hours.The original time limit was calculated based on a unit capacity factor of 77X.As a result of longer operating cycles and improved plant performance, the Cook Nuclear Plant capacity factor is now forecasted to be 93X.Utilizing the same calculation which established the 200 hour limit, and increasing the capacity factor to 93X yields a value of 240 hours.This increased time allotment reflects the additional time the unit will remain in MODES 1, 2, 3, and 4 with a 93K capacity factor.As stated in the technical specification bases, the containment purge system at Cook Nuclear Plant has been designed in accordance with NRC Branch Technical Position CBS 6-4, Rev.1, and demonstrated to be capable of closure against the dynamic forces associated with a loss of coolant accident.The purge valves will receive a containment ventilation isolation signal on both a safety injection and high radiation signals and close within 5 seconds.In accordance with the above Branch Technical Position, the potential site boundary doses were calculated based on the original analysis used to determine the radiological consequences of a loss of coolant accident.The results of this analysis indicated a total thyroid dose of 165 rem for the 0-2 hour site boundary dose and a whole body dose of 9.32 rem.Since physical changes will not result from the proposed amendment, the site boundary does guidelines of 10 CFR 100 (300 rem thyroid and 25 rem whole body)will not be exceeded in the event of an accident during containment purging operations.
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The addition of 40 hours of allowable annual purge time will not result in a significant increase in the amount of effluent released.The Offsite Dose Calculation Manual (ODCM)ensures that the dose rate at any time at the SITE BOUNDARY from gaseous effluent from all units on the site will be within the annual dose limits of Appendix B, Table 2, Column 1 of 10 CFR 20 for UNRESTRICTED AREAS.These specifications will be strictly adhered to during any release via the purge pathway.
 
Attachment 1 to AEP:NRC:1185 Page 3 In conclusion, we believe that the proposed technical specifications will not affect system capability or introduce a new or different mode of purge system operation not previously addressed in the above analysis.III.10 CFR 50 92 CRITERIA Per 10 CFR 50.92, a proposed change does not involve a significant hazards consideration if the change does not: involve a significant increase in the probability or consequences of an accident previously evaluated, 2.create the possibility of a new or different kind of accident from any accident previously evaluated, or 3.involve a significant reduction in a margin of safety.Criter on The purpose of this amendment is to allow flexibility in the use of the containment purge system during MODES 1, 2, 3, and 4.The use of this system during these modes of operation has previously been approved (Amendment No.66).Therefore, this amendment request does not involve a ,significant increase in the probability or consequences of an accident previously evaluated because the proposed change'o the T/Ss does not affect the assumptions, parameters, or results of any UFSAR accident analysis.Based on the existing system design and demonstrated closure capability it is concluded that the proposed changes do not modify the response of the containment during a design basis accident.The proposed amendment does not add or modify any existing equipment.
U. S. Nuclear Regulatory Commission                 AEP:NRC:1185 Page 2 In compliance with the requirements of 10 CFR 50.91(b)(l), copies of this letter and its attachments have been transmitted to the Michigan Public Service Commission and to the Michigan Department of Public Health.
Based on these considerations, it is concluded that the changes do not involve a significant increase in the probability or consequences of an accident previously evaluated.
Sincerely, E. E. Fit p trick Vice President SWORN TO AND SUBSCRIBED BEFORE ME THIS ~4~~   DAY OF QQ~~I~1995
Criterion 2 The proposed change does not involve physical changes to the plant or changes in the plant operating configuration.
                  /0 Nota     Public My Commission   Expires:~P-$ '$'h Attachments CC:   A. A. Blind G. Charnoff J. B. Martin NFEM Section Chief NRC Resident Inspector - Bridgman J. R. Padgett
Thus, it is concluded that the proposed change does not create the possibility of a new or different kind of accident from any accident previously evaluated.
 
