05000498/LER-2024-004-01, Loss of Offsite Power Resulting in Unit 1 Automatic Reactor Trip and Actuation of Emergency Diesel Generators and Auxiliary Feedwater Pumps: Difference between revisions

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On July 24, 2024, STP Unit 1 experienced a Loss of Offsite Power (LOOP), resulting in an automatic reactor trip and actuation of all three Unit 1 Standby Diesel Generators (SBDG) and all four Auxiliary Feedwater (AFW) pumps. All three trains of Engineered Safety Feature (ESF) buses were energized and all equipment responded as expected without any complications with the exception of Steam Generator Power Operated Relief Valve "1C." Unit 2 experienced a partial LOOP and automatic actuation of SBDG 22 and one of four AFW pumps. The systems for each unit actuated due to the Switchyard experiencing electrical faults during the Shunt Reactor RT-2 fire event, which was caused by the insulation breakdown on the C-Phase (H3) GE Type U high-voltage bushing. Immediate corrective actions included restoring offsite power circuits. A Transmission Distribution Service Provider (TDSP) had not established and implemented adequate management controls governing design changes to equipment in the Switchyard to ensure that changes were consistent with design requirements and aligned with requirements and recommendations of applicable Industry Standards; and subsequently, STPNOC did not rigorously implement management controls during the review and approval of design changes developed by the TDSP. Planned corrective actions include enhancements to STP procedure 0PGP05-ZA-0002, "10CFR50.59 Evaluations" and development and implementation of written instructions that include management controls to govern the review and approval of all four TD63V' Switchyard changes.
On July 24, 2024, STP Unit 1 experienced a Loss of Offsite Power (LOOP), resulting in an automatic reactor trip and actuation of all three Unit 1 Standby Diesel Generators (SBDG) and all four Auxiliary Feedwater (AFW) pumps. All three trains of Engineered Safety Feature (ESF) buses were energized and all equipment responded as expected without any complications with the exception of Steam Generator Power Operated Relief Valve "1C." Unit 2 experienced a partial LOOP and automatic actuation of SBDG 22 and one of four AFW pumps. The systems for each unit actuated due to the Switchyard experiencing electrical faults during the Shunt Reactor RT-2 fire event, which was caused by the insulation breakdown on the C-Phase (H3) GE Type U high-voltage bushing. Immediate corrective actions included restoring offsite power circuits. A Transmission Distribution Service Provider (TDSP) had not established and implemented adequate management controls governing design changes to equipment in the Switchyard to ensure that changes were consistent with design requirements and aligned with requirements and recommendations of applicable Industry Standards; and subsequently, STPNOC did not rigorously implement management controls during the review and approval of design changes developed by the TDSP. Planned corrective actions include enhancements to STP procedure 0PGP05-ZA-0002, "10CFR50.59 Evaluations" and development and implementation of written instructions that include management controls to govern the review and approval of all four TD63V' Switchyard changes.
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Latest revision as of 01:56, 21 February 2026

Loss of Offsite Power Resulting in Unit 1 Automatic Reactor Trip and Actuation of Emergency Diesel Generators and Auxiliary Feedwater Pumps
ML25254A061
Person / Time
Site: South Texas  
Issue date: 09/11/2025
From: Norris R
South Texas
To:
Office of Nuclear Reactor Regulation, Document Control Desk
References
NOC-AE-25004126, STI: 35773211 LER 2024-004-01
Download: ML25254A061 (1)


LER-2024-004, Loss of Offsite Power Resulting in Unit 1 Automatic Reactor Trip and Actuation of Emergency Diesel Generators and Auxiliary Feedwater Pumps
Event date:
Report date:
4982024004R01 - NRC Website

text

......

Nuclear Operating Company IIIIIJ. ~

ATTN: Document Control Desk U.S. Nuclear Regulatory Commission Washington, DC 20555-0001 South Texas Project Units 1 and 2 September 11, 2025 NOC-AE-25004126 10 CFR 50.73 STI: 35773211 Docket Nos. STN 50-498 and STN 50-499 Licensee Event Report 2024-004-01 Supplement to Loss of Offsite Power Resulting in Unit 1 Automatic Reactor Trip and Actuation of Emergency Diesel Generators and Auxiliary Feedwater Pumps Reference: Letter; J. Tomlinson (STP) to Document Control Desk (NRC)- "Licensee Event Report 2024-004-00, Loss of Offsite Power Resulting in Unit 1 Automatic Reactor Trip and Actuation of Emergency Diesel Generators and Auxiliary Feedwater Pumps,"

September 19, 2024, (NOC-AE-24004064), (ML24263A145)

On September 19, 2024, STP Nuclear Operating Company (STPNOC) submitted the referenced Licensee Event Report. This letter is a supplement to the report to provide updates as a result of the causal investigation. The updated information is denoted by revision bars located in the right-hand margin. The report is submitted in accordance with 10 CFR 50. 73.

