05000313/FIN-2016004-04: Difference between revisions

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| identified by = Licensee
| identified by = Licensee
| Inspection procedure =  
| Inspection procedure =  
| Inspector = B Correll, B Tindell, G Pick, J Choate, J Dixon, J Mateychick, M Phalen, M Tobin, N Greene, N O, 'Keefep Jayroe, R Deese, S Money, M Kirk
| Inspector = B Correll, B Tindell, G Pick, J Choate, J Dixon, J Mateychick, M Phalen, M Tobin, N Greene, N O'Keefe, P Jayroe, R Deese, S Money, M Kirk
| CCA = N/A for ROP
| CCA = N/A for ROP
| INPO aspect =  
| INPO aspect =  
| description =  During the fall 2016 Unit 1 refueling outage, the licensee foreign object search and retrieval (FOSAR) inspections in the steam generator bowls and reactor vessel identified a number of foreign objects, including an 8-inch metal rod. Discussions with the licensee indicated that some of the debris constituted foreign material that should have been prevented from being introduced into the RCS by the foreign material exclusion program. The inspectors concluded that the foreign material was most likely introduced during the previous refueling outage.  During the prior operating cycle, the licensees chemistry sampling identified increased RCS activity, and subsequent fuel bundle examinations of fuel removed from the core identified wear marks through the cladding of two adjacent fuel pins. The fuel assembly with the damage was not placed back into the RCS. Since there was no evidence of broken components inside the RCS, the licensee concluded that the most likely cause was the introduction of foreign material. While it was not possible to determine whether any of the foreign material had actually caused the fuel damage, the inspectors concluded that the licensee had failed to control foreign material and prevent it from entering the RCS.  Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities affecting quality shall be accomplished in accordance with documented instructions, procedures, or drawings of a type appropriate to the circumstances. Licensee Procedure EN-MA-118, Foreign Material Exclusion, Revision 10,  an Appendix B quality-related procedure, provides instructions for controlling foreign material. Procedure EN-MA-118, Step 5.5, requires, in part, that all material and tools that were introduced to the FME zone are accounted for. Contrary to the above, between January 25, and March 1, 2015, the licensee failed to ensure that all material and tools that were introduced to the FME zone were accounted for. Specifically, the licensee failed to maintain adequate FME control, leading to two damaged cladding pins and slightly elevated dose rates in the RCS piping, as well as another piece of metallic FME in the vessel, as documented in CR-ANO-1-2016-03340. This issue was documented in the licensees corrective action program under CR-ANO-1-2016-03521. Corrective actions taken include a search for the foreign material and permanent removal of the fuel assembly from the core.  Prior to 2012, the NRCs Significance Determination Process in IMC 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, contained guidance to screen all more than minor performance deficiencies affecting fuel barriers to very low safety significance. The inspection manual chapters were restructured in 2012, and the screening was inadvertently omitted, though the NRC was in the process of reinstating that same guidance. Therefore, after consultation with the Office of Nuclear Reactor Regulation, the inspectors determined that this finding is of very low safety significance (Green).  
| description =  During the fall 2016 Unit 1 refueling outage, the licensee foreign object search and retrieval (FOSAR) inspections in the steam generator bowls and reactor vessel identified a number of foreign objects, including an 8-inch metal rod. Discussions with the licensee indicated that some of the debris constituted foreign material that should have been prevented from being introduced into the RCS by the foreign material exclusion program. The inspectors concluded that the foreign material was most likely introduced during the previous refueling outage.  During the prior operating cycle, the licensees chemistry sampling identified increased RCS activity, and subsequent fuel bundle examinations of fuel removed from the core identified wear marks through the cladding of two adjacent fuel pins. The fuel assembly with the damage was not placed back into the RCS. Since there was no evidence of broken components inside the RCS, the licensee concluded that the most likely cause was the introduction of foreign material. While it was not possible to determine whether any of the foreign material had actually caused the fuel damage, the inspectors concluded that the licensee had failed to control foreign material and prevent it from entering the RCS.  Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, requires, in part, that activities affecting quality shall be accomplished in accordance with documented instructions, procedures, or drawings of a type appropriate to the circumstances. Licensee Procedure EN-MA-118, Foreign Material Exclusion, Revision 10,  an Appendix B quality-related procedure, provides instructions for controlling foreign material. Procedure EN-MA-118, Step 5.5, requires, in part, that all material and tools that were introduced to the FME zone are accounted for. Contrary to the above, between January 25, and March 1, 2015, the licensee failed to ensure that all material and tools that were introduced to the FME zone were accounted for. Specifically, the licensee failed to maintain adequate FME control, leading to two damaged cladding pins and slightly elevated dose rates in the RCS piping, as well as another piece of metallic FME in the vessel, as documented in CR-ANO-1-2016-03340. This issue was documented in the licensees corrective action program under CR-ANO-1-2016-03521. Corrective actions taken include a search for the foreign material and permanent removal of the fuel assembly from the core.  Prior to 2012, the NRCs Significance Determination Process in IMC 0609, Attachment 4, Phase 1 - Initial Screening and Characterization of Findings, contained guidance to screen all more than minor performance deficiencies affecting fuel barriers to very low safety significance. The inspection manual chapters were restructured in 2012, and the screening was inadvertently omitted, though the NRC was in the process of reinstating that same guidance. Therefore, after consultation with the Office of Nuclear Reactor Regulation, the inspectors determined that this finding is of very low safety significance (Green).  
}}
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Latest revision as of 11:55, 30 May 2018

04
Site: Arkansas Nuclear Entergy icon.png
Report IR 05000313/2016004 Section 4OA7
Date counted Dec 31, 2016 (2016Q4)
Type: NCV: Green
cornerstone No Cornerstone
Identified by: Licensee-identified
Inspection Procedure:
Inspectors (proximate) B Correll
B Tindell
G Pick
J Choate
J Dixon
J Mateychick
M Phalen
M Tobin
N Greene
N O'Keefe
P Jayroe
R Deese
S Money
M Kirk
Violation of: 10 CFR 50 Appendix B Criterion V
INPO aspect
'