Attachment 1 to AEP:NRC:1185 Page 4 Criterion 3 The margin for safety presently provided is not reduced by the proposed change.As discussed previously, the containment purge valves have been designed and demonstrated capable of closure against the dynamic forces resulting from a loss of coolant accident.The proposed amendment does not impact the ability of the purge valves to perform their intended.function (i.e.achieve closure)in the event of an accident.Based on these considerations, it is concluded that the changes do not involve a significant reduction in a margin of safety.IV.CONCLUSION In conclusion, we believe that the proposed change does not involve significant hazards considerations because, as demonstrated in the previous discussions, operation of the Cook Nuclear Plant in accordance with the changes would not: involve a significant increase in the probability or consequences of an accident previously evaluated, 2.create the possibility of a new or different kind of accident from any accident previously evaluated, or 3.involve a significant reduction in a margin of safety.
ATTACHMENT 1 TO AEP:NRC:1185 DESCRIPTION AND JUSTIFICATION OF CHANGES 10 CFR 50.92 ANALYSIS FOR CHANGES TO THE DONALD C. COOK NUCLEAR PLANT UNITS 1 AND 2 TECHNICAL SPECIFICATIONS
ATTACHMENT 2 TO AEP:NRC:1185 EXISTING TECHNICAL SPECIFICATION PAGES MARKED TO REFLECT PROPOSED CHANGES 4\~}}
 
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to AEP:NRC:1185                                         Page 1 I. ESCRIPTION OF CHANGES The proposed amendment to Technical Specifications (T/Ss) 3/4.6.1.7 makes the following specific changes to the Cook Nuclear Plant Units 1 and 2 T/Ss:
T/S 3/4.6.1.7 A.       Revises the   Limiting Condition for Operation for specification 3/4.6.1.7 (on page 3/4 6-9a) to redefine the conditions in which   it is permissible to operate the containment purge system when in MODES 1, 2, 3, and 4. The proposed Limiting Condition for Operation would be modified to read:
              "The containment purge supply and exhaust isolation valves shall be closed except when operation of the containment purge system is required for; pressure         control, ALARA, and respirable air quality considerations for personnel entry and for surveillance testing and maintenance activities."
B.       Revise the Bases for specification 3/4.6.1.7 (page B 3/4 6-2a) to reflect the activities which allow purging in MODES 1, 2, 3, and 4, as defined above. Additional changes to the bases will include, 1) increasing the allowable purge time from 200 to 240 hours, 2) adding a reference to the ability of the purge isolation valves to close against LOCA forces, thereby assuring 10 CFR 100 guidelines are maintained, and 3) deleting
              "**" notes corrected during previous amendments.
IX. JUSTIFICATION FOR     CHANGES T/S 3/4.6.1.7 We propose to change the wording in both the Limiting Condition For Operation and the Bases of T/S 3/4.6.1.7 to allow limited containment purging while in MODES 1, 2, 3, and 4 for reasons other than "safety related reasons."
As currently written,. use of the containment purge system during MODES   1, 2, 3, and 4 is limited to "safety related reasons." These are defined as "the need to improve containment working conditions, e.g., reduce airborne activity, to perform surveillance and/or maintenance on a safety-related system or piece of equipment."
Additionally, purge operation is limited to 200 hours, per the technical specification bases.
The restrictiveness of this wording results in unnecessary hardship to operators, maintenance technicians, instrument technicians, and other plant workers performing routine tasks in containment. For example, maintenance activities related to the upper containment
 
