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{{#Wiki_filter:REGULATORYIFORMATION DISTRIBUTION SYEIA(RIDE)ACCUSSIIlfNNBR8'5290295 DOC8DATE~84/05/21NOTARIZED~NODOCKETFACIL:50316DonaldO~CookNuclearPowerPlentyUnit2FIndiana805000316AUTH~NAI<EAUTIIORAFFILIATION
{{#Wiki_filter:REGULATORYIFORMATION DISTRIBUTION SYEIA (RIDE)ACCUS SI IlfN NBR 8'5290295 DOC 8 DATE~84/05/2 1 NOTARI ZED~NO DOCKET FACIL:50 316 Donald O~Cook Nuclear Power Plenty Unit 2F Indiana 8 05000316 AUTH~NAI<E AUTIIOR AFFILIATION
)ALEXICHFM.P, Indiana8MichiganElectricCo,RECIP~NAMERECIPIENT AFFILIATION DENTONFHBR
)ALEXICHFM.P, Indiana 8 Michigan Electr ic Co, RECIP~NAME RECIPIENT AFFILIATION DENTONFHBR
~OfficeofNuclearReactorRegulationi Director
~Office of Nuclear Reactor Regulationi Director  


==SUBJECT:==
==SUBJECT:==
Revisedapplication foramendtoLicenseDPR74.Amendreflectsaddilimitation onnuclearenthalpyrisehotchannelfactorduetonewLOCA/ECCS analysisinsupportofCycle5re'load.Application partof8ff0301submittal+
Revised application for amend to License DPR 74.Amend reflects addi limitation on nuclear enthalpy rise hot channel factor due to new LOCA/ECCS analysis in support of Cycle 5 re'load.Application part of 8ff0301 submittal+
DISTRIBUTION CODE:IE26SCOPIESRECEIVED:LTR ENCLgSIZEGjL4,2~I(,TITLE:Start-UpReport/Refueling Report(50kt)NOTES:RECIPIENT IDCODE/NAME NRRORB1BC04INTERNAI.:
DISTRIBUTION CODE: IE26S COPIES RECEIVED:LTR ENCL g SIZEG j L 4, 2~I(, TITLE: Start-Up Repor t/Refueling Repor t (50 kt)NOTES: RECIPIENT ID CODE/NAME NRR ORB1 BC 04 INTERNAI.:
IEFILEOlNRR/DHFSDIR08NRR/DSI/CPB 12COPIESLTTRENCL33111111RECIPIENT IDCODE/NAME NRR/DHFSDEPY07NRR/DHFS/PSRB11 RM/DDAMI/MIB09COPIESLTTRENCLEXTERNAL:
IE FILE Ol NRR/DHFS DIR 08 NRR/DSI/CPB 12 COPIES LTTR ENCL 3 3 1 1 1 1 1 1 RECIPIENT ID CODE/NAME NRR/DHFS DEPY07 NRR/DHFS/PSRB11 RM/DDAMI/MI B 09 COPIES LTTR ENCL EXTERNAL: ACRS 13 NRC PDR 02 NTIS 5 5 1 1 1 1 LPDR NSIC 03 05 COri)~~.e.Fi~TOTAL NUMBER OF.COPIES REQUIRED: LTTR 18 ENCL 18 It iin nn nIi I H)i'ii~
ACRS13NRCPDR02NTIS551111LPDRNSIC0305COri)~~.e.Fi~TOTALNUMBEROF.COPIESREQUIRED:
INDIANA 8 NICHIGAN ELECTRIC COMPANY P.O, BOX 16631 COLUMBUS, OHIO 43216 May 21, 1984 AEP:NRC:0860K Donald C.Cook Nuclear Plant Unit No.2 Docket No.50-316 License No.DPR-74 REVISION TO THE APPLICATION FOR CHANGES TO THE UNIT 2 TECHNICAL SPECIFICATION FOR THE CYCLE 5 RELOAD Mr.Harold R.Denton, Director Office of Nuclear Reactor Regulation U.S.Nuclear Regulatory Commission Washington, D.C.20555  
LTTR18ENCL18 ItiinnnnIiIH)i'ii~
INDIANA8NICHIGANELECTRICCOMPANYP.O,BOX16631COLUMBUS, OHIO43216May21,1984AEP:NRC:0860K DonaldC.CookNuclearPlantUnitNo.2DocketNo.50-316LicenseNo.DPR-74REVISIONTOTHEAPPLICATION FORCHANGESTOTHEUNIT2TECHNICAL SPECIFICATION FORTHECYCLE5RELOADMr.HaroldR.Denton,DirectorOfficeofNuclearReactorRegulation U.S.NuclearRegulatory Commission Washington, D.C.20555