The event did not have an adverse effect on the health and safety of the public.

There are no commitments in this submittal.

If there are any questions regarding this submittal, please contact Chris Warren at (361) 972-7293 or me at (361) 972-7566.

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Robert B. Norris Site Vice President Attachment: Units 1 and 2 LER 2024-004-01, Supplement to Loss of Offsite Power Resulting in Unit 1 Automatic Reactor Trip and Actuation of Emergency Diesel Generators and Auxiliary Feedwater Pumps cc:

Regional Administrator, Region IV U.S. Nuclear Regulatory Commission 1600 E. Lamar Boulevard Arlington, TX 76011-4511

NOC-AE-25004126 Attachment Attachment Units 1 and 2 LER 2024-004-01 Units 1 and 2 LER 2024-004-01, Supplement to Loss of Offsite Power Resulting in Unit 1 Automatic Reactor Trip and Actuation of Emergency Diesel Generators and Auxiliary Feedwater Pumps

NRC FORM 366 (04-02-2024)

U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)

(See Page 2 for required number of digits/characters for each block)

(See NUREG-1022, R.3 for instruction and guidance for completing this form http://www.nrc.gov/reading-rm/doc-collections/nuregs/staff/sr1022/r3/)

APPROVED BY OMB: NO. 3150-0104 EXPIRES: 04/30/2027

1. Facility Name 052 050
2. Docket Number
3. Page 1 OF
4. Title
5. Event Date Month Day Year
6. LER Number Year Sequential Number Revision No.
7. Report Date Month Day Year
8. Other Facilities Involved Facility Name Facility Name Docket Number Docket Number
9. Operating Mode
10. Power Level 050 052

Month Day Year South Texas Project Unit 1

00498 5

Loss of Offsite Power Resulting in Unit 1 Automatic Reactor Trip and Actuation of Emergency Diesel Generators and Auxiliary Feedwater Pumps 07 24 2024 2024 004 01 0



2025 South Texas Project Unit 2 N/A 00499 1

100%

Chris Warren, Licensing Engineer 361-972-7293 X

N/A INS G080 Y

16. Abstract (Limit to 1326 spaces, i.e., approximately 13 single-spaced typewritten lines)

On July 24, 2024, STP Unit 1 experienced a Loss of Offsite Power (LOOP), resulting in an automatic reactor trip and actuation of all three Unit 1 Standby Diesel Generators (SBDG) and all four Auxiliary Feedwater (AFW) pumps. All three trains of Engineered Safety Feature (ESF) buses were energized and all equipment responded as expected without any complications with the exception of Steam Generator Power Operated Relief Valve "1C." Unit 2 experienced a partial LOOP and automatic actuation of SBDG 22 and one of four AFW pumps. The systems for each unit actuated due to the Switchyard experiencing electrical faults during the Shunt Reactor RT-2 fire event, which was caused by the insulation breakdown on the C-Phase (H3) GE Type U high-voltage bushing. Immediate corrective actions included restoring offsite power circuits. A Transmission Distribution Service Provider (TDSP) had not established and implemented adequate management controls governing design changes to equipment in the Switchyard to ensure that changes were consistent with design requirements and aligned with requirements and recommendations of applicable Industry Standards; and subsequently, STPNOC did not rigorously implement management controls during the review and approval of design changes developed by the TDSP. Planned corrective actions include enhancements to STP procedure 0PGP05-ZA-0002, "10CFR50.59 Evaluations" and development and implementation of written instructions that include management controls to govern the review and approval of all four TD63V' Switchyard changes.

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Summary of the Event Timeline (Note: All times are in Central Daylight Time)

Unit 1 - 07/24/2024 (0702) - Unit 1 reactor trip due to fire in the switchyard. The 345kV North Bus and the Unit 1 Generator tripped. All SBDGs automatically actuated and sequenced on a Loss of Offsite Power. The following busses were deenergized: 13.8kV Auxiliary busses 1F, 1G, 1H, and 1J, 13.8kV Standby busses 1F, 1H, and 1G, and 480V Load Center 1W.

Units 1 and 2 - 07/24/2024 (0702) - Due to loss of two independent offsite power circuits, entered Technical Specification 3.8.1.1, Action 'e'.

Unit 1 - 07/24/2024 (0702) - All four Reactor Coolant Pumps (RCP) lost power. Entered Technical Specification 3.4.1.2.

Unit 2 - 07/24/2024 (0703) - Report of explosion and fire in the switchyard. Entered off-normal procedure 0POP04-ZO-0008, Fire/Explosion.

Unit 1 - 07/24/2024 (0735) - Verified natural circulation with Steam Generator (S/G) Power Operated Relief Valves (PORV) open in Manual.

07/24/2024 (0800) - Bay City Fire Department arrive on site at the switchyard.