-a I n e
to AEP:NRC:1185                                       Page 2 ventilation systems     and the glycol floor cooling system represent required activities     on equipment which is not characterized as "safety related."
A change     to the specification would allow the limited use of containment purge to address adverse environmental conditions (i.e.,
temperature, humidity, and/or pressure), ALARA concerns, and to assure that respirable air quality is maintained.         It should be noted that the use of the purge system to support the above activities would be restricted to occasions when the existing air filtration and temperature control systems were not sufficient to provide a containment atmosphere supportive of working conditions.
An additional change to T/S 3/4.6.1.7 is to increase the current purge   limit of 200 hours per year to 240 hours. The original time limit was calculated based on a unit capacity factor of 77X. As a result of longer operating cycles and improved plant performance, the Cook Nuclear Plant capacity factor is now forecasted to be 93X.
Utilizing the same calculation which established the 200 hour limit, and increasing the capacity factor to 93X yields a value of 240 hours. This increased time allotment reflects the additional time the unit will remain in MODES 1, 2, 3, and 4 with a 93K capacity factor.
As   stated in the technical specification bases, the containment purge system at Cook Nuclear Plant has been designed in accordance with NRC Branch Technical Position CBS 6-4, Rev. 1, and demonstrated to be capable of closure against the dynamic forces associated with a loss of coolant accident.         The purge valves will receive a containment ventilation isolation signal on both a safety injection and high radiation signals and close within 5 seconds.             In accordance with the above Branch Technical Position, the potential site boundary doses were calculated based on the original analysis used to determine the radiological consequences of a loss of coolant accident. The results of this analysis indicated a total thyroid dose   of 165 rem for the 0-2 hour site boundary dose and a whole body dose   of 9.32 rem. Since physical changes will not result from the proposed amendment, the site boundary does guidelines of 10 CFR 100 (300 rem thyroid and 25 rem whole body) will not be exceeded in the event of an accident during containment purging operations.
The   addition of 40 hours of allowable annual purge time will not result in a significant increase in the amount of effluent released.
The Offsite Dose Calculation Manual (ODCM) ensures that the dose rate at any time at the SITE BOUNDARY from gaseous effluent from all units on the site will be within the annual dose limits of Appendix B, Table 2, Column 1 of 10 CFR 20 for UNRESTRICTED AREAS. These specifications will be strictly adhered to during any release via the purge pathway.
to AEP:NRC:1185                                           Page 3 In conclusion,     we believe that the proposed technical specifications will not affect       system capability or introduce a new or different mode   of   purge system operation not previously addressed in the above analysis.
III. 10 CFR 50 92 CRITERIA Per 10 CFR 50.92, a proposed change does not involve a           significant hazards consideration         if the change does not:
involve     a   significant increase in the probability or consequences     of an accident previously evaluated,
: 2.       create the possibility of a new or different kind of accident from any accident previously evaluated, or
: 3.       involve   a   significant reduction in   a margin of safety.
Criter on The purpose     of this amendment is to allow flexibility in the use of the containment purge system during MODES 1, 2, 3, and 4. The use of this system during these modes of operation has previously been approved (Amendment No. 66). Therefore, this amendment request does not involve a ,significant increase in the probability or consequences       of an accident previously evaluated because the proposed change       'o   the T/Ss does not affect the assumptions, parameters, or results of any UFSAR accident analysis. Based on the existing system design and demonstrated closure capability             it is concluded that the proposed changes do not modify the response of the containment during a design basis accident. The proposed amendment does not add or modify any existing equipment.           Based on these considerations,           it is concluded that the changes do not involve a significant increase in the probability or consequences of an accident previously evaluated.
Criterion   2 The proposed change does         not involve physical changes to the plant or changes in the plant operating configuration. Thus,                 it is concluded that the proposed change does not         create the possibility of a new or different kind of accident from any accident previously evaluated.
to AEP:NRC:1185                                           Page 4 Criterion 3 The margin for safety presently provided is not reduced by the proposed change.         As discussed previously, the containment purge valves have been designed and demonstrated capable of closure against the dynamic forces resulting from a loss of coolant accident. The proposed amendment does not impact the ability of the purge valves to perform their intended .function (i.e. achieve closure) in the event of an accident.                   Based   on these considerations,       it is concluded that the changes do not involve a significant reduction in a margin of safety.
IV. CONCLUSION In conclusion, we believe that the proposed       change does not involve significant hazards considerations because,         as demonstrated in the previous discussions, operation of the           Cook Nuclear Plant in accordance with the changes would not:
involve   a   significant increase in the probability or consequences     of an accident previously evaluated,
: 2.     create the possibility of a new or different kind of accident from any accident previously evaluated, or
: 3.      involve  a  significant reduction in  a margin  of safety.
 