==DearMr.Denton:==
==Dear Mr.Denton:==
Thisletteranditsattachments constitute arevisiontoourapplication (AEP:NRC:0860, datedMarch1,1984)foramendment totheDonaldC.CookNuclearPlantUnitNo.2AppendixATechnical Specifications (T/S).ThisproposedrevisionisinresponsetoconcernsraisedbytheNRCduringthereviewofourproposedUnit2Cycle5reloadlicenseapplication.
This letter and its attachments constitute a revision to our application (AEP:NRC:0860, dated March 1, 1984)for amendment to the Donald C.Cook Nuclear Plant Unit No.2 Appendix A Technical Specifications (T/S).This proposed revision is in response to concerns raised by the NRC during the review of our proposed Unit 2 Cycle 5 reload license application.
Specifically, theproposedchangereflectsanadditional limitation onthenuclearenthalpyrisehotchannelfactor(FI"),duetothenewLOCA/ECCS bHanalysis.
Specifically, the proposed change reflects an additional limitation on the nuclear enthalpy rise hot channel factor (F I"), due to the new LOCA/ECCS bH analysis.The analysis was performed in support of the Cycle 5 reload as a result of your staff's review.Attachment 1 to this letter provides the results and bases of the new LOCA/ECCS analysis as it relates to F><.The analysis was performed by our fuels vendor (Exxon Nuclear, Co.).The results of this analysis were not available to us until May 18, 1984.We met with your staff on May 18, 1984 in an open meeting to discuss the results of the new analysis and our suggested T/S changes.We have revised the proposed T/S based on the NRC's comments.Due to the fact that our Unit 2 startup (i.e., entry into MODE 4)is currently scheduled for June 10, 1984 and that we, were only able to verify the need for the proposed change very recently, we request that the time for notice and publication in the Federal Register be shortened on schedule commensurate with our scheduled reload startup date;Based on our review, the proposed change to the technical specification is based on analytical methods which we were told were found acceptable to the NRC.In addition, the results of the analysis are within all acceptance criteria with respect to the ECCS.Therefore, we believe the proposed change does not involve a significant hazards consideration as defined in 10 CFR 50.92.In addition, since the proposed T/S keeps the plant within all design bases, the change will not adversely impact the environment.
Theanalysiswasperformed insupportoftheCycle5reloadasaresultofyourstaff'sreview.Attachment 1tothisletterprovidestheresultsandbasesofthenewLOCA/ECCS analysisasitrelatestoF><.Theanalysiswasperformed byourfuelsvendor(ExxonNuclear,Co.).Theresultsofthisanalysiswerenotavailable tousuntilMay18,1984.WemetwithyourstaffonMay18,1984inanopenmeetingtodiscusstheresultsofthenewanalysisandoursuggested T/Schanges.WehaverevisedtheproposedT/SbasedontheNRC'scomments.
':.8405290295 840521 ,'PDR ADOCK 05000316.sp;PDR CpP g II I Mr.Harold R.Den AEP: NRC: 0860K Attachment 2 to this letter contains the proposed revised T/S pages.The changes are indicated by vertical bars drawn on the right hand margin of the page.The proposed changes have been reviewed by the Plant Nuclear Safety Review Committee and will be reviewed by the Nuclear Safety and Design Review Committee at its next meeting.Pursuant to the requirement of 10 CFR 50.91(b)(1), a copy of this letter and its attachments have been transmitted to the State of Michigan.In addition, commensurate with our request for shortening the period for notice and publication in the Federal Register, we notified the State of Michigan by, telephone on May 21, 1984 of this requested amendment to our T/S.We consider this application for a licensee amendment to be part of the application submitted in our letter AEP:NRC:0860.