Unit 1 - 07/24/2024 (0848) - Spent Fuel Pool pump 1B is running, restoring cooling to the Spent Fuel Pool.

07/24/2024 (0925) - Fire in Shunt Reactor RT-2 is extinguished.

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South Texas Project Unit 1 00498 2024 004 01

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Timeline (Note: All times are in Central Daylight Time)

Unit 1 - 07/24/2024 (0953) - S/G PORV 1C declared inoperable and nonfunctional due to not operating in AUTO or MANUAL from the Control Room.

Unit 1 - 07/24/2024 (1054) - Completed NRC 4-hour Non-Emergency Notification under 10 CFR 50.72(b)(2)(iv)(B) for a Reactor Trip from 100% power (RPS actuation). Event Notification 57237.

Unit 1 - 07/24/2024 (1346) - Started Reactor Coolant Pump 1D. Reactor Coolant Loop D and its associated steam generator and reactor coolant pump are in operation with reactor trip breakers OPEN. Exited LCO 3.4.1.2, Action 'c'.

Unit 2 - 07/24/2024 (1350) - Both 345kV North and South buses are OPERABLE and all three ESF buses are powered by the Unit Auxiliary Transformer. Exited Technical Specification 3.8.1.1, Action 'e' and entered Action 'a.'

07/24/2024 (1455) - Completed NRC 8-hour non-emergency notification under 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in the valid actuation of a PWR auxiliary system and emergency AC electrical power system. Completed NRC 4-hour non-emergency notification under 10 CFR 50.72(b)(2)(xi) for the issuance of a news release. Event Notification EN 57237.

Unit 2 - 07/24/2024 (1537) - Normal offsite power to Unit 2 restored. Exited Technical Specification 3.8.1.1, Action 'a.'

Unit 1 - 07/25/2024 (0057) - Switchyard Breakers Y0520 and Y0510 closed. Main and Auxiliary transformers are energized.

Unit 1 - 07/25/2024 (0933) - Normal offsite power to Unit 1 restored. Exited Technical Specification 3.8.1.1, Action 'a'.

E. Method of Discovery

The event was self-revealing when Unit 1 experienced an automatic reactor trip coincident with a Loss of Offsite Power and actuation of the SBDGs for all three ESF buses.

II. Component Failures

A. Failure Mode, Mechanism, and Effects of Failed Components

Two independent failure analyses were performed and concluded that the Shunt Reactor RT-2 H3 GE Type U high-voltage bushing failed due to an insulation breakdown. The independent failure analyses could not determine the cause of the insulation breakdown due to extensive damage sustained during the event. The failure of the bushing resulted in the subsequent fire. The smoke plume reached the A-phase conductor associated with the Unit 1 Main Generator Transformer and the C-phase conductor associated with the No. 1 Standby Transformer, allowing phase-to-ground faults through the plume and the loss of two independent offsite transmission circuits.

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South Texas Project Unit 1 00498 2024 004 01

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3. LER NUMBER YEAR SEQUENTIAL NUMBER REV NO.

052 050

IV. Cause of Event

A Transmission Distribution Service Provider (TDSP) had not established and implemented adequate management controls governing design changes to equipment in the Switchyard to ensure that changes were consistent with design requirements and aligned with requirements and recommendations of applicable Industry Standards; and subsequently, STPNOC did not rigorously implement management controls during the review and approval of design changes developed by the TDSP. As a result, in 2014 the Shunt Reactors were relocated, and their associated circuit switchers were replaced with circuit breakers without adequately evaluating the change. Consequently, due to the relocation of Shunt Reactor 2, on July 24, 2024, a single bushing failure caused a fire that resulted in loss of the independent transmission circuits, which caused a loss of offsite power to Unit 1, and resulted in a partial loss of offsite power to Unit 2.

V. Corrective Actions

The following Corrective Actions are planned and tracked in the STP Corrective Action Program:

1. Revise STP procedure 0PGP05-ZA-0002, "10CFR50.59 Evaluations," to require 10CFR 50.59 Screenings and Evaluations address all elements of the change; and change the Usage category to "Referenced" as delineated in STP Procedure 0PAP01-ZA-0101, Plant Procedure Writers Guide.
2. Develop and implement written instructions that include management controls to govern the review and approval of Transmission Distribution Service Providers' procedure changes, design changes, tests or changes in the conduct of other activities which might affect compliance with regulatory requirements, the Updated Final Safety Analysis Report and/or NRC commitments involving the Switchyard and associated transmission lines and equipment which could affect offsite power supply to STP consistent with the South Texas Project Interconnection Agreement, Exhibit D,Section V, Review and Approval.

VI. Previous Similar Events

A review of events over the past 3 years did not identify any similar events with the same cause as this event.

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South Texas Project Unit 1 00498 2024 004 01

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