ATTACHMENT 2 TO AEP:NRC:1185 EXISTING TECHNICAL SPECIFICATION PAGES MARKED TO REFLECT PROPOSED CHANGES
 
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Latest revision as of 04:10, 16 November 2019

Application for Amends to Licenses DPR-58 & DPR-74.Amends Would Modify TS 3/4.6.1.7 to Allow Limited Purge Operation in Modes 1,2,3 & 4 for Pressure Control,Alara & Respirable Air Quality Considerations
ML17332A720
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 03/31/1995
From: Fitzpatrick E
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
Shared Package
ML17332A721 List:
References
AEP:NRC:1185, NUDOCS 9504060198
Download: ML17332A720 (14)


Text

R.ICDR.IMY' P'CELERATED RIDS PROCESSING)

REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9504060198 DOC.DATE: 95/03/31 NOTARIZED: YES DOCKET FACIL:50-315 Donald C. Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 50-316 Donald C. Cook Nuclear Power Plant, Unit 2, Indiana M 05000316 AUTH. NAME AUTHOR AFFILIATION FITZPATRICK,E. Indiana Michigan Power Co. (formerly Indiana & Michigan Ele RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

SUBZECT: Application for amends to licenses DPR-58 & DPR-74.Amends

. would modify TS 3/4.6.1.7 to allow limited purge operation in modes 1,2,3 & 4 for pressure control,ALARA & respirable air quality considerations.

DISTRIBUTION CODE: A001D COPIES RECEIVED:LTR ENCL SIZE:

TITLE: OR Submittal: General Distribution NOTES:

RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD3-1 LA 1 1 PD3-1 PD 1 1 HICKMAN,Z 1 1 INTERNAL~FILE CENTER 1 1 NMS S/DWM/LLDP 2 2

~01'RR/DRCH/HICB 1 1 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 NUDOCS-ABSTRACT 1 1 OGC/HDS2 1 0 EXTERNAL: NOAC NRC PDR 1 1 NOTE TO ALL"RIDS'ECIPIENTS:

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM PI-37 (EXT. 504-2083 ) TO ELIMINATEYOUR NAME FROM DISTRIBUTIONLISTS FOR DOCUMENTS YOU DON'T NEEDl TOTAL NUMBER OF COPIES REQUIRED: LTTR 13 ENCL 12

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indiana Michigan Power Company P.O. Box 16631 Columbus, OH 43216 i4arch 31, 1995 AEP:NRC:1185 Docket Nos.: 50-315 50-316 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555 Gentlemen:

Donald C. Cook Nuclear Plant Units 1 and 2 PROPOSED AMENDMENT TO TECHNICAL SPECIFICATION SECTION 3/4.6.1.7 FOR CONTAINMENT PURGE REQUIREMENTS and This letter and its attachments constitute an application for amendment to the Technical Specifications (T/Ss) for Donald C. Cook Nuclear Plant Units 1 and 2. Specifically, we are proposing to modify T/Ss 3/4.6.1.7, Containment Ventilation System, and its associated Bases, to allow limited (240 hours0.00278 days <br />0.0667 hours <br />3.968254e-4 weeks <br />9.132e-5 months <br /> annually) purge operation in MODES 1, 2, 3, and 4 for pressure control, ALARA and respirable air quality considerations. The proposed changes will enhance our ability to use the containment purge system to reduce unnecessaiy hardships on plant personnel performing activities in containment. Additionally, an increase in allowable purge time is being requested to address improvements in plant operations and capacity factors.

Attachment 1 provides a detailed description of the proposed changes, the justification for the changes, and ou'r determination of no significant hazards consideration performed pursuant to 10 CFR 50.92. Attachment 2 contains the existing T/S pages marked to reflect the proposed changes. Attachment 3 contains the revised T/S pages.

We believe the proposed changes will not result in (1) a significant increase in .the amounts, and no significant change in the types of any effluent that may be released offsite, or (2) a significant increase in individual or cumulative occupational radiation exposure.

These proposed changes have been reviewed by the Plant Nuclear Safety Review Committee and the Nuclear Safety and Design Review Committee.