DuetothefactthatourUnit2startup(i.e.,entryintoMODE4)iscurrently scheduled forJune10,1984andthatwe,wereonlyabletoverifytheneedfortheproposedchangeveryrecently, werequestthatthetimefornoticeandpublication intheFederalRegisterbeshortened onschedulecommensurate withourscheduled reloadstartupdate;Basedonourreview,theproposedchangetothetechnical specification isbasedonanalytical methodswhichweweretoldwerefoundacceptable totheNRC.Inaddition, theresultsoftheanalysisarewithinallacceptance criteriawithrespecttotheECCS.Therefore, webelievetheproposedchangedoesnotinvolveasignificant hazardsconsideration asdefinedin10CFR50.92.Inaddition, sincetheproposedT/Skeepstheplantwithinalldesignbases,thechangewillnotadversely impacttheenvironment.
Therefore, we interpret.
':.8405290295 840521,'PDRADOCK05000316.sp;PDR CpPgIII Mr.HaroldR.DenAEP:NRC:0860KAttachment 2tothislettercontainstheproposedrevisedT/Spages.Thechangesareindicated byverticalbarsdrawnontherighthandmarginofthepage.TheproposedchangeshavebeenreviewedbythePlantNuclearSafetyReviewCommittee andwillbereviewedbytheNuclearSafetyandDesignReviewCommittee atitsnextmeeting.Pursuanttotherequirement of10CFR50.91(b)(1),
10 CFR 170.22 as not requiring any additional payments for processing the aforementioned request.This document has been prepared following Corporate procedures which incorporate a reasonable set of controls to insure its accuracy and, completeness
acopyofthisletteranditsattachments havebeentransmitted totheStateofMichigan.
'prior to signature by the undersigned.
Inaddition, commensurate withourrequestforshortening theperiodfornoticeandpublication intheFederalRegister, wenotifiedtheStateofMichiganby,telephone onMay21,1984ofthisrequested amendment toourT/S.Weconsiderthisapplication foralicenseeamendment tobepartoftheapplication submitted inourletterAEP:NRC:0860.
Very truly your I M.P.Ale hach Vice Pre ident MPA/dew Attachment cc: John E.Dolan W.G.Smith, Jr.-Bridgman R.C.Callen G.Charnoff E.R.Swanson, NRC Resident Inspector-Bridgman 0 J!'1 p l, I 1 I ap I ll E Mr.Harold R.Dent AEP:NRC:0860K ATTACHMENT 1 The LOCA/ECCS analysis for Unit 2, Cycle 5 operation with up to five percent (5%)of the steam generator tubes plugged was performed by Exxon Nuclear Co.(ENC).The analysis was performed using the EXEM/PWR model with changes as explained in the ENC letter JCC:076:84 dated May 7, 1984.Letter JCC:076:84 was transmitted to you in our letter AEP:NRC:0860F, dated May ll, 1984.The results of the new ECCS/LOCA analysis are presented in the attached Tables 2.1, 3.2, 3.4, and Figures 3.41, 3.42, and 3.43.For breaks up to and including the double-ended severance o'f a reactor coolant pipe, the new analysis showed that the Unit 2 Emergency Core Cooling System will meet the acceptance criteria as presented in 10 CFR 50.46 for operation with ENC 17x17 fuel operating in accordance with the peaking factor limits noted in Table 2.1.That is: 1.The calculated'eak fuel element clad temperature o does not exceed the 2200 F limit.2.The amount of fuel element cladding that reacts chemically with water or steam does not exceed 1%of the total amount of zircaloy in the reactor.3.The cladding temperature transient is terminated at a time when the core geometry is still amenable to cooling.The hot fuel and cladding oxidation limits of 17%are not exceeded during or after quenching.
Therefore, weinterpret.
4.The core temperature is reduced and decay heat is removed for an extended period of time, as required by the long-lived radioactivity remaining in the core.Based on the new LOCA/ECCS analysis performed, the limit on F H, is 1.415.When included in the,T/S, this value is reduced by 4 0 to account for measurement uncertainty.