', 9504060198 950331 PDR ADDCK 05000315 'l )

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U. S. Nuclear Regulatory Commission AEP:NRC:1185 Page 2 In compliance with the requirements of 10 CFR 50.91(b)(l), copies of this letter and its attachments have been transmitted to the Michigan Public Service Commission and to the Michigan Department of Public Health.

Sincerely, E. E. Fit p trick Vice President SWORN TO AND SUBSCRIBED BEFORE ME THIS ~4~~ DAY OF QQ~~I~1995

/0 Nota Public My Commission Expires:~P-$ '$'h Attachments CC: A. A. Blind G. Charnoff J. B. Martin NFEM Section Chief NRC Resident Inspector - Bridgman J. R. Padgett

ATTACHMENT 1 TO AEP:NRC:1185 DESCRIPTION AND JUSTIFICATION OF CHANGES 10 CFR 50.92 ANALYSIS FOR CHANGES TO THE DONALD C. COOK NUCLEAR PLANT UNITS 1 AND 2 TECHNICAL SPECIFICATIONS

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to AEP:NRC:1185 Page 1 I. ESCRIPTION OF CHANGES The proposed amendment to Technical Specifications (T/Ss) 3/4.6.1.7 makes the following specific changes to the Cook Nuclear Plant Units 1 and 2 T/Ss:

T/S 3/4.6.1.7 A. Revises the Limiting Condition for Operation for specification 3/4.6.1.7 (on page 3/4 6-9a) to redefine the conditions in which it is permissible to operate the containment purge system when in MODES 1, 2, 3, and 4. The proposed Limiting Condition for Operation would be modified to read:

"The containment purge supply and exhaust isolation valves shall be closed except when operation of the containment purge system is required for; pressure control, ALARA, and respirable air quality considerations for personnel entry and for surveillance testing and maintenance activities."

B. Revise the Bases for specification 3/4.6.1.7 (page B 3/4 6-2a) to reflect the activities which allow purging in MODES 1, 2, 3, and 4, as defined above. Additional changes to the bases will include, 1) increasing the allowable purge time from 200 to 240 hours0.00278 days <br />0.0667 hours <br />3.968254e-4 weeks <br />9.132e-5 months <br />, 2) adding a reference to the ability of the purge isolation valves to close against LOCA forces, thereby assuring 10 CFR 100 guidelines are maintained, and 3) deleting

"**" notes corrected during previous amendments.

IX. JUSTIFICATION FOR CHANGES T/S 3/4.6.1.7 We propose to change the wording in both the Limiting Condition For Operation and the Bases of T/S 3/4.6.1.7 to allow limited containment purging while in MODES 1, 2, 3, and 4 for reasons other than "safety related reasons."

As currently written,. use of the containment purge system during MODES 1, 2, 3, and 4 is limited to "safety related reasons." These are defined as "the need to improve containment working conditions, e.g., reduce airborne activity, to perform surveillance and/or maintenance on a safety-related system or piece of equipment."

Additionally, purge operation is limited to 200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br />, per the technical specification bases.

The restrictiveness of this wording results in unnecessary hardship to operators, maintenance technicians, instrument technicians, and other plant workers performing routine tasks in containment. For example, maintenance activities related to the upper containment

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to AEP:NRC:1185 Page 2 ventilation systems and the glycol floor cooling system represent required activities on equipment which is not characterized as "safety related."

A change to the specification would allow the limited use of containment purge to address adverse environmental conditions (i.e.,

temperature, humidity, and/or pressure), ALARA concerns, and to assure that respirable air quality is maintained. It should be noted that the use of the purge system to support the above activities would be restricted to occasions when the existing air filtration and temperature control systems were not sufficient to provide a containment atmosphere supportive of working conditions.

An additional change to T/S 3/4.6.1.7 is to increase the current purge limit of 200 hours0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> per year to 240 hours0.00278 days <br />0.0667 hours <br />3.968254e-4 weeks <br />9.132e-5 months <br />. The original time limit was calculated based on a unit capacity factor of 77X. As a result of longer operating cycles and improved plant performance, the Cook Nuclear Plant capacity factor is now forecasted to be 93X.

Utilizing the same calculation which established the 200 hour0.00231 days <br />0.0556 hours <br />3.306878e-4 weeks <br />7.61e-5 months <br /> limit, and increasing the capacity factor to 93X yields a value of 240 hours0.00278 days <br />0.0667 hours <br />3.968254e-4 weeks <br />9.132e-5 months <br />. This increased time allotment reflects the additional time the unit will remain in MODES 1, 2, 3, and 4 with a 93K capacity factor.

As stated in the technical specification bases, the containment purge system at Cook Nuclear Plant has been designed in accordance with NRC Branch Technical Position CBS 6-4, Rev. 1, and demonstrated to be capable of closure against the dynamic forces associated with a loss of coolant accident. The purge valves will receive a containment ventilation isolation signal on both a safety injection and high radiation signals and close within 5 seconds. In accordance with the above Branch Technical Position, the potential site boundary doses were calculated based on the original analysis used to determine the radiological consequences of a loss of coolant accident. The results of this analysis indicated a total thyroid dose of 165 rem for the 0-2 hour site boundary dose and a whole body dose of 9.32 rem. Since physical changes will not result from the proposed amendment, the site boundary does guidelines of 10 CFR 100 (300 rem thyroid and 25 rem whole body) will not be exceeded in the event of an accident during containment purging operations.

The addition of 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> of allowable annual purge time will not result in a significant increase in the amount of effluent released.

The Offsite Dose Calculation Manual (ODCM) ensures that the dose rate at any time at the SITE BOUNDARY from gaseous effluent from all units on the site will be within the annual dose limits of Appendix B, Table 2, Column 1 of 10 CFR 20 for UNRESTRICTED AREAS. These specifications will be strictly adhered to during any release via the purge pathway.

to AEP:NRC:1185 Page 3 In conclusion, we believe that the proposed technical specifications will not affect system capability or introduce a new or different mode of purge system operation not previously addressed in the above analysis.

III. 10 CFR 50 92 CRITERIA Per 10 CFR 50.92, a proposed change does not involve a significant hazards consideration if the change does not:

involve a significant increase in the probability or consequences of an accident previously evaluated,

2. create the possibility of a new or different kind of accident from any accident previously evaluated, or
3. involve a significant reduction in a margin of safety.

Criter on The purpose of this amendment is to allow flexibility in the use of the containment purge system during MODES 1, 2, 3, and 4. The use of this system during these modes of operation has previously been approved (Amendment No. 66). Therefore, this amendment request does not involve a ,significant increase in the probability or consequences of an accident previously evaluated because the proposed change 'o the T/Ss does not affect the assumptions, parameters, or results of any UFSAR accident analysis. Based on the existing system design and demonstrated closure capability it is concluded that the proposed changes do not modify the response of the containment during a design basis accident. The proposed amendment does not add or modify any existing equipment. Based on these considerations, it is concluded that the changes do not involve a significant increase in the probability or consequences of an accident previously evaluated.

Criterion 2 The proposed change does not involve physical changes to the plant or changes in the plant operating configuration. Thus, it is concluded that the proposed change does not create the possibility of a new or different kind of accident from any accident previously evaluated.

to AEP:NRC:1185 Page 4 Criterion 3 The margin for safety presently provided is not reduced by the proposed change. As discussed previously, the containment purge valves have been designed and demonstrated capable of closure against the dynamic forces resulting from a loss of coolant accident. The proposed amendment does not impact the ability of the purge valves to perform their intended .function (i.e. achieve closure) in the event of an accident. Based on these considerations, it is concluded that the changes do not involve a significant reduction in a margin of safety.

IV. CONCLUSION In conclusion, we believe that the proposed change does not involve significant hazards considerations because, as demonstrated in the previous discussions, operation of the Cook Nuclear Plant in accordance with the changes would not:

involve a significant increase in the probability or consequences of an accident previously evaluated,

2. create the possibility of a new or different kind of accident from any accident previously evaluated, or
3. involve a significant reduction in a margin of safety.

ATTACHMENT 2 TO AEP:NRC:1185 EXISTING TECHNICAL SPECIFICATION PAGES MARKED TO REFLECT PROPOSED CHANGES

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