10CFR170.22asnotrequiring anyadditional paymentsforprocessing theaforementioned request.Thisdocumenthasbeenpreparedfollowing Corporate procedures whichincorporate areasonable setofcontrolstoinsureitsaccuracyand,completeness
Thus the F<limit for operation at hH AH 100%power is 1.36.Xn addition to the above limitation, it was also necessary to change the allowance for increased F~based on reduced power when F~<is limited , AH H.by ECCS analyses, but not limited by Departure from Nucleate Boiling (DNB).This change is reflected by the phrase"F<~~1.36/P for Exxon Nuclear Co.fuel" included in the revised Technical Specifications.
'priortosignature bytheundersigned.
e'I 1 4~(I~g P h C P'I g Pd W'g~i,'1)V C f.>J V f II)p II i U'"~"(1 III t I'I.'l I l Q)'V$f L l f%'J'l Lf'lg I'I l c i'I Mr.Harold R.Den f<J AEP:NRC:0860K bc: J.G.Feinstein J.M.Cleveland/G.
VerytrulyyourIM.P.AlehachVicePreidentMPA/dewAttachment cc:JohnE.DolanW.G.Smith,Jr.-BridgmanR.C.CallenG.CharnoffE.R.Swanson,NRCResidentInspector
L.John/V.Vanderburg H.N.Scherer, Jr./S.H.Horowitz/R.
-Bridgman 0J!'1pl,I1IapIllE Mr.HaroldR.DentAEP:NRC:0860K ATTACHMENT 1TheLOCA/ECCS analysisforUnit2,Cycle5operation withuptofivepercent(5%)ofthesteamgenerator tubespluggedwasperformed byExxonNuclearCo.(ENC).Theanalysiswasperformed usingtheEXEM/PWRmodelwithchangesasexplained intheENCletterJCC:076:84 datedMay7,1984.LetterJCC:076:84 wastransmitted toyouinourletterAEP:NRC:0860F, datedMayll,1984.TheresultsofthenewECCS/LOCA analysisarepresented intheattachedTables2.1,3.2,3.4,andFigures3.41,3.42,and3.43.Forbreaksuptoandincluding thedouble-ended severance o'fareactorcoolantpipe,thenewanalysisshowedthattheUnit2Emergency CoreCoolingSystemwillmeettheacceptance criteriaaspresented in10CFR50.46foroperation withENC17x17fueloperating inaccordance withthepeakingfactorlimitsnotedinTable2.1.Thatis:1.Thecalculated'eak fuelelementcladtemperature odoesnotexceedthe2200Flimit.2.Theamountoffuelelementcladdingthatreactschemically withwaterorsteamdoesnotexceed1%ofthetotalamountofzircaloyinthereactor.3.Thecladdingtemperature transient isterminated atatimewhenthecoregeometryisstillamenabletocooling.Thehotfuelandcladdingoxidation limitsof17%arenotexceededduringorafterquenching.
C.Carruth R.F.Hering/S.H.Steinhart/J.
4.Thecoretemperature isreducedanddecayheatisremovedforanextendedperiodoftime,asrequiredbythelong-lived radioactivity remaining inthecore.BasedonthenewLOCA/ECCS analysisperformed, thelimitonFH,is1.415.Whenincludedinthe,T/S,thisvalueisreducedby40toaccountformeasurement uncertainty.
A.Kobyra R.W.Jurgensen R.F.Kroeger T.P.Beilman-Bridgman J.F.Stietzel-Bridgman B.H.Bennett/F.
ThustheF<limitforoperation athHAH100%poweris1.36.Xnadditiontotheabovelimitation, itwasalsonecessary tochangetheallowance forincreased F~basedonreducedpowerwhenF~<islimited,AHH.byECCSanalyses, butnotlimitedbyDeparture fromNucleateBoiling(DNB).Thischangeisreflected bythephrase"F<~~1.36/PforExxonNuclearCo.fuel"includedintherevisedTechnical Specifications.
S.VanPelt, Jr.J.B.Shinnock D.Wigginton, NRC-Washington, D.C., AEP:NRC:0860K DC-N-6015.1 DC-N-6485'NMFM 233
e'I14~(I~gPhCP'IgPdW'g~i,'1)VCf.>JVfII)pIIiU'"~"(1IIItI'I.'lIlQ)'V$fLlf%'J'lLf'lgI'Ilci'I Mr.HaroldR.Denf<JAEP:NRC:0860K bc:J.G.Feinstein J.M.Cleveland/G.
,1 f 4'r~J f 3 l'I w f I'I}}
L.John/V.Vanderburg H.N.Scherer,Jr./S.H.Horowitz/R.
C.CarruthR.F.Hering/S.
H.Steinhart/J.
A.KobyraR.W.Jurgensen R.F.KroegerT.P.Beilman-BridgmanJ.F.Stietzel-BridgmanB.H.Bennett/F.
S.VanPelt,Jr.J.B.ShinnockD.Wigginton, NRC-Washington, D.C.,AEP:NRC:0860K DC-N-6015.1 DC-N-6485
'NMFM233
,1f4'r~Jf3l'IwfI'I}}

Revision as of 08:54, 6 July 2018

Revised Application for Amend to License DPR-74.Amend Reflects Addl Limitation on Nuclear Enthalpy Rise Hot Channel Factor Due to New Loca/Eccs Analysis in Support of Cycle 5 Reload.Application Part of 840301 Submittal
ML17320B073
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 05/21/1984
From: ALEXICH M P
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To: DENTON H R
Office of Nuclear Reactor Regulation
Shared Package
ML17320B074 List:
References
AEP:NRC:0860K, AEP:NRC:860K, NUDOCS 8405290295
Download: ML17320B073 (10)


Text

REGULATORYIFORMATION DISTRIBUTION SYEIA (RIDE)ACCUS SI IlfN NBR 8'5290295 DOC 8 DATE~84/05/2 1 NOTARI ZED~NO DOCKET FACIL:50 316 Donald O~Cook Nuclear Power Plenty Unit 2F Indiana 8 05000316 AUTH~NAI<E AUTIIOR AFFILIATION

)ALEXICHFM.P, Indiana 8 Michigan Electr ic Co, RECIP~NAME RECIPIENT AFFILIATION DENTONFHBR

~Office of Nuclear Reactor Regulationi Director

SUBJECT:

Revised application for amend to License DPR 74.Amend reflects addi limitation on nuclear enthalpy rise hot channel factor due to new LOCA/ECCS analysis in support of Cycle 5 re'load.Application part of 8ff0301 submittal+

DISTRIBUTION CODE: IE26S COPIES RECEIVED:LTR ENCL g SIZEG j L 4, 2~I(, TITLE: Start-Up Repor t/Refueling Repor t (50 kt)NOTES: RECIPIENT ID CODE/NAME NRR ORB1 BC 04 INTERNAI.:

IE FILE Ol NRR/DHFS DIR 08 NRR/DSI/CPB 12 COPIES LTTR ENCL 3 3 1 1 1 1 1 1 RECIPIENT ID CODE/NAME NRR/DHFS DEPY07 NRR/DHFS/PSRB11 RM/DDAMI/MI B 09 COPIES LTTR ENCL EXTERNAL: ACRS 13 NRC PDR 02 NTIS 5 5 1 1 1 1 LPDR NSIC 03 05 COri)~~.e.Fi~TOTAL NUMBER OF.COPIES REQUIRED: LTTR 18 ENCL 18 It iin nn nIi I H)i'ii~

INDIANA 8 NICHIGAN ELECTRIC COMPANY P.O, BOX 16631 COLUMBUS, OHIO 43216 May 21, 1984 AEP:NRC:0860K Donald C.Cook Nuclear Plant Unit No.2 Docket No.50-316 License No.DPR-74 REVISION TO THE APPLICATION FOR CHANGES TO THE UNIT 2 TECHNICAL SPECIFICATION FOR THE CYCLE 5 RELOAD Mr.Harold R.Denton, Director Office of Nuclear Reactor Regulation U.S.Nuclear Regulatory Commission Washington, D.C.20555

Dear Mr.Denton:

This letter and its attachments constitute a revision to our application (AEP:NRC:0860, dated March 1, 1984)for amendment to the Donald C.Cook Nuclear Plant Unit No.2 Appendix A Technical Specifications (T/S).This proposed revision is in response to concerns raised by the NRC during the review of our proposed Unit 2 Cycle 5 reload license application.

Specifically, the proposed change reflects an additional limitation on the nuclear enthalpy rise hot channel factor (F I"), due to the new LOCA/ECCS bH analysis.The analysis was performed in support of the Cycle 5 reload as a result of your staff's review.Attachment 1 to this letter provides the results and bases of the new LOCA/ECCS analysis as it relates to F><.The analysis was performed by our fuels vendor (Exxon Nuclear, Co.).The results of this analysis were not available to us until May 18, 1984.We met with your staff on May 18, 1984 in an open meeting to discuss the results of the new analysis and our suggested T/S changes.We have revised the proposed T/S based on the NRC's comments.Due to the fact that our Unit 2 startup (i.e., entry into MODE 4)is currently scheduled for June 10, 1984 and that we, were only able to verify the need for the proposed change very recently, we request that the time for notice and publication in the Federal Register be shortened on schedule commensurate with our scheduled reload startup date;Based on our review, the proposed change to the technical specification is based on analytical methods which we were told were found acceptable to the NRC.In addition, the results of the analysis are within all acceptance criteria with respect to the ECCS.Therefore, we believe the proposed change does not involve a significant hazards consideration as defined in 10 CFR 50.92.In addition, since the proposed T/S keeps the plant within all design bases, the change will not adversely impact the environment.

':.8405290295 840521 ,'PDR ADOCK 05000316.sp;PDR CpP g II I Mr.Harold R.Den AEP: NRC: 0860K Attachment 2 to this letter contains the proposed revised T/S pages.The changes are indicated by vertical bars drawn on the right hand margin of the page.The proposed changes have been reviewed by the Plant Nuclear Safety Review Committee and will be reviewed by the Nuclear Safety and Design Review Committee at its next meeting.Pursuant to the requirement of 10 CFR 50.91(b)(1), a copy of this letter and its attachments have been transmitted to the State of Michigan.In addition, commensurate with our request for shortening the period for notice and publication in the Federal Register, we notified the State of Michigan by, telephone on May 21, 1984 of this requested amendment to our T/S.We consider this application for a licensee amendment to be part of the application submitted in our letter AEP:NRC:0860.

Therefore, we interpret.

10 CFR 170.22 as not requiring any additional payments for processing the aforementioned request.This document has been prepared following Corporate procedures which incorporate a reasonable set of controls to insure its accuracy and, completeness

'prior to signature by the undersigned.

Very truly your I M.P.Ale hach Vice Pre ident MPA/dew Attachment cc: John E.Dolan W.G.Smith, Jr.-Bridgman R.C.Callen G.Charnoff E.R.Swanson, NRC Resident Inspector-Bridgman 0 J!'1 p l, I 1 I ap I ll E Mr.Harold R.Dent AEP:NRC:0860K ATTACHMENT 1 The LOCA/ECCS analysis for Unit 2, Cycle 5 operation with up to five percent (5%)of the steam generator tubes plugged was performed by Exxon Nuclear Co.(ENC).The analysis was performed using the EXEM/PWR model with changes as explained in the ENC letter JCC:076:84 dated May 7, 1984.Letter JCC:076:84 was transmitted to you in our letter AEP:NRC:0860F, dated May ll, 1984.The results of the new ECCS/LOCA analysis are presented in the attached Tables 2.1, 3.2, 3.4, and Figures 3.41, 3.42, and 3.43.For breaks up to and including the double-ended severance o'f a reactor coolant pipe, the new analysis showed that the Unit 2 Emergency Core Cooling System will meet the acceptance criteria as presented in 10 CFR 50.46 for operation with ENC 17x17 fuel operating in accordance with the peaking factor limits noted in Table 2.1.That is: 1.The calculated'eak fuel element clad temperature o does not exceed the 2200 F limit.2.The amount of fuel element cladding that reacts chemically with water or steam does not exceed 1%of the total amount of zircaloy in the reactor.3.The cladding temperature transient is terminated at a time when the core geometry is still amenable to cooling.The hot fuel and cladding oxidation limits of 17%are not exceeded during or after quenching.

4.The core temperature is reduced and decay heat is removed for an extended period of time, as required by the long-lived radioactivity remaining in the core.Based on the new LOCA/ECCS analysis performed, the limit on F H, is 1.415.When included in the,T/S, this value is reduced by 4 0 to account for measurement uncertainty.

Thus the F<limit for operation at hH AH 100%power is 1.36.Xn addition to the above limitation, it was also necessary to change the allowance for increased F~based on reduced power when F~<is limited , AH H.by ECCS analyses, but not limited by Departure from Nucleate Boiling (DNB).This change is reflected by the phrase"F<~~1.36/P for Exxon Nuclear Co.fuel" included in the revised Technical Specifications.

e'I 1 4~(I~g P h C P'I g Pd W'g~i,'1)V C f.>J V f II)p II i U'"~"(1 III t I'I.'l I l Q)'V$f L l f%'J'l Lf'lg I'I l c i'I Mr.Harold R.Den f<J AEP:NRC:0860K bc: J.G.Feinstein J.M.Cleveland/G.

L.John/V.Vanderburg H.N.Scherer, Jr./S.H.Horowitz/R.

C.Carruth R.F.Hering/S.H.Steinhart/J.

A.Kobyra R.W.Jurgensen R.F.Kroeger T.P.Beilman-Bridgman J.F.Stietzel-Bridgman B.H.Bennett/F.

S.VanPelt, Jr.J.B.Shinnock D.Wigginton, NRC-Washington, D.C., AEP:NRC:0860K DC-N-6015.1 DC-N-6485'NMFM 233

,1 f 4'r~J f 3 l'I w f